Design and Development of Double Helix Fuel Injection Pump for Four Stroke V-16 Rail Traction Diesel Engine

Author(s):  
A. K. Kathpal ◽  
Anirudh Gautam ◽  
Avinash Kumar Agarwal ◽  
R. Baskaran

The diesel fuel-injection system of ALCO DLW 251 engine consists of single cylinder injection pumps, delivery pipes, and fuel injector nozzles. Fuel injection into the combustion chamber through multi-hole nozzles delivers designed power and fuel efficiency. The two most important variables in a fuel injection system of a diesel engine are the injection pressure and injection timing. Proper timing of the injection process is essential for satisfactory diesel engine operation and performance. Injection timing needs to be optimised for an engine based on requirements of power, fuel economy, mechanical and thermal loading limitations, smoke and emissions etc. Since each of these requirements varies with the operating conditions, sometimes contrary to the requirements of the other parameters, the map of optimised injection timing can be very complex. The ALCO DLW 251 engine’s fuel injection pump is jerk type to permit accurate metering and timing of the fuel injected. The pump has a ported barrel and constant-stroke plunger incorporating a bottom helix for fuel delivery control with constant injection timing. From the point of view of good power and fuel economy, combustion should take place so that the peak firing pressure occurs at about 10–15° after TDC and is usually a few degrees after combustion starts. For this to happen, fuel should be injected at an appropriate time, depending on Injection delay and Ignition delay. Both these factors are dependent on the speed and load. Changing the operating point of the engine may change either one or both types of delay, altering the moment of start of combustion. Various researchers have shown that both the Injection and the Ignition delay are reduced as the engine speed is decreased resulting in advancement of injection timing at lower speeds (and loads). This condition will be corrected by varying the static injection timing, which can be achieved by providing a modified helix on the plunger to delay the start of fuel injection, for the lower speeds and loads. A new double helix (upper and lower helix) fuel injection pump for the ALCO DLW 251 16 V engine has been designed. The new fuel injection pump has been tested on the engine test cell at Research Designs & Standards Organisation and has shown an improvement of 1.2% in locomotive duty cycle fuel consumption. This paper describes the design & development of double helix fuel injection pump and discusses the engine tests completed to verify the projected improvements in fuel efficiency.

Author(s):  
Anirudh Gautam ◽  
Prem Chandra ◽  
Kamlesh Kumar ◽  
Mani Ram Sharma ◽  
Sanjeet Kumar ◽  
...  

An electronic fuel injection system for a 4-stroke, 16 cylinders, V-configuration, medium speed, large bore locomotive diesel engine has been developed and successfully retrofitted on a rebuilt diesel locomotive. The engine employs a Pump-Line-Nozzle (PLN) system of fuel injection into the cylinder. Original fuel injection system used is a mechanical fuel injection pump connected to a mechanical fuel injector through a high pressure fuel line. The fuel injection pump meters the fuel delivery using a single helix machined on its plunger. The fuel injection timings are however optimized only for the rated speed and load resulting in non-optimised operation at other engine operating points. An electronic fuel injection pump having a solenoid valve for both fuel metering and injection timing along with ECU has been developed for retrofitment on rebuilt diesel locomotives. Interfacing of the ECU to the engine test cell controller has been done by developing suitable hardware and software. ECU calibration has been done and various maps of the engine have been developed. The engine was tested on the engine test bed. High pressure injector, modified fuel headers, fuel connection systems, a new high capacity fuel pump and layout of the wire harness were installed. After thorough testing and debugging, the EFI kit has been retrofitted on a rebuilt diesel locomotive and tested on load box followed by brief field trials. A savings of 4% fuel consumption over the duty cycle has been obtained. In addition there is an appreciable reduction in the smoke emissions during steady-state as well as transient operations.


2011 ◽  
Vol 148-149 ◽  
pp. 1504-1509
Author(s):  
Li Yan Feng ◽  
Bao Guo Du ◽  
Jia Xing Li ◽  
Xin Liu

This paper presents the endeavor to use Heavy Fuel Oil on a medium-speed diesel engine. The researched engine is a locomotive diesel engine, which used to be only fuelled with light diesel fuel. Since the fuel injection system of the original engine is unfit for HFO, the authors reformed the fuel injection system to meet the requirements of using HFO. In order to decrease the viscosity of the fuel, light diesel fuel was blended with HFO and heating apparatus was applied. A serial of experiments were carried out to check the performance of the reformed engine. Meanwhile, 1-D engine working cycle simulation tool was employed to study the fuel economy and combustion performance of the engine. The results indicate that compared with using light diesel fuel, when using HFO, the engine’s power performance was maintained, and the brake specific fuel consumption was increased. But considering lower price of heavy fuel oil, the fuel economy was greatly improved.


2019 ◽  
Vol 179 (4) ◽  
pp. 75-79
Author(s):  
Łukasz GRABOWSKI ◽  
Paweł KARPIŃSKI ◽  
Grzegorz BARAŃSKI

This paper presents the results of experimental studies of the opposed-piston diesel engine. This engine was designed during one of the stages of the research on a new-type drive unit for gyrocopter applications. In order to conduct research, a special test stand as well as control and measurement systems were developed. As part of the work on the engine, the fuel injection system, engine temperature control system and measurement systems were designed. In addition, a computer program has been developed for the fuel injection system control (injectors, valves fuel pressure regulators). The paper presents the results of the preliminary tests for a single value of engine speed (1500 rpm) and three values of load defined by torque. The measured value of the indicated pressure made it possible to calculate the maximum pressure. The results obtained from the bench tests were analyzed.


Energies ◽  
2019 ◽  
Vol 12 (12) ◽  
pp. 2413 ◽  
Author(s):  
Lebedevas ◽  
Pukalskas ◽  
Daukšys ◽  
Rimkus ◽  
Melaika ◽  
...  

This paper presents a study on the energy efficiency and emissions of a converted high-revolution bore 79.5 mm/stroke 95 mm engine with a conventional fuel injection system for operation with dual fuel feed: diesel (D) and natural gas (NG). The part of NG energy increase in the dual fuel is related to a significant deterioration in energy efficiency (ηi), particularly when engine operation is in low load modes and was determined to be below 40% of maximum continuous rating. The effectiveness of the D injection timing optimisation was established in high engine load modes within the range of a co-combustion ratio of NG ≤ 0.4: with an increase in ηi, compared to D, the emissions of NOx+ HC decreased by 15% to 25%, while those of CO2 decreased by 8% to 16%; the six-fold CO emission increase, up to 6 g/kWh, was unregulated. By referencing the indicated process characteristics of the established NG phase elongation in the expansion stroke, the combustion time increase as well as the associated decrease in the cylinder excess air ratio (α) are possible reasons for the increase in the incomplete combustion product emission.


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