Full-Coverage Film Cooling: Film Effectiveness and Heat Transfer Coefficients for Dense and Sparse Hole Arrays at Different Blowing Ratios

2012 ◽  
Vol 134 (6) ◽  
Author(s):  
Phil Ligrani ◽  
Matt Goodro ◽  
Mike Fox ◽  
Hee-Koo Moon

Experimental results are presented for a full coverage film cooling arrangement which simulates a portion of a gas turbine engine, with appropriate streamwise static pressure gradient and varying blowing ratio along the length of the contraction passage which contains the cooling hole arrangement. Film cooling holes are sharp-edged, streamwise inclined at 20 deg with respect to the liner surface, and are arranged with a length to diameter ratio of 8.35. The film cooling holes in adjacent streamwise rows are staggered with respect to each other. Data are provided for turbulent film cooling, contraction ratios of 1 and 4, blowing ratios (at the test section entrance) of 2.0, 5.0, and 10.0, coolant Reynolds numbers Refc from 10,000 to 12,000 (for a blowing ratio of 5.0), freestream temperatures from 75 °C to 115 °C, a film hole diameter of 7 mm, and density ratios from 1.15 to 1.25. Changes to X/D and Y/D, nondimensional streamwise and spanwise film cooling hole spacings, with Y/D of 3, 5, and 7, and with X/D of 6 and 18, are considered. For all X/D=6 hole spacings, only a slight increase in effectiveness (local, line-averaged, and spatially-averaged) values are present as the blowing ratio increases from 2.0 to 5.0, with no significant differences when the blowing ratio increases from 5.0 to 10.0. This lack of dependence on blowing ratio indicates a condition where excess coolant is injected into the mainstream flow, a situation not evidenced by data obtained with the X/D=18 hole spacing arrangement. With this sparse array configuration, local and spatially-averaged effectiveness generally increase continually as the blowing ratio becomes larger. Line-averaged and spatially-averaged heat transfer coefficients are generally higher at each streamwise location, also with larger variations with streamwise development, with the X/D=6 hole array, compared to the X/D=18 array.

Author(s):  
Matt Goodro ◽  
Phil Ligrani ◽  
Mike Fox ◽  
Hee-Koo Moon

Experimental results are presented for a full coverage film cooling arrangement which simulates a portion of a gas turbine engine, with appropriate streamwise static pressure gradient and varying blowing ratio along the length of the contraction passage which contains the cooling hole arrangement. Film cooling holes are sharp-edged, streamwise inclined at 20° with respect to the liner surface, and are arranged with a length to diameter ratio of 8.35. The film cooling holes in adjacent streamwise rows are staggered with respect to each other. Data are provided for turbulent film cooling, contraction ratios of 1 and 4, blowing ratios (at the test section entrance) of 2.0, 5.0, and 10.0, coolant Reynolds numbers Refc from 10,000 to 12,000, freestream temperatures from 75°C to 115°C, a film hole diameter of 7 mm, and density ratios from 1.15 to 1.25. Changes to X/D and Y/D, non-dimensional streamwise and spanwise film cooling hole spacings, with Y/D of 3, 5, and 7, and with X/D of 6 and 18, are considered. For all X/D = 6 hole spacings, only a slight increase in effectiveness (local, line-averaged, and spatially-averaged) values are present as the blowing ratio increases from 2.0 to 5.0, with no significant differences when the blowing ratio increases from 5.0 to 10.0. This lack of dependence on blowing ratio indicates a condition where excess coolant is injected into the mainstream flow, a situation not evidenced by data obtained with the X/D = 18 hole spacing arrangement. With this sparse array configuration, local and spatially-averaged effectiveness generally increase continually as the blowing ratio becomes larger. Line-averaged and spatially-averaged heat transfer coefficients are generally higher at each streamwise location, also with larger variations with streamwise development, with the X/D = 6 hole array, compared to the X/D = 18 array.


2013 ◽  
Vol 135 (3) ◽  
Author(s):  
Phil Ligrani ◽  
Matt Goodro ◽  
Mike Fox ◽  
Hee-Koo Moon

Experimental results are presented for a full-coverage film cooling arrangement which simulates a portion of a gas turbine engine, with appropriate streamwise static pressure gradient. The test surface utilizes varying blowing ratio (BR) along the length of the contraction passage which contains the cooling hole arrangement. For the different experimental conditions examined, film cooling holes are sharp-edged and streamwise inclined either at 20 deg or 30 deg with respect to the liner surface. The film cooling holes in adjacent streamwise rows are staggered with respect to each other. Data are provided for turbulent film cooling, contraction ratios of 1, 3, 4, and 5, blowing ratios (at the test section entrance) of 2.0, 5.0, and 10.0, coolant Reynolds numbers Refc of 10,000–12,000, freestream temperatures from 75 °C to 115 °C, a film hole diameter of 7 mm, and density ratios from 1.15 to 1.25. Nondimensional streamwise and spanwise film cooling hole spacings, X/D and Y/D, are 6, and 5, respectively. When the streamwise hole inclination angle is 20 deg spatially averaged and line-averaged adiabatic effectiveness values at each x/D location are about the same as the contraction ratio varies between 1, 3, and 4, with slightly higher values at each x/D location when the contraction ratio Cr is 5. For each contraction ratio, there is a slight increase in effectiveness when the blowing ratio is increased from 2.0 to 5.0 but there is no further substantial improvement when the blowing ratio is increased to 10.0. Overall, line-averaged and spatially averaged-adiabatic film effectiveness data, and spatially averaged heat transfer coefficient data are described as they are affected by contraction ratio, blowing ratio, hole angle α, and streamwise location x/D. For example, when α = 20 deg, the detrimental effects of mainstream acceleration are apparent since heat transfer coefficients for contraction ratios Cr of 3 and 5 are often higher than values for Cr = 1, especially for x/D > 100.


Author(s):  
Matt Goodro ◽  
Phil Ligrani ◽  
Mike Fox ◽  
Hee-Koo Moon

Experimental results are presented for a full coverage film cooling arrangement which simulates a portion of a gas turbine engine, with appropriate streamwise static pressure gradient. The test surface utilizes varying blowing ratio along the length of the contraction passage which contains the cooling hole arrangement. For the different experimental conditions examined, film cooling holes are sharp-edged and streamwise inclined either at 20° or 30° with respect to the liner surface. The film cooling holes in adjacent streamwise rows are staggered with respect to each other. Data are provided for turbulent film cooling, contraction ratios of 1, 3, 4, and 5, blowing ratios (at the test section entrance) of 2.0, 5.0, and 10.0, coolant Reynolds numbers Refc of 10,000 to 12,000, freestream temperatures from 75°C to 115°C, a film hole diameter of 7 mm, and density ratios from 1.15 to 1.25. Non-dimensional streamwise and spanwise film cooling hole spacings, X/D and Y/D, are 6, and 5, respectively. When the streamwise hole inclination angle is 20°, spatially-averaged and line-averaged adiabatic effectiveness values at each x/D location are about the same as the contraction ratio varies between 1, 3, and 4, with slightly higher values at each x/D location when the contraction ratio Cr is 5. For each contraction ratio, there is a slight increase in effectiveness when the blowing ratio is increased from 2.0 to 5.0 but there is no further substantial improvement when the blowing ratio is increased to 10.0. Overall, line-averaged and spatially-averaged adiabatic film effectiveness data, and spatially-averaged heat transfer coefficient data are described as they are affected by contraction ratio, blowing ratio, hole angle α, and streamwise location x/D. For example, when α = 20°, the detrimental effects of mainstream acceleration are apparent since heat transfer coefficients for contraction ratios Cr of 3 and 5 are often higher than values for Cr = 1, especially for x/D > 100.


Author(s):  
Phillip Ligrani ◽  
Matt Goodro ◽  
Michael D. Fox ◽  
Hee-Koo Moon

The present experimental investigation considers a full coverage film cooling arrangement with differrent streamwise static pressure gradients. The film cooling holes in adjacent streamwise rows are staggered with respect to each other, with sharp edges, and streamwise inclination angles of 20 degrees with respect to the liner surface. Data are provided for turbulent film cooling, contraction ratios of 1 and 4, blowing ratios (at the test section entrance) of 2.0, 5.0, and 10.0, coolant Reynolds numbers of 12,000, freestream temperatures from 75°C to 115°C, a film hole diameter of 7 mm, and density ratios from 1.15 to 1.25. Non-dimensional streamwise and spanwise film cooling hole spacings, X/D and Y/D, are 18, and 5, respectively. Data illustrating the effects of contraction ratio, blowing ratio, and streamwise location on local, line-averaged and spatially-averaged adiabatic film effectiveness data, and on local, line-averaged and spatially-averaged heat transfer coefficient data are presented. Varying blowing ratio values are utilized along the length of the contraction passage, which contains the cooling hole arrangement, when contraction ratio is 4. Dependence on blowing ratio indicates important influences of coolant concentration and distribution. For example, line-averaged and spatially-averaged adiabatic effectiveness data show vastly different changes with blowing ratio BR for the configurations with contraction ratios of 1 and 4. These changes from acceleration are thus mostly due to different blowing ratio distributions along the test section. In particular, much larger effectiveness alterations are present as BR changes from 2.0 to 10.0, when significant acceleration is present and Cr = 4 (in comparison with the Cr = 1 data). When BR = 10.0, much smaller changes due to different contract ratios are present. This is because coolant distributions along the test surfaces are so abundant that magnitudes of streamwise acceleration (and different streamwise variations of blowing ratio) have little effect on near-wall film concentration distributions, or on variations of film cooling effectiveness.


2015 ◽  
Vol 137 (3) ◽  
Author(s):  
Phil Ligrani ◽  
Matt Goodro ◽  
Michael D. Fox ◽  
Hee-Koo Moon

The present experimental investigation considers a full coverage film cooling arrangement with different streamwise static pressure gradients. The film cooling holes in adjacent streamwise rows are staggered with respect to each other, with sharp edges and streamwise inclination angles of 20 deg with respect to the liner surface. Data are provided for turbulent film cooling, contraction ratios of 1 and 4, blowing ratios (BRs) (at the test section entrance) of 2.0, 5.0, and 10.0, a coolant Reynolds number of 12,000, freestream temperatures from 75 °C to 115 °C, a film hole diameter of 7 mm, and density ratios from 1.15 to 1.25. Nondimensional streamwise and spanwise film cooling hole spacings, X/D and Y/D, are 18 and 5, respectively. Data illustrating the effects of contraction ratio, BR, and streamwise location on local, line-averaged, and spatially averaged adiabatic film effectiveness data; and on local, line-averaged and spatially averaged heat transfer coefficient data are presented. Varying BR values are present along the length of the contraction passage, which contains the cooling hole arrangement, when contraction ratio is 4. Dependence on BR indicates important influences of coolant concentration and distribution. For example, line-averaged and spatially averaged adiabatic effectiveness data show vastly different changes with BR for the configurations with contraction ratios of 1 and 4. In addition, much larger effectiveness alterations are present as BR changes from 2.0 to 10.0, when significant acceleration is present and Cr = 4 (in comparison with the Cr = 1 data).


Author(s):  
Jin Wang ◽  
Yong Yu ◽  
M. Zeng ◽  
Q. W. Wang

Three-dimensional simulations of the squealer tip on the GE-E3 blade with eight film cooling holes were carried out. The effect of different blade spans and different blowing ratios on the tip flow and cooling performance was revealed with the k-ε model. For the squealer tip, the depth of the cavity and the height of the tip clearance were fixed, the influence of different spans (10%, 25%, 50%, 75% and 100% span) on the tip heat transfer was investigated. It was found that the velocity field above the blade tip and the heat transfer distribution on the groove floor for the 10% span (cut-back span) model had no difference from that for the 100% span (whole span) model obviously. However, the leakage flow for the 10% span model showed larger interaction with the passage flow. With different spans, the effect of different blowing ratios, i.e., M = 0.4, 0.8 and 1.2, was investigated. Increasing the blowing ratio (from M = 0.4 to 1.2) increased the film cooling effectiveness and made the heat transfer coefficients of all the models smaller. Because the cut-back model for the 10% span had similar tip flow field with the 100% span model, the simulation for the 10% span model could be used to find out the tip flow and heat transfer for the 100% span model.


2003 ◽  
Vol 125 (4) ◽  
pp. 648-657 ◽  
Author(s):  
Jae Su Kwak ◽  
Je-Chin Han

Experimental investigations were performed to measure the detailed heat transfer coefficients and film cooling effectiveness on the squealer tip of a gas turbine blade in a five-bladed linear cascade. The blade was a two-dimensional model of a first stage gas turbine rotor blade with a profile of the GE-E3 aircraft gas turbine engine rotor blade. The test blade had a squealer (recessed) tip with a 4.22% recess. The blade model was equipped with a single row of film cooling holes on the pressure side near the tip region and the tip surface along the camber line. Hue detection based transient liquid crystals technique was used to measure heat transfer coefficients and film cooling effectiveness. All measurements were done for the three tip gap clearances of 1.0%, 1.5%, and 2.5% of blade span at the two blowing ratios of 1.0 and 2.0. The Reynolds number based on cascade exit velocity and axial chord length was 1.1×106 and the total turning angle of the blade was 97.9 deg. The overall pressure ratio was 1.2 and the inlet and exit Mach numbers were 0.25 and 0.59, respectively. The turbulence intensity level at the cascade inlet was 9.7%. Results showed that the overall heat transfer coefficients increased with increasing tip gap clearance, but decreased with increasing blowing ratio. However, the overall film cooling effectiveness increased with increasing blowing ratio. Results also showed that the overall film cooling effectiveness increased but heat transfer coefficients decreased for the squealer tip when compared to the plane tip at the same tip gap clearance and blowing ratio conditions.


2017 ◽  
Vol 139 (5) ◽  
Author(s):  
Nathan Rogers ◽  
Zhong Ren ◽  
Warren Buzzard ◽  
Brian Sweeney ◽  
Nathan Tinker ◽  
...  

Experimental results are presented for a double wall cooling arrangement which simulates a portion of a combustor liner of a gas turbine engine. The results are collected using a new experimental facility designed to test full-coverage film cooling and impingement cooling effectiveness using either cross flow, impingement, or a combination of both to supply the film cooling flow. The present experiment primarily deals with cross flow supplied full-coverage film cooling for a sparse film cooling hole array that has not been previously tested. Data are provided for turbulent film cooling, contraction ratio of 1, blowing ratios ranging from 2.7 to 7.5, coolant Reynolds numbers based on film cooling hole diameter of about 5000–20,000, and mainstream temperature step during transient tests of 14 °C. The film cooling hole array consists of a film cooling hole diameter of 6.4 mm with nondimensional streamwise (X/de) and spanwise (Y/de) film cooling hole spacing of 15 and 4, respectively. The film cooling holes are streamwise inclined at an angle of 25 deg with respect to the test plate surface and have adjacent streamwise rows staggered with respect to each other. Data illustrating the effects of blowing ratio on adiabatic film cooling effectiveness and heat transfer coefficient are presented. For the arrangement and conditions considered, heat transfer coefficients generally increase with streamwise development and increase with increasing blowing ratio. The adiabatic film cooling effectiveness is determined from measurements of adiabatic wall temperature, coolant stagnation temperature, and mainstream recovery temperature. The adiabatic wall temperature and the adiabatic film cooling effectiveness generally decrease and increase, respectively, with streamwise position, and generally decrease and increase, respectively, as blowing ratio becomes larger.


Author(s):  
M. Gritsch ◽  
A. Schulz ◽  
S. Wittig

Detailed measurements of heat transfer coefficients in the nearfield of three different film-cooling holes are presented. The hole geometries investigated include a cylindrical hole and two holes with a diffuser shaped exit portion (i.e. a fan-shaped and a laidback fanshaped hole). They were tested over a range of blowing ratios M = 0.25…1.75 at an external crossflow Mach number of 0.6 and a coolant-to-mainflow density ratio of 1.85. Additionally, the effect of the internal coolant supply Mach number is addressed. Temperatures of the diabatic surface downstream of the injection location are measured by means of an infrared camera system. They are used as boundary conditions for a finite element analysis to determine surface heat fluxes and heat transfer coefficients. The superposition method is applied to evaluate the overall film-cooling performance of the hole geometries investigated. As compared to the cylindrical hole, both expanded holes show significantly lower heat transfer coefficients downstream of the injection location, particularly at high blowing ratios. The laidback fanshaped hole provides a better lateral spreading of the injected coolant than the fanshaped hole which leads to lower laterally averaged heat transfer coefficients. Coolant passage crossflow Mach number affects the flowfield of the jet being ejected from the hole and, therefore, has an important impact on film-cooling performance.


Author(s):  
Sumanta Acharya ◽  
Huitao Yang ◽  
Srinath V. Ekkad ◽  
Chander Prakash ◽  
Ron Bunker

Numerical simulations of flow and heat transfer are presented for a GE-E3 turbine blade with a film-cooled tip. Results are presented for both a flat tip and a squealer tip. Straight-through coolant holes are considered, and the calculation domain includes the flow development in the coolant delivery tubes. Results are presented with three different tip gaps representing 1%, 1.5% and 2.5% of blade span, a blowing ratio (ratio of coolant-jet-exit velocity to average passage flow velocity) of 1, and an inlet turbulence intensity of 6.1%. On a flat tip, film coolant injection is shown to lower the local pressure ratio and alters the nature of the leakage vortex. High film cooling effectiveness and low heat transfer coefficients are obtained along the coolant trajectory; these values increase slightly with increasing tip clearances. For a squealer tip, the flow inside the squealer cavity exhibits streamwise directed flow, which alters the trajectory of the coolant jets and reduces their effectiveness.


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