APLIKASI PROSES BIOLOGI ANAEROBIK PADA PENGOLAHAN AIR LIMBAH ORGANIK BERKONSENTRASI GARAM TINGGI “STUDI KASUS INDUSTRI UME BOSHI”

2018 ◽  
Vol 1 (2) ◽  
Author(s):  
Ikbal Mahmud

Anaerobic treatment of wastewater with high organic and salt content but low pH (TOC, 14 g/l; salt, 150 g/l; pH,2.7) generated during an “ume boshi” manufacturing process was investigated. Five-fold-diluted “ume boshi” effluent was treated by a draw-and-fill method at a volumetric TOC (total organic carbon) loading rate of 3.0  g/l/d with a TOC removal efficiency of 75%. Five-fold-diluted “ome boshi” effluent was also treated in an anaerobic fluidized-bed reactor (AFBR) at a maximum volumetric TOC loading rate of 3.0 g/l/d, which gave almost the same results as the draw-and-fill method. However, ten-fold-diluted “ome boshi” effluent could be treated in the AFBR at a maximum volumetric TOC loading rate of 11 g/l/d with a TOC removal efficiency of 85%. The methane content in the evolved gas was high, being 70%. The red pigment in the “ome boshi” effluent was completely decolorized by the anaerobic treatment.  Key words :, Anaerobic fluidized-bed reactor, “Ume boshi”Co2+ and Ni2+ ions, decolorization

2017 ◽  
Vol 1 (1) ◽  
Author(s):  
Ikbal Mahmud

Anaerobic treatment of synthetic wastewater with a high NaCl content was investigated for its effect on the process. The synthetic wastewater, including NaCl up to 40 g/l, was treated anaerobically by draw-and-fill method at a treatment temperature of 37℃ and volumetric loading of rate TOC of 1 g/l/d. TOC removal efficiency and rate of gas evolution rate gradually decreased as salt content increased, although stable operation was maintained. TOC removal efficiency remained high at concentration of NaCl up to 20 g/l, although it fell to 82 % at 30 g NaCl/l. The gas yield at 10, 20 and 30 g NaCl/l were 1.35; 1.10 and 1.00 l/g-TOC loaded, which corresponded to 96; 83 and 78% of that without NaCl, respectively. The content of methane in the evolved gas was 50 to 55% throughout the experiment. Stable operation could not be maintained at 40 g NaCl/l since the TOC removal efficiency gradually decreased with the rapid increased in levels of volatile fatty acidsKata kunci : fermentasi metana, garam NaCl, konduktifitas, asam-asam organik, biogas 


2000 ◽  
Vol 41 (4-5) ◽  
pp. 245-251 ◽  
Author(s):  
P. Castilla ◽  
M. Meraz ◽  
O. Monroy ◽  
A. Noyola

Low concentration synthetic and municipal wastewaters were treated at HRT as short as 3 and 0.6 h respectively in an anaerobic inverse fluidized bed. Both bioreactors showed gas hold up due to the liquid downflow pattern of the prototype. The bioreactor operated at 3 h had a removal efficiency of 83%, specific activity of 4.5 kg CODremoved/kg IVS (d and the gas hold up varied from 23 to 55%. The reactor treating municipal wastewater had a removal efficiency of 44% when operating at 0.6 h, the specific activity was 4.2 kg CODremoved/kg IVS (d and no biogas was detected apparently because an important fraction was dissolved in the liquid phase. The biomass concentration was 13.8 and 1.1 kg IVS/m3 for synthetic and municipal wastewater and the SEM microphotographs showed a bacterial diversity for the first run and only cocci cells for the second run. The system does not remove suspended solids, so a polishing postreatment to improve water quality has to be implemented.


2016 ◽  
Vol 73 (10) ◽  
pp. 2446-2452 ◽  
Author(s):  
B. Düppenbecker ◽  
P. Cornel

This study focuses on the anaerobic treatment of sulfate-containing municipal wastewater at 20 °C with a fluidized bed reactor. Mean influent chemical oxygen demand (COD) and sulfate concentrations were 481 and 96 mg/l. The response of the COD removal efficiency to increasing organic loading rates (OLR) was investigated. Average total COD removal was 61% at OLR between 2.7 and 13.7 kg COD/(m³·d) and did not distinctly depend on the OLR. To assess the removal efficiency in more detail the COD in- and output mass flows were balanced. The results showed that only 11–12% of the input COD was recovered as gaseous methane. About 12–13% of the input COD remained in the effluent as dissolved methane. Furthermore, a distinct amount of 12–19% of the input COD remained in the reactor as settled sludge and was not further biologically degraded. Due to the reduction by sulfate-reducing bacteria, 13–14% of the input COD was degraded. Further adverse impacts of the influent sulfate on the anaerobic treatment process are discussed as well.


2001 ◽  
Vol 44 (6) ◽  
pp. 141-147 ◽  
Author(s):  
R. Saravanane ◽  
D. V.S. Murthy ◽  
K. Krishnaiah

Starch manufacturing industrial units, such as sago mills, both at medium and large scale, suffer from inadequate treatment and disposal problems due to high concentration of suspended solid content present in the effluent. In order to investigate the viability of treatment of sago effluent, a laboratory scale study was conducted. The treatment of sago effluent was studied in a continuous flow anaerobic fluidized bed reactor. The start-up of the reactor was carried out using a mixture of digested supernatant sewage sludge and cow dung slurry in different proportions. The effect of operating variables such as COD of the effluent, bed expansion, minimum fluidization velocity on efficiency of treatment and recovery of biogas was investigated. The treated wastewater was analysed for recycling and reuse to ensure an alternative for sustainable water resourse management. The maximum efficiency of treatment was found to be 82% and the nitrogen enriched digested sludge was recommended for agricultural use.


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