Measurement Uncertainty Analysis in Determining Adiabatic Film Cooling Effectiveness by Using Pressure Sensitive Paint Technique

2016 ◽  
Vol 138 (12) ◽  
Author(s):  
Blake Johnson ◽  
Hui Hu

While pressure sensitive paint (PSP) technique has been widely used to measure adiabatic film cooling effectiveness distributions on the surfaces of interest based on a mass transfer analog to traditional thermal-based measurements, very little can be found in literature to provide a comprehensive analysis on the uncertainty levels of the measured film cooling effectiveness distributions derived from PSP measurements. In the present study, a detailed analysis is performed to evaluate the effects of various associated uncertainties in the PSP measurements on the measured film cooling effectiveness distributions over the surfaces of interest. The experimental study is conducted in a low-speed wind tunnel under an isothermal condition. While airflow is used to represent the “hot” mainstream flow, an oxygen-free gas, i.e., carbon dioxide (CO2) gas with a density ratio of DR = 1.5 for the present study, is supplied to simulate the “coolant” stream for the PSP measurements to map the adiabatic film cooling effectiveness distribution over a flat test plate with an array of five cylindrical coolant holes at a span-wise spacing of three diameters center-to-center. A comprehensive analysis was carried out with focus on the measurement uncertainty and process uncertainty for the PSP measurements to determine the film cooling effectiveness distributions over the surface of interest. The final analysis indicates that the total uncertainty in the adiabatic film cooling effectiveness measurements by using the PSP technique depends strongly on the local behavior of the mixing process between the mainstream and coolant flows. The measurement uncertainty is estimated as high as 5% at the near field behind the coolant holes. In the far field away from the coolant holes, the total measurement uncertainty is found to be more uniform throughout the measurement domain and generally lower than those in the near field at about 3%.

Author(s):  
Blake Everett Johnson ◽  
Hui Hu

Pressure sensitive paint (PSP) is useful for measurements of wall pressure in high speed flows, but can be used in an alternative manner in low-speed flows as a gas species concentration detector. Film cooling technology studies have been greatly aided by this use of PSP through use of a mass transfer analogy to determine the adiabatic film cooling effectiveness. The PSP technique allows measurements that have high spatial resolution at high enough sampling rate that a good statistical mean can be determined rapidly. Due to the potential of this technique to deliver high quality adiabatic effectiveness measurements, a detailed analysis of its associated uncertainty is presented herein. In this study, an ambient temperature low speed wind tunnel drives air as the main flow while carbon dioxide (CO2, DR=1.5) is used as the “coolant” gas, though the experiments are done under isothermal conditions. A detailed analysis of the technique is performed here with focus on the measurement uncertainty and process uncertainty for a film cooling study using an array of five cylindrical holes spaced across the span of a flat test plate at a spacing of three diameters center-to-center. The final analysis indicates that the total uncertainty depends strongly on the local behavior of the coolant, with near-field uncertainty as high as 5% at isolated points. In the far-field, the total uncertainty is more uniform throughout the measurement domain and generally lower, at about 3%.


Author(s):  
A. Suryanarayanan ◽  
B. Ozturk ◽  
M. T. Schobeiri ◽  
J. C. Han

Film cooling effectiveness is measured on a rotating turbine blade platform for coolant injection through discrete holes using pressure sensitive paint technique (PSP). Most of the existing literatures provide information only for stationary end-walls. The effects of rotation on the platform film cooling effectiveness are not well documented. Hence, the existing 3-stage turbine research facility at TPFL, Texas A&M University was re-designed and installed to enable coolant gas injection on the 1st stage rotor platform. Two distinct coolant supply loops were incorporated into the rotor to facilitate separate feeds for upstream cooling using stator-rotor gap purge flow and downstream discrete-hole film cooling. As a continuation of the previously published work involving stator-rotor gap purge cooling, this study investigates film cooling effectiveness on the 1st stage rotor platform due to coolant gas injection through nine discrete holes located downstream within the passage region. Film cooling effectiveness is measured for turbine rotor frequencies of 2400rpm, 2550rpm and 3000rpm corresponding to rotation numbers of Ro = 0.18, 0.19 and 0.23 respectively. For each of the turbine rotational frequencies, film cooling effectiveness is determined for average film-hole blowing ratios of Mholes = 0.5, 0.75, 1.0, 1.25, 1.5 and 2.0. To provide a complete picture of hub cooling under rotating conditions, simultaneous injection of coolant gas through upstream stator-rotor purge gap and downstream discrete film-hole is also studied. The combined tests are conducted for gap purge flow corresponding to coolant to mainstream mass flow ratio of MFR = 1% with three downstream film-hole blowing ratios of Mholes = 0.75, 1.0 and 1.25 for each of the three turbine speeds. The results for combined upstream stator-rotor gap purge flow and downstream discrete holes provide information about the optimum purge flow coolant mass, average coolant hole blowing ratios for each rotational speed and coolant injection location along the passage to obtain efficient platform film cooling.


2021 ◽  
Author(s):  
Izhar Ullah ◽  
Sulaiman M. Alsaleem ◽  
Lesley M. Wright ◽  
Chao-Cheng Shiau ◽  
Je-Chin Han

Abstract This work is an experimental study of film cooling effectiveness on a blade tip in a stationary, linear cascade. The cascade is mounted in a blowdown facility with controlled inlet and exit Mach numbers of 0.29 and 0.75, respectively. The free stream turbulence intensity is measured to be 13.5 % upstream of the blade’s leading edge. A flat tip design is studied, having a tip gap of 1.6%. The blade tip is designed to have 15 shaped film cooling holes along the near-tip pressure side (PS) surface. Fifteen vertical film cooling holes are placed on the tip near the pressure side. The cooling holes are divided into a 2-zone plenum to locally maintain the desired blowing ratios based on the external pressure field. Two coolant injection scenarios are considered by injecting coolant through the tip holes only and both tip and PS surface holes together. The blowing ratio (M) and density ratio (DR) effects are studied by testing at blowing ratios of 0.5, 1.0, and 1.5 and three density ratios of 1.0, 1.5, and 2.0. Three different foreign gases are used to create density ratio effect. Over-tip flow leakage is also studied by measuring the static pressure distributions on the blade tip using the pressure sensitive paint (PSP) measurement technique. In addition, detailed film cooling effectiveness is acquired to quantify the parametric effect of blowing ratio and density ratio on a plane tip design. Increasing the blowing ratio and density ratio resulted in increased film cooling effectiveness at all injection scenarios. Injecting coolant on the PS and the tip surface also resulted in reduced leakage over the tip. The conclusions from this study will provide the gas turbine designer with additional insight on controlling different parameters and strategically placing the holes during the design process.


2006 ◽  
Vol 128 (9) ◽  
pp. 879-888 ◽  
Author(s):  
Jaeyong Ahn ◽  
M. T. Schobeiri ◽  
Je-Chin Han ◽  
Hee-Koo Moon

Detailed film cooling effectiveness distributions are measured on the leading edge of a rotating gas turbine blade with two rows (pressure-side row and suction-side row from the stagnation line) of holes aligned to the radial axis using the pressure sensitive paint (PSP) technique. Film cooling effectiveness distributions are obtained by comparing the difference of the measured oxygen concentration distributions with air and nitrogen as film cooling gas respectively and by applying the mass transfer analogy. Measurements are conducted on the first-stage rotor blade of a three-stage axial turbine at 2400rpm (positive off-design), 2550rpm (design), and 3000rpm (negative off-design), respectively. The effect of three blowing ratios is also studied. The blade Reynolds number based on the axial chord length and the exit velocity is 200,000 and the total to exit pressure ratio was 1.12 for the first-stage rotor blade. The corresponding rotor blade inlet and outlet Mach numbers are 0.1 and 0.3, respectively. The film cooling effectiveness distributions are presented along with discussions on the influence of rotational speed (off design incidence angle), blowing ratio, and upstream nozzle wakes around the leading edge region. Results show that rotation has a significant impact on the leading edge film cooling distributions with the average film cooling effectiveness in the leading edge region decreasing with an increase in the rotational speed (negative incidence angle).


2005 ◽  
Vol 127 (5) ◽  
pp. 521-530 ◽  
Author(s):  
Jaeyong Ahn ◽  
Shantanu Mhetras ◽  
Je-Chin Han

Effects of the presence of squealer, the locations of the film-cooling holes, and the tip-gap clearance on the film-cooling effectiveness were studied and compared to those for a plane (flat) tip. The film-cooling effectiveness distributions were measured on the blade tip using the pressure-sensitive paint technique. Air and nitrogen gas were used as the film-cooling gases, and the oxygen concentration distribution for each case was measured. The film-cooling effectiveness information was obtained from the difference of the oxygen concentration between air and nitrogen gas cases by applying the mass transfer analogy. Plane tip and squealer tip blades were used while the film-cooling holes were located (a) along the camber line on the tip or (b) along the tip of the pressure side. The average blowing ratio of the cooling gas was 0.5, 1.0, and 2.0. Tests were conducted with a stationary, five-bladed linear cascade in a blow-down facility. The free-stream Reynolds number, based on the axial chord length and the exit velocity, was 1,138,000, and the inlet and the exit Mach numbers were 0.25 and 0.6, respectively. Turbulence intensity level at the cascade inlet was 9.7%. All measurements were made at three different tip-gap clearances of 1%, 1.5%, and 2.5% of blade span. Results show that the locations of the film-cooling holes and the presence of squealer have significant effects on surface static pressure and film-cooling effectiveness, with film-cooling effectiveness increasing with increasing blowing ratio.


2012 ◽  
Vol 134 (8) ◽  
Author(s):  
Akhilesh P. Rallabandi ◽  
Shiou-Jiuan Li ◽  
Je-Chin Han

The effect of an unsteady stator wake (simulated by wake rods mounted on a spoke-wheel wake generator) on the modeled rotor blade is studied using the pressure sensitive paint (PSP) mass-transfer analogy method. Emphasis of the current study is on the midspan region of the blade. The flow is in the low Mach number (incompressible) regime. The suction (convex) side has simple angled cylindrical film-cooling holes; the pressure (concave) side has compound angled cylindrical film-cooling holes. The blade also has radial shower-head leading edge film-cooling holes. Strouhal numbers studied range from 0 to 0.36; the exit Reynolds number based on the axial chord is 530,000. Blowing ratios range from 0.5 to 2.0 on the suction side and 0.5 to 4.0 on the pressure side. Density ratios studied range from 1.0 to 2.5, to simulate actual engine conditions. The convex suction surface experiences film-cooling jet lift-off at higher blowing ratios, resulting in low effectiveness values. The film coolant is found to reattach downstream on the concave pressure surface, increasing effectiveness at higher blowing ratios. Results show deterioration in film-cooling effectiveness due to increased local turbulence caused by the unsteady wake, especially on the suction side. Results also show a monotonic increase in film-cooling effectiveness on increasing the coolant to mainstream density ratio.


2016 ◽  
Vol 138 (5) ◽  
Author(s):  
Chao-Cheng Shiau ◽  
Andrew F Chen ◽  
Je-Chin Han ◽  
Salam Azad ◽  
Ching-Pang Lee

Researchers in gas turbine field take great interest in the cooling performance on the first-stage vane because of the complex flow characteristics and intensive heat load that comes from the exit of the combustion chamber. A better understanding is needed on how the coolant flow interacts with the mainstream and the resulting cooling effect in the real engine especially for the first-stage vane. An authentic flow channel and condition should be achieved. In this study, three full-scale turbine vanes are used to construct an annular-sector cascade. The film-cooling design is attained through numerous layback fan-shaped and cylindrical holes dispersed on the vane and both endwalls. With the three-dimensional vane geometry and corresponding wind tunnel design, the true flow field can thus be simulated as in the engine. This study targets the film-cooling effectiveness on the inner endwall (hub) of turbine vane. Tests are performed under the mainstream Reynolds number 350,000; the related inlet Mach number is 0.09; and the freestream turbulence intensity is 8%. Two variables, coolant-to-mainstream mass flow ratios (MFR = 2%, 3%, and 4%) and density ratios (DR = 1.0 and 1.5), are examined. Pressure-sensitive paint (PSP) technique is utilized to capture the detail contour of film-cooling effectiveness on the inner endwall and demonstrate the coolant trace. The presented results serve as a comparison basis for other sets of vanes with different cooling designs. The results are expected to strengthen the promise of PSP technique on evaluating the film-cooling performance of the engine geometries.


2019 ◽  
Vol 141 (4) ◽  
Author(s):  
Nian Wang ◽  
Mingjie Zhang ◽  
Chao-Cheng Shiau ◽  
Je-Chin Han

This study investigates the effects of blowing ratio, density ratio, and spanwise pitch on the flat plate film cooling from two rows of compound angled cylindrical holes. Two arrangements of two-row compound angled cylindrical holes are tested: (a) the first row and the second row are oriented in staggered and same compound angled direction (β = +45 deg for the first row and +45 deg for the second row); (b) the first row and the second row are oriented in inline and opposite direction (β = +45 deg for the first row and −45 deg for the second row). The cooling hole is 4 mm in diameter with an inclined angle of 30 deg. The streamwise row-to-row spacing is fixed at 3d, and the spanwise hole-to-hole (p) is varying from 4d, 6d to 8d for both designs. The film cooling effectiveness measurements were performed in a low-speed wind tunnel in which the turbulence intensity is kept at 6%. There are 36 cases for each design including four blowing ratios (M = 0.5, 1.0, 1.5, and 2.0), three density ratios (DR = 1.0, 1.5, and 2.0), and three hole-to-hole spacing (p/d = 4, 6, and 8). The detailed film cooling effectiveness distributions were obtained by using the steady-state pressure-sensitive paint (PSP) technique. The spanwise-averaged cooling effectiveness are compared over the range of flow parameters. Some interesting observations are discovered including blowing ratio effect strongly depending on geometric design; staggered arrangement of the hole with same orientation does not yield better effectiveness at higher blowing ratio. Currently, film cooling effectiveness correlation of two-row compound angled cylindrical holes is not available, so this study developed the correlations for the inline arrangement of holes with opposing angles and the staggered arrangement of holes with same angles. The results and correlations are expected to provide useful information for the two-row flat plate film cooling analysis.


Sign in / Sign up

Export Citation Format

Share Document