scholarly journals Film Cooling With Compound Angle Holes: Adiabatic Effectiveness

Author(s):  
Donald L. Schmidt ◽  
Basav Sen ◽  
David G. Bogard

Film cooling effectiveness was studied experimentally in a flat plate test facility with zero pressure gradient using a single row of inclined holes which injected high density, cryogenically cooled air. Round holes and holes with a diffusing expanded exit were directed laterally away from the freestream direction with a compound angle of 60°. Comparisons were made with a baseline case of round holes aligned with the freestream. The effects of doubling the hole spacing to six hole diameters for each geometry were also examined. Experiments were performed at a density ratio of 1.6 with a range of blowing ratios from 0.5 to 2.5 and momentum flux ratios from 0.16 to 3.9. Lateral distributions of adiabatic effectiveness results were determined at streamwise distances from 3 D to 15 D downstream of the injection holes. All hole geometries had similar maximum spatially averaged effectiveness at a low momentum flux ratio of I = 0.25, but the round and expanded exit holes with compound angle had significantly greater effectiveness at larger momentum flux ratios. The compound angle holes with expanded exits had a much improved lateral distribution of coolant near the hole for all momentum flux ratios.

1996 ◽  
Vol 118 (4) ◽  
pp. 807-813 ◽  
Author(s):  
D. L. Schmidt ◽  
B. Sen ◽  
D. G. Bogard

Film cooling effectiveness was studied experimentally in a flat plate test facility with zero pressure gradient using a single row of inclined holes, which injected high-density, cryogenically cooled air. Round holes and holes with a diffusing expanded exit were directed laterally away from the free-stream direction with a compound angle of 60 deg. Comparisons were made with a baseline case of round holes aligned with the free stream. The effects of doubling the hole spacing to six hole diameters for each geometry were also examined. Experiments were performed at a density ratio of 1.6 with a range of blowing ratios from 0.5 to 2.5 and momentum flux ratios from 0.16 to 3.9. Lateral distributions of adiabatic effectiveness results were determined at streamwise distances from 3 D to 15 D downstream of the injection holes. All hole geometries had similar maximum spatially averaged effectiveness at a low momentum flux ratio of I = 0.25, but the round and expanded exit holes with compound angle had significantly greater effectiveness at larger momentum flux ratios. The compound angle holes with expanded exits had a much improved lateral distribution of coolant near the hole for all momentum flux ratios.


Author(s):  
Kevin Liu ◽  
Shang-Feng Yang ◽  
Je-Chin Han

Adiabatic film-cooling effectiveness is examined systematically on a typical high pressure turbine blade by varying three critical flow parameters: coolant blowing ratio, coolant-to-mainstream density ratio, and freestream turbulence intensity. Three average coolant blowing ratios 1.0, 1.5, and 2.0; three coolant density ratios 1.0, 1.5, and 2.0; two turbulence intensities 4.2% and 10.5%, are chosen for this study. Conduction-free pressure sensitive paint (PSP) technique is used to measure film-cooling effectiveness. Three foreign gases — N2 for low density, CO2 for medium density, and a mixture of SF6 and Argon for high density are selected to study the effect of coolant density. The test blade features 45° compound-angle shaped holes on the suction side and pressure side, and 3 rows of 30° radial-angle cylindrical holes around the leading edge region. The inlet and the exit Mach number are 0.27 and 0.44, respectively. Reynolds number based on the exit velocity and blade axial chord length is 750,000. Results reveal that the PSP is a powerful technique capable of producing clear and detailed film effectiveness contours with diverse foreign gases. As blowing ratio exceeds the optimum value, it induces more mixing of coolant and mainstream. Thus film-cooling effectiveness reduces. Greater coolant-to-mainstream density ratio results in lower coolant-to-mainstream momentum and prevents coolant to lift-off; as a result, film-cooling increases. Higher freestream turbulence causes effectiveness to drop everywhere except in the region downstream of suction side. Results are also correlated with momentum flux ratio and compared with previous studies. It shows that compound shaped hole has the greatest optimum momentum flux ratio, and then followed by axial shaped hole, compound cylindrical hole, and axial cylindrical hole.


Author(s):  
Scot K. Waye ◽  
David G. Bogard

Film cooling adiabatic effectiveness for axial and compound angle holes on the suction side of a simulated turbine vane was investigated to determine the relative performance of these configurations. The effect of the surface curvature was also evaluated by comparing to previous curvature studies and flat plate film cooling results. Experiments were conducted for varying coolant density ratio, mainstream turbulence levels, and hole spacing. Results from these measurements showed that for mild curvature, 2r/d ≈ 160, flat plate results are sufficient to predict the cooling effectiveness. Furthermore, the compound angle injection improves adiabatic effectiveness for higher blowing ratios, similar to previous studies using flat plate facilities.


2016 ◽  
Vol 138 (12) ◽  
Author(s):  
Sean R. Klavetter ◽  
John W. McClintic ◽  
David G. Bogard ◽  
Jason E. Dees ◽  
Gregory M. Laskowski ◽  
...  

Early stage gas turbine blades feature complicated internal geometries in order to enhance internal heat transfer and to supply coolant for film cooling. Most film cooling experiments decouple the effect of internal coolant feed from external film cooling effectiveness, even though engine parts are commonly fed by cross-flow and feature internal rib turbulators which can affect film cooling. Experiments measuring adiabatic effectiveness were conducted to investigate the effects of turbulated perpendicular cross-flow on a row of 45 deg compound angle cylindrical film cooling holes for a total of eight internal rib configurations. The ribs were angled to the direction of prevailing internal cross-flow at two different angles: 45 deg or 135 deg. The ribs were also positioned at two different spanwise locations relative to the cooling holes: in the middle of the cooling hole pitch and slightly intersecting the holes. Experiments were conducted at a density ratio of DR = 1.5 for a range of blowing ratios including M = 0.5, 0.75, 1.0, 1.5, and 2.0. This study demonstrates that peak effectiveness can be attained through the optimization of cross-flow direction relative to the compound angle direction and rib configuration, verifying the importance of hole inlet conditions in film cooling experiments. It was found that ribs tend to reduce adiabatic effectiveness relative to a baseline, smooth-walled configuration. Rib configurations that directed the internal coolant forward in the direction of the mainstream resulted in higher peak adiabatic effectiveness. However, no other parameters could consistently be identified correlating to increased film cooling performance. It is likely that a combination of factors is responsible for influencing performance, including internal local pressure caused by the ribs, the internal channel flow field, in-hole vortices, and jet exit velocity profiles. This study also attempted to replicate the possibility that film cooling holes may intersect ribs and found that a hole which partially intersects a rib still maintains moderate levels of effectiveness.


Author(s):  
Sean R. Klavetter ◽  
John W. McClintic ◽  
David G. Bogard ◽  
Jason E. Dees ◽  
Gregory M. Laskowski ◽  
...  

Early stage gas turbine blades feature complicated internal geometries in order to enhance internal heat transfer and to supply coolant for film cooling. Most film cooling experiments decouple the effect of internal coolant feed from external film cooling effectiveness, even though engine parts are commonly fed by cross-flow and feature internal rib turbulators which can affect film cooling. Experiments measuring adiabatic effectiveness were conducted to investigate the effects of turbulated perpendicular cross-flow on a row of 45° compound angle cylindrical film cooling holes for a total of eight internal rib configurations. The ribs were angled to the direction of prevailing internal cross-flow at two different angles: 45° or 135°. The ribs were also positioned at two different span-wise locations relative to the cooling holes: in the middle of the cooling hole pitch, and slightly intersecting the holes. Experiments were conducted at a density ratio of DR = 1.5 for a range of blowing ratios including M = 0.5, 0.75, 1.0, 1.5, and 2.0. This study demonstrates that peak effectiveness can be attained through the optimization of cross-flow direction relative to the compound angle direction and rib configuration, verifying the importance of hole inlet conditions in film cooling experiments. It was found that ribs tend to reduce adiabatic effectiveness relative to a baseline, smooth-walled configuration. Rib configurations that directed the internal coolant forward in the direction of the mainstream resulted in higher peak adiabatic effectiveness. However, no other parameters could consistently be identified correlating to increased film cooling performance. It is likely that a combination of factors is responsible for influencing performance, including internal local pressure caused by the ribs, the internal channel flow field, in-hole vortices, and jet exit velocity profiles. This study also attempted to replicate the possibility that film cooling holes may intersect ribs and found that a hole which partially intersects a rib still maintains moderate levels of effectiveness.


2006 ◽  
Vol 129 (2) ◽  
pp. 202-211 ◽  
Author(s):  
Scot K. Waye ◽  
David G. Bogard

Film cooling adiabatic effectiveness for axial and compound angle holes on the suction side of a simulated turbine vane was investigated to determine the relative performance of these configurations. The effect of the surface curvature was also evaluated by comparing to previous curvature studies and flat plate film cooling results. Experiments were conducted for varying coolant density ratio, mainstream turbulence levels, and hole spacing. Results from these measurements showed that for mild curvature, 2r∕d≈160, flat plate results are sufficient to predict the cooling effectiveness. Furthermore, the compound angle injection improves adiabatic effectiveness for higher blowing ratios, similar to previous studies using flat plate facilities.


1999 ◽  
Vol 122 (2) ◽  
pp. 224-232 ◽  
Author(s):  
C. M. Bell ◽  
H. Hamakawa ◽  
P. M. Ligrani

Local and spatially averaged magnitudes of the adiabatic film cooling effectiveness, the iso-energetic Stanton number ratio, and film cooling performance parameter are measured downstream of (i) cylindrical round, simple angle (CYSA) holes, (ii) laterally diffused, simple angle (LDSA) holes, (iii) laterally diffused, compound angle (LDCA) holes, (iv) forward diffused, simple angle (FDSA) holes, and (v) forward diffused, compound angle (FDCA) holes. Data are presented for length-to-inlet metering diameter ratio of 3, blowing ratios from 0.4 to 1.8, momentum flux ratios from 0.17 to 3.5, and density ratios from 0.9 to 1.4. The LDCA and FDCA arrangements produce higher effectiveness magnitudes over much wider ranges of blowing ratio and momentum flux ratio compared to the three simple angle configurations tested. All three simple angle hole geometries, CYSA, FDSA, and LDSA, show increases of spanwise-averaged adiabatic effectiveness as the density ratio increases from 0.9 to 1.4, which are larger than changes measured downstream of FDCA and LDCA holes. Iso-energetic Stanton number ratios downstream of LDCA and FDCA holes (measured with unity density ratios) are generally increased relative to simple angle geometries for m⩾1.0 when compared at particular normalized streamwise locations, x/D, and blowing ratios, m. Even though this contributes to higher performance parameters and lower protection, overall film cooling performance parameter q˙″/q˙o″ variations with x/D and m are qualitatively similar to variations of adiabatic film cooling effectiveness with x/D and m. Consequently, the best overall protection over the widest ranges of blowing ratios, momentum flux ratios, and streamwise locations is provided by LDCA holes, followed by FDCA holes. Such improvements in protection are partly due to film diffusion from expanded hole shapes, as well as increased lateral spreading of injectant from compound angles. [S0022-1481(00)02202-7]


1991 ◽  
Vol 113 (3) ◽  
pp. 442-449 ◽  
Author(s):  
A. K. Sinha ◽  
D. G. Bogard ◽  
M. E. Crawford

Film-cooling effectiveness was studied using a row of inclined holes that injected cryogenically cooled air across a flat, adiabatic test plate. The density ratio of the coolant to mainstream varied from 1.2 to 2.0. Surface temperatures were measured using a unique surface thermocouple arrangement free of conduction errors. Temperatures were obtained along the jet centerline and across a number of lateral locations. By independently varying density ratio and blowing rate, scaling of adiabatic effectiveness with mass flux ratio, velocity ratio, and momentum ratio was determined. Depending on the momentum flux ratio, the jet either remains attached to the surface, detaches and then reattaches, or is fully detached. For attached jets, the centerline effectiveness scaled with the mass flux ratio. However, for detached-reattached jets, a consistent scaling was not found although the general distribution of the centerline effectiveness scaled with momentum flux ratio. Laterally averaged effectiveness was found to be dependent on density ratio and momentum flux ratio. Decreases in density ratio and increases in momentum flux ratio were found to reduce the spreading of the film cooling jet significantly and thereby reduce laterally averaged effectiveness.


Author(s):  
Lesley M. Wright ◽  
Stephen T. McClain ◽  
Charles P. Brown ◽  
Weston V. Harmon

A novel, double hole film cooling configuration is investigated as an alternative to traditional cylindrical and fanshaped, laidback holes. This experimental investigation utilizes a Stereo-Particle Image Velocimetry (S-PIV) to quantitatively assess the ability of the proposed, double hole geometry to weaken or mitigate the counter-rotating vortices formed within the jet structure. The three-dimensional flow field measurements are combined with surface film cooling effectiveness measurements obtained using Pressure Sensitive Paint (PSP). The double hole geometry consists of two compound angle holes. The inclination of each hole is θ = 35°, and the compound angle of the holes is β = ± 45° (with the holes angled toward one another). The simple angle cylindrical and shaped holes both have an inclination angle of θ = 35°. The blowing ratio is varied from M = 0.5 to 1.5 for all three film cooling geometries while the density ratio is maintained at DR = 1.0. Time averaged velocity distributions are obtained for both the mainstream and coolant flows at five streamwise planes across the fluid domain (x/d = −4, 0, 1, 5, and 10). These transverse velocity distributions are combined with the detailed film cooling effectiveness distributions on the surface to evaluate the proposed double hole configuration (compared to the traditional hole designs). The fanshaped, laidback geometry effectively reduces the strength of the kidney-shaped vortices within the structure of the jet (over the entire range of blowing ratios considered). The three-dimensional velocity field measurements indicate the secondary flows formed from the double hole geometry strengthen in the plane perpendicular to the mainstream flow. At the exit of the double hole geometry, the streamwise momentum of the jets is reduced (compared to the single, cylindrical hole), and the geometry offers improved film cooling coverage. However, moving downstream in the steamwise direction, the two jets form a single jet, and the counter-rotating vortices are comparable to those formed within the jet from a single, cylindrical hole. These strong secondary flows lift the coolant off the surface, and the film cooling coverage offered by the double hole geometry is reduced.


Author(s):  
Kevin Liu ◽  
Shang-Feng Yang ◽  
Je-Chin Han

A detailed parametric study of film-cooling effectiveness was carried out on a turbine blade platform. The platform was cooled by purge flow from a simulated stator–rotor seal combined with discrete hole film-cooling. The cylindrical holes and laidback fan-shaped holes were accessed in terms of film-cooling effectiveness. This paper focuses on the effect of coolant-to-mainstream density ratio on platform film-cooling (DR = 1 to 2). Other fundamental parameters were also examined in this study—a fixed purge flow of 0.5%, three discrete-hole film-cooling blowing ratios between 1.0 and 2.0, and two freestream turbulence intensities of 4.2% and 10.5%. Experiments were done in a five-blade linear cascade with inlet and exit Mach number of 0.27 and 0.44, respectively. Reynolds number of the mainstream flow was 750,000 and was based on the exit velocity and chord length of the blade. The measurement technique adopted was the conduction-free pressure sensitive paint (PSP) technique. Results indicated that with the same density ratio, shaped holes present higher film-cooling effectiveness and wider film coverage than the cylindrical holes, particularly at higher blowing ratios. The optimum blowing ratio of 1.5 exists for the cylindrical holes, whereas the effectiveness for the shaped holes increases with an increase of blowing ratio. Results also indicate that the platform film-cooling effectiveness increases with density ratio but decreases with turbulence intensity.


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