Enhancement of Production Rate and Flexibility in an Assembly Line by Execution of Various Lean Techniques - A Case Study

Author(s):  
D. Sobya ◽  
S. Jeyabalan

This research work mainly focuses on the flexibility and productivity improvement through the execution of different lean techniques in the valve assembly of medium scale manufacturing unit. The different types of wastes percentage are determined to find out the waste which mainly affects the productivity. The major wastes of motion waste by about 30% and unwanted distance of 250 square foot were reduced by implementation of kaizen in the valve assembly area. Value stream mapping was used to identify the bottleneck process and by eliminating the bottleneck process results in the reduction of excess motion and non-value added activity by 45%. Work-in-process aging and work-in-process inventory cost was calculated and the production level was estimated by using 95th Percentile calculation. The total lead time was reduced about 54minutes with reduction of transportation time 2.7minutes after the implementation of lean techniques and the productivity of the valve assembly was also increased to about 6% after reducing the non-value added activities.

Author(s):  
V. Saravanan ◽  
S. Nallusamy ◽  
Abraham George

Productivity is an important parameter for all small and medium scale manufacturing industries. Lean manufacturing emerged as production strategy capable of increasing productivity by identifying and eliminating non value added activities. This article deals with productivity improvement in a pre-assembly line of gearbox manufacturing company with a case study using lean concepts like process flow chart, process Gantt chart and time study. This paper illustrates using a case study on how a value stream mapping has to be carried out in a planet carrier pre-assembly line. Value stream mapping and work standardization are the key tools used in lean manufacturing and lean transformation. It makes the process smoother, helps in reduction of lead time and ultimately increasing the productivity. From the observed results it was found that, the productivity has been increased from 7 pieces to 10 pieces in the first step assembly when the proposed VSM was implemented. The second step processing time was reduced by the execution of proposed value stream mapping with TAKT time of 126 minutes and 165 minutes of processing time for demand of 10 pieces were achieved and the overall processing time has been reduced by about 24%.


2011 ◽  
Vol 110-116 ◽  
pp. 2062-2066 ◽  
Author(s):  
Paramdeep Singh ◽  
Harpuneet Singh

Lean manufacturing has been proved to be an effective management philosophy for improving businesses in a competitive market by eliminating non-value added waste and improving in process operations. Value stream mapping is an important tool used to identify the opportunities for various lean techniques. The present research mainly focuses on the description of a model that is developed to contrast the “before” and “after” scenarios in detail in order to obtain the various benefits such as reduced production lead time, lower work in process inventory [1] and proper utilisation of the workforce. The current manufacturing system has been compared with the proposed pull (Kanban) system which shows the benefits of the proposed lean manufacturing system over the existing traditional manufacturing system. The present research work has been carried out at typical tractor industry which shows 50.5% reduction in total lead time in the future state value mapping of the crank case and the number of operators involved in processing of crank case has also been reduced from 22 to 18.


2018 ◽  
Vol 154 ◽  
pp. 01093
Author(s):  
Halimatussa’ diah ◽  
Ali Parkhan ◽  
Muchamad Sugarindra

The increaseing productivity is one of the competitive strategies that can be applied in a company in order to survive in an intense competitive presure. PT. XYZ is a textile industry manufacturing golf gloves and caddy bag. Every day, the company has a production target of 600 pieces per line. However, the desired target is not achieved that it will affect the delay in delivery of products to customers. In this research, a case study on implementing value stream mapping and Kaizen as the lean manufacturing concept is reported. The purpose of this study is to map the current production line, analyse and design the future value stream mapping by eliminating waste occured. It is obtained a lead time reduction as much as 440.4 seconds through eliminating 17 non-value added activities. Then, the output can be increased up to 21% which is equal to 502 pieces.


2021 ◽  
Author(s):  
Sam Ataei

For many years, productivity improvement through value stream mapping and simulation has been studied in manufacturing industry where the flow of materials is visible and the work can be standardized. In recent years, the service industry has become a new arena for lean operations. Within the service industry, client-based companies have distinct challenges in streamlining their process, as it may not be feasible to standardize the needs of different clients. This thesis focuses on a case from a client-based company in the area of graphic communications and brand point management services. The thesis examines the application of lean principles towards a set of subjective processes and provides directions for improving productivity. Some lean methods utilized in the study include creating process flows, conducting operator interviews to back-up the process flow, collecting data such as processing time and creating a detailed values stream map of the retail packaging process in order to analyze any necessary areas of improvement. Value stream mapping has been used to identify the areas where the non-value-added tasks can be reduced, and simulation models have been used to imitate and predict the company's different scenarios in dealing with bottlenecks, different kinds of wastes, and to assess potential areas for improvements. The analysis of results indicates that it is necessary to have two different streams of the processes; one for a team-based job and another one for a non-team-based job. The proper touch points from each department have been found and value-added and non-value added times have been determined in order to create the current-state. Furthermore, future-states have been created with some recommendations kept in mind to validate the time savings. The results have been verified through a simulation analysis.


2021 ◽  
Vol 13 (21) ◽  
pp. 11997
Author(s):  
Varun Tripathi ◽  
Somnath Chattopadhyaya ◽  
Alok Bhadauria ◽  
Shubham Sharma ◽  
Changhe Li ◽  
...  

Worldwide, industries are emphasizing the development of an agile system to sustain higher productivity, which can be applied to ensure improvements in all production conditions in industry 4.0. In the present scenario, several methods are used for improvements in production, such as value stream mapping, kaizen, just in time, Kanban, and total productive maintenance, etc., The objective of the present research article is to produce an agile system to sustain improvements in productivity through a methodology coupled with value stream mapping in industry 4.0. Value stream mapping is a lean-based method and is used for the maximization of productivity by the elimination of non-value-added activities. The proposed methodology has been validated by productivity enhancements achieved in a case study of the earthmoving machinery manufacturing sector. The study establishes that the proposed methodology would encourage industry personnel during decision-making processes, which would lead to improvements in production in industry 4.0.


2019 ◽  
Author(s):  
◽  
Kate Lusiba

Lean manufacturing is an optimum approach for the reduction and elimination of waste within an organization. The case study company is based in South Africa and produces heat exchangers through main processes or fractals, which include pre-assembly, core building, brazing and final assembly. A walk through the plant showed that there was a large amount of inventory awaiting final assembly and that the brazing furnace often waited for material from core building. This was an indication that there could be an imbalance between the three fractals in terms of cycle time. Thus, the aim of this study was to improve the manufacturing processes for heat exchangers at the automotive manufacturing company through the deployment of value stream mapping, subsequent line balancing and developing a roadmap for reduction of waste. The case study research strategy was adopted for the study since it provided an in-depth view of phenomena. The first objective was to outline the production flow for the manufacture of automotive heat exchanger parts. The method used was a walk through the plant and observations were made to gain an understanding of the production steps from logistics production planning to shipping of the finished goods, and subsequently to a mapping-out of the production process flow was undertaken. The results showed that there was a large amount of inventory awaiting final assembly and that the brazing furnace often waited for material from core building. It was concluded that there was need to conduct a detailed process analysis to identify sources of waste. The second objective was to conduct value stream mapping for assessing the value- and non-value-adding activities in the manufacture of automotive heat exchangers components. A value stream map was developed through walking to Gemba and mapping out the production process, collecting data and pinpointing waste activities or areas to be improved. The kaizen flashes from the value stream map also revealed that operators were not fully utilizing the capacity of the bottleneck workstations. It was concluded that two instead of one planning points, and inefficiency at assembly were root causes of the high work-in-process level. The third objective was to conduct a line balancing analysis for the three production fractals. The method used was a Pareto analysis for evaluating the products, analysing the product mix and line balancing analysis of the production line. The results revealed that the furnace was run on two shifts while the subsequent assembly and preceding core building were running on three shifts causing a work-in-process build-up, thereby resulting in line imbalance. It was concluded that it was imperative to change the scheduling approach, and adopt one that prioritised and spread the cores that had relatively short cycle times, and also reduce downtime, change-over time as well as additional time for scrap and defects, and a future-state balance chart revealed that the fractals imbalance had been reduced. The fourth objective was to develop a roadmap for reduction of waste in the manufacture of car heat exchangers components. The method used was to develop proposals and assess the feasibility and cost implications of implementing each option. Recommendations were made for continuous process improvement and a roadmap for reduction of waste was proposed. In order to improve the output of assembly, training for the operators was recommended since it would also enable the removal of the second planning point at assembly. Further research could also be conducted to develop an optimal scheduling algorithm for allocation of products to work centres to ensure high utilization of work centres and reduce work-in-process inventory.


2019 ◽  
Vol 5 (1) ◽  
pp. 1-7
Author(s):  
Catur Kusbiantoro ◽  
Ellysa Nursanti

CV. Tanara Textile merupakan salah satu perusahaan tekstil yang termasuk dalam kelompok industri penyempurnaan kain berupa kain kaos. Pada proses produksi di perusahaan masih ditemukan beberapa waste. Penelitian ini bertujuan untuk mengidentifikasi dan menurunkan waste yang terjadi pada proses produksi maka digunakan pendekatan lean manufacturing. Metode Value Stream Mapping (VSM) digunakan untuk pemetaan aliran produksi dan aliran informasi terhadap suatu produk pada tingkat produksi total, melakukan wawancara untuk pembobotan penyebab 7 waste yang sering terjadi pada proses produksi, VALSAT untuk menganalisa pemborosan dari hasil pembobotan yang selanjutnya melakukan detailed mapping tools, serta analisis FMEA untuk mengetahui penyebab kegagalan prosesyang terjadi di lini produksi lalu menghitung nilai RPN tertinggi. Selanjutnya melakukan usulan perbaikan untuk menurunkan waste unnecessary inventory serta menganalisis perbaikan secara berkelanjutan dengan PDCA. Waste terbesar ada pada Unncessary Inventory sebesar 28,571% faktor penyebabnya adalah penumpukan bahan baku, work in process (WIP), sparepart yang tidak terpakai dan penimbunan pada finished goods Sebelum perbaikan proses produksi 16 hari 9 jam dimana Value Added 6 hari 4 jam dan Lead Time 10 hari 4 jam, setelah perbaikan proses produksi menjadi 14 hari 5 jam dimana Value Added 6 hari 4 jam dan Lead Time 8 hari 1 jam, dengan demikian dapat meningkatkan process cycle efficiency sebesar 17,19% dan menghemat lead time sebesar 2,546% dengan penurunan waste sebesar 8,31%


Author(s):  
S. Nallusamy ◽  
M.A. Adil Ahamed

Value stream mapping has the reputation of uncovering waste in manufacturing, production and business process. This helps in identifying and removing or streaming value added steps and eliminating non value added steps. In this study the process was analyzed to find an opportunity to drastically reduce the number of actions and to simplify the same. By reducing waste the proportion of value adding time increases in the whole process and the process throughput speed could also be increased. This makes the redesigned process more effective and more efficient. The reengineered process was flow charted in its future state with process steps and information flows re-engineering, simplified and economized. The current layout was analysed to identify and eliminate the non value added activities through lean tools like 5S, VSM and line balancing in a manufacturing industry. From the observed results, it was concluded that the non value added time could be reduced by about 13% while the process cycle efficiency could be increased by about 10%. Virtual simulation was conducted to verify and validate the existing situation as well as to propose the results and the effectiveness of lean principles in a systematic manner with the help of ARENA.


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