Experimental Performance Results from a Carbon Dioxide/Oxygen Breathing Diesel Engine

1994 ◽  
Author(s):  
J. G. Hawley ◽  
G. T. Reader
1994 ◽  
Vol 04 (04) ◽  
pp. 477-488 ◽  
Author(s):  
S.K.S. GUPTA ◽  
C.-H. HUANG ◽  
P. SADAYAPPAN ◽  
R.W. JOHNSON

Implementations of various fast Fourier transform (FFT) algorithms are presented for distributed-memory multiprocessors. These algorithms use data redistribution to localize the computation. The goal is to optimize communication cost by using a minimum number of redistribution steps. Both analytical and experimental performance results on the Intel iPSC/860 system are presented.


2011 ◽  
Author(s):  
Elfed Lewis ◽  
John Clifford ◽  
Colin Fitzpatrick ◽  
Gerard Dooly ◽  
Weizhong Zhao ◽  
...  

Author(s):  
Liam Barr ◽  
Stephen Spence ◽  
David Thornhill ◽  
Paul Eynon

This report details the numerical and experimental investigation of the performance characteristics of a conventional radial turbine compared with a new back swept design for the same application. The blade geometry of an existing turbine from a turbocharger was used as a baseline. A new back swept blade was subsequently designed for the rotor, which departed from the conventional radial inlet blade angle to incorporate a 25° inlet blade angle. A comparative numerical analysis between the two geometries is presented. Results show that the 25° back swept blade offers significant increases in efficiency while operating at lower than optimum velocity ratios (U/C). Improvements in efficiency at off-design conditions could significantly improve turbocharger performance since the turbine typically experiences lower than optimum velocity ratios while accelerating during engine transients. A commercial CFD code was used to construct single passage steady state numerical models. The numerical predictions show off-design performance gains of 2% can be achieved, while maintaining design point efficiency. A finite element stress analysis was conducted to show that the nonradial inlet blade angle could be implemented without exceeding the acceptable stress levels for the rotor. A modal analysis was also carried out in order to identify the natural blade frequencies, showing that these were not significantly changed by the implementation of backswept blading. A prototype backswept rotor was produced and tested in a direct comparison with the baseline rotor geometry. Experimental performance results showed strong correlations with those obtained numerically, and verified the predicted performance gains at off-deign velocity ratios. This numerical and experimental study has shown that it is feasible from both an aerodynamic and structural point of view to improve the performance characteristic of a radial turbine at lower than optimum velocity ratios through the implementation of back swept blading.


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