813 The Performance Improvement of Direct Injection Gasoline Engine with a Three-Dimensional Cam that Independently Controls Lift and Timing

2008 ◽  
Vol 2008.45 (0) ◽  
pp. 271-272
Author(s):  
Youichi Kawaguchi ◽  
Kazunori Miyata ◽  
Masaru Ogura
Author(s):  
Xinyan Wang ◽  
Jun Ma ◽  
Hua Zhao

In this study, a two-stroke boosted uniflow scavenged direct injection gasoline (BUSDIG) engine was proposed and researched to achieve aggressive engine downsizing and downspeeding. Compared to loop or cross scavenged two-stroke engines, the BUSDIG engine can achieve excellent scavenging performance and be operated with higher boost pressure as well as the absence of air and fuel short-circuiting. As a fundamental engine geometric parameter, the bore/stroke (B/S) ratio would directly affect the scavenging process in the uniflow scavenged two-stroke engine. Three-dimensional computational fluid dynamics simulations were used to investigate the scavenging process in the BUSDIG engine with different B/S ratios. Four B/S ratios of 0.66, 0.8, 1, and 1.3 were analyzed. The results indicate that a bigger B/S ratio leads to deteriorated swirl flow motion but better delivery ratio, scavenging efficiency, and charging efficiency. In order to fulfil the potential of the BUSDIG engine with different B/S ratios, two key scavenge port angles, i.e. axis inclination angle (AIA) and swirl orientation angle (SOA), were varied from the baseline design (AIA = 90°, SOA = 20°) to study their effects on the scavenging process for each B/S ratio design. Overall, a larger AIA leads to lower swirl ratio (SR) but achieves better scavenge performance, which is crucial for a large B/S ratio design. A small SOA design leads to noticeably lower SR but superior scavenging performances for a small B/S ratio design. An intermediate SOA, e.g. 10 and 20°, is preferred to improve the scavenging for a large B/S ratio design.


2000 ◽  
Vol 1 (2) ◽  
pp. 147-161 ◽  
Author(s):  
J Reissing ◽  
H Peters ◽  
J. M. Kech ◽  
U Spicher

Gasoline direct injection (GDI) spark ignition engine technology is advancing at a rapid rate. The development and optimization of GDI engines requires new experimental methods and numerical models to analyse the in-cylinder processes. Therefore the objective of this paper is to present numerical and experimental methods to analyse the combustion process in GDI engines. The numerical investigation of a four-stroke three-valve GDI engine was performed with the code KIVA-3V [1]. For the calculation of the turbulent combustion a model for partially premixed combustion, developed and implemented by Kech [4], was used. The results of the numerical investigation are compared to experimental results, obtained using an optical fibre technique in combination with spectroscopic temperature measurements under different engine conditions. This comparison shows good agreement in temporal progression of pressure. Both the numerical simulation and the experimental investigation predicted comparable combustion phenomena.


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