A Successful Application of Continuous Pack-Off Technology to Water Shutoff Recompletion for High-WCT Gravel-Packed Horizontal Well

2021 ◽  
Author(s):  
An Jiang ◽  
Yunpeng Li ◽  
Xing Liu ◽  
Fengli Zhang ◽  
Tianhui Wang ◽  
...  

Abstract Objectives/Scope Controlling the excessive water production from the high water cut gravel packing horizontal well is a challenge. The approach which uses regular packers or packers with ICD screens to control the unwanted water does not function well. This is mainly because of the length limitation of packers which will make the axial flow resistance insufficient. Methods, Procedures, Process In this paper, a successful case that unwanted water is shutoff by using continuous pack-off particles with ICD screens (CPI) in the whole horizontal section in an offshore oilfield of Bohai bay is presented. The reservoir of this case is the bottom-water high viscosity reservoir. The process is to run 2 3/8" ICD screen string into the 4" screen string originally in place, then to pump the pack-off particles into the annulus between the two screens, and finally form the 360m tightly compacted continuous pack-off particle ring. Results, Observations, Conclusions The methodology behind the process is that the 2-3/8" ICD screens limit the flow rate into the pipes as well as the continuous pack-off particle ring together with the gravel ring outside the original 4" screens to prevent the water channeling into the oil zone along the horizontal section. This is the first time this process is applied in a high water cut gravel packed horizontal well. After the treatment, the water rate decreased from 6856BPD to 836.6BPD, the oil rate increased from 44BPD to 276.8BPD. In addition, the duration of this performance continued a half year until March 21, 2020. Novel/Additive Information The key of this technology is to control the unwanted water by using the continuous pack-off particles instead of the parkers, which will bring 5 advantages, a) higher efficiency in utilizing the production interval; b) no need to find the water source and then fix it; c) the better ability to limit the axial flow; d) effective to multi-WBT (water break though) points and potential WBT points; e) more flexible for further workover. The technology of this successful water preventing case can be reference to other similar high water cut gravel packed wells. Also, it has been proved that the well completion approach of using CPI can have good water shutoff and oil incremental result. Considering the experiences of historical applications, CPI which features good sand control, water shutoff and anti-clogging is a big progress compared to the current completion technologies.

2021 ◽  
Author(s):  
Hongfu Shi ◽  
Yingxian Liu ◽  
Lifu Jiang ◽  
Jingding Zheng ◽  
Liqin Gan

Abstract Abundant faults, long oil-bearing intervals (up to 500m), and diverse fluids including conventional oil and heavy oil, result in P oilfield became one of the most complex oil fields in the Bohai Bay. The main characters ofinitial development plan are directional well with commingle production, open hole completion, large draw down, high oil production rate, and reverse nine-point well pattern. At present, the oilfield has entered a stage of high water cut, with average water cut more than 85%. What can we do next, decommissioning or rebirthing? An integrated solution was proposed to redevelop the oilfield which focus on the layers’ subdivision, the fine description of the sand body,a large number of horizontal wells on the top of the water-flooded layer are used to tap the potential, increase the water injector to transform the stream lines and rebuild the reservoir pressure, and search for potential sand bodies to increase reserves.


2006 ◽  
Author(s):  
Nashi Mohammed Al-Otaibi ◽  
Abdulwafi A. Al-Gamber ◽  
Michael R. Konopczynski ◽  
Suresh Jacob

2016 ◽  
Vol 139 (1) ◽  
Author(s):  
Lei Zhang ◽  
Chunsheng Pu ◽  
Shuxia Cui ◽  
Khan Nasir ◽  
Yang Liu

In order to effectively plug the fracture channeling-path in the high water cut fractured low permeability reservoir, a new type of water shutoff agent is developed by bottle tests and its injectivity and plugging performance in fractures are systematically studied by rheology and fractured core displacement experiment. The gelant consists of modified starch, dimethyl diallyl ammonium chloride, N,N′-methylene diacrylamide, and potassium persulfate, which behaves as a Newtonian with a good flowing capacity that allows its accurate positioning in the fractures. After gelatinization, the gel has high elastic modulus and viscous modulus. During the gelant injection into the fractured core, the filtration from fracture into matrix of the gelant leads to a difference between the injection volume of the gelant and the plugged fracture volume. Thus, a mathematical model for calculating filtration volume is established and applied in plugging experiment very well. After plugging, the two block cores can be tightly cemented together by the starch gel. The experiments show that the water shutoff agent and the mathematical model of filtration can be used to effectively plug the fracture channeling-path in the high water cut fractured low permeability reservoir.


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