Study and Application of Shallow Water Fracturing Fluid in High Temperature Deep Carbonate Reservoir

2013 ◽  
Author(s):  
Mingguang Che ◽  
Yonghui Wang ◽  
Xingsheng Cheng ◽  
Yongjun Lu ◽  
Yongping Li ◽  
...  
2013 ◽  
Author(s):  
Mingguang Che ◽  
Yonghui Wang ◽  
Xingsheng Cheng ◽  
Yongjun Lu ◽  
Yongping Li ◽  
...  

2016 ◽  
Author(s):  
Ying Gao ◽  
Shengjiang Lian ◽  
Yang Shi ◽  
Xianyou Yang ◽  
Fujian Zhou ◽  
...  

Author(s):  
Hiromichi Mitamura ◽  
Hideaki Nishizawa ◽  
Yasushi Mitsunaga ◽  
Kotaro Tanaka ◽  
Junichi Takagi ◽  
...  

2021 ◽  
Author(s):  
Juan Manuel Leon ◽  
Shehadeh K. Masalmeh ◽  
Siqing Xu ◽  
Ali M. AlSumaiti ◽  
Ahmed A. BinAmro ◽  
...  

Abstract Assessing polymer injectivity for EOR field applications is highly important and challenging. An excessive injectivity reduction during and after polymer injection may potentially affect the well integrity and recovery efficiency and consequently, injection strategy and the economics of the polymer projects. Moreover, well conditions such as skin, completion configuration, and injection water quality can significantly impact polymer injectivity. Additionally, the presence of fractures or micro-fractures may govern injection pressure. In contrast, historic field applications have shown that polymer injectivity is in general better than expected from simulations or laboratory data. In the laboratory experiments, the polymer injectivity has been evaluated by injection of significant amounts of pore volumes of polymer at relevant well-injection rates. In addition, several experiments were performed to measure the complex in-situ rheology expected to dominate the flow near the wellbore This paper presents the analysis of the the world's first polymer injectivity test (PIT) conducted in a high temperature and high salinity (HTHS) carbonate reservoir in Abu Dhabi as part of a comprehensive de-risking program for a new polymer-based EOR scheme proposed by ADNOC for these challenging carbonate reservoirs (see Masalmeh et. al., 2014). The de-risking program includes an extensive laboratory experimental program and field injectivity test to ensure that the identified polymer can be injected and propagated in the target formation before multi-well pilot and full-field implementation stages. Experimental laboratory data and the field injectivity test results are presented in earlier publications (Masalmeh et. al., 2019; Rachapudi et. al., 2020) and references therein. This PIT is the world's first polymer injectivity test in a carbonate reservoir under such harsh conditions of high salinity, high content of divalent ions and high temperature. In addition, the polymer used during the test has never been field-tested before. Therefore, the results of the PIT interpretation will help to de-risk the suitable polymer for the future inter-well pilot for the new proposed EOR Polymer-based scheme and it is a game-changer to unlock several opportunities for different Chemical EOR applications on full-field scale in other reservoirs with similar characteristics. A single well radial simulation model was built to integrate the surveillance data during PIT and the extensive laboratory experiments. Morever, multiple Pressure Fall Off Tests (PFOs) during the same periods were analyzed and intergaretd in the model.The study assessed the effect of polymer viscosity on mobility reduction, evaluated the polymer bank propagation, investigated the effect of the skin build-up, residual resistance factor (RRF) and shear effects on the well injectivity. Additionally, a comprehensive assisted history match method and robust simulation sensitivity analysis was implemented, thousands of sensitivity simulation runs were performed to capture several possible injection scenarios and validate laboratory parameters. The simulation study confirmed that the PIT could be interpreted using the laboratory-measured polymer parameters such as polymer bulk viscosity, in-situ rheology, RRF and adsorption.


2021 ◽  
Author(s):  
Frank Figueroa ◽  
Gustavo Mejías ◽  
José Frías ◽  
Bonifacio Brito ◽  
Diana Velázquez ◽  
...  

Abstract Enhanced hydrocarbon production in a high-pressure/high-temperature (HP/HT) carbonate reservoir, involves generating highly conductive channels using efficient diversion techniques and custom-designed acid-based fluid systems. Advanced stimulation design includes injection of different reactive fluids, which involves challenges associated with controlling fluid leak-off, implementing optimal diversion techniques, controlling acid reaction rates to withstand high-temperature conditions, and designing appropriate pumping schedules to increase well productivity and sustainability of its production through efficient acid etching and uniform fluid distribution in the pay zone. Laboratory tests such as rock mineralogy, acid etching on core samples and solubility tests on formation cuttings were performed to confirm rock dissolving capability, and to identify stimulation fluids that could generate optimal fracture lengths and maximus etching in the zone of interest while corrosion test was run to ensure corrosion control at HT conditions. After analyzing laboratory tests results, acid fluid systems were selected together with a self-crosslinking acid system for its diversion properties. In addition, customized pumping schedule was constructed using acid fracturing and diverting simulators and based on optimal conductivity/productivity results fluid stages number and sequence, flow rates and acid volumes were selected. The engineered acid treatment generated a network of conductive fractures that resulted in a significant improvement over initial production rate. Diverting agent efficiency was observed during pumping treatment by a 1,300 psi increase in surface pressures when the diverting agent entered the formation. Oil production increased from 648.7 to 3105.89 BPD, and gas production increased from 4.9 to 26.92 MMSCFD. This success results demonstrates that engineering design coupled with laboratory tailor fluids designs, integrated with a flawless execution, are the key to a successful stimulation. This paper describes the details of acidizing technique, treatment design and lessons learned during execution and results.


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