scholarly journals TAKT TIME E BALANCEAMENTO NO FORMATO DA PROGRAMAÇÃO DE LINHA DE PRODUÇÃO

Author(s):  
Patrick Cemin ◽  
Zaida Cristiane Dos Reis ◽  
Vandoir Welchen ◽  
Juliana Matte ◽  
Daniel Hank Miri ◽  
...  

Produzir mais, empregando menos tempo e menos recursos, é o sonho de qualquer empresa. Diante disso, este estudo busca resolver problemas de utilização da capacidade e de desnivelamentos de produção. Dessa maneira, o objetivo consiste em propor um formato de programação que otimize a utilização dos recursos e resulte em maior equilíbrio na produção de uma empresa do ramo metalúrgico, produtora de implementos rodoviários e localizada na região Sul do Brasil. Por meio de um estudo de caso, identificaram-se a forma de trabalho e a situação da programação da empresa. A partir disso, criou-se um modelo de um novo formato de produção, voltado à minimização das variações de volumes e fundamentado, basicamente, na utilização dos conceitos de takt time e de balanceamento das linhas. Conclui-se que o modelo proposto permitirá um ritmo continuado na produção, sendo capaz de estabilizá-la. Ademais, conforme for aplicado nas linhas da empresa, evidenciará os pontos ao longo do fluxo que precisam de melhoria, identificando gargalos e ociosidades. A soma de tais fatores proporcionará o aprimoramento contínuo dos processos da empresa e a otimização dos recursos disponíveis para a produção. Palavras-Chave: Linha de produção. Programação de produção. Takt time. Balanceamento de linha. Capacidade produtiva.   Abstract: Producing more, using less time and fewer resources, is the dream of any company. Therefore, this study seeks to solve problems of capacity utilization and production unevenness. Thus, the objective is to propose a programming format that optimizes the use of resources and results in greater balance in the production of a company in the metallurgical sector, producer of road implements and located in the southern region of Brazil. Through a case study, the way of working and the situation of the company's programming were identified. From this, a model of a new production format was created, aimed at minimizing volume variations and basically based on the use of the concepts of takt time and line balancing. It is concluded that the proposed model will allow a continued pace in production, being able to stabilize it. Furthermore, as applied to the company's lines, it will highlight the points along the flow that need improvement, identifying bottlenecks and idleness. The sum of these factors will provide the continuous improvement of the company's processes and the optimization of the resources available for production. Keywords: Production line. Production schedule. Takt time. Line balancing. Productive capacity.  

2015 ◽  
Vol 44 (2) ◽  
pp. 117-123 ◽  
Author(s):  
Md. Mahbubur Rahman ◽  
Farjana Nur ◽  
Subrata Talapatra

For every manufacturing organization, price of the product primarily comprises of manufacturing cost and desired profit. If a company wishes to increase its profit, one way is to reduce the manufacturing cost with maintaining the quality of the product. Waste reduction, especially the (wait) time waste, is an important factor to shrink the manufacturing cost. The purpose of this paper is to identify and address the way to reduce idle time in the apparel manufacturing organization using various line balancing technique to improve productivity and efficiency in domestic context. Line balancing job has been done through the ‘Largest Candidate Rule’ and ‘Ranked Positional Weight Technique’. Using these techniques, a software has been developed to arrange the elemental tasks in the workstation, and to show the balancing efficiencies of each method and other important information. The overall job may be very helpful in some decision making process of the organization. At last an efficient and balanced line has been proposed through the study.


2017 ◽  
Vol 7 (1) ◽  
pp. 1-22
Author(s):  
Kunal K. Ganguly ◽  
Siddharth Rai

Subject area The subject area of the case is operations management and capacity planning. The case adopts different operation strategies to use the idle capacity. Study level/applicability The case study is suitable for discussion in masters level classes. The case explains the situation of a company which is fighting for its survival. The case reveals the alternative operations strategies it applies to maximize its capacity utilization and reduce its costs. Case overview The case describes a paper producing company which is earning low margins. The company’s capacity remains unused during the off-seasons. The company then plans to share its capacity with another dying industry. Both the companies plan to cooperate and share resources. However, there are other attractive alternatives too and the dilemma situations leave the gap for continuous discussions. Expected learning outcomes The case aims at providing potential alternatives to the students and initiating healthy discussions. The students will be able to understand the capacity utilization dilemmas and applicability of the operations strategy concept in practice. Supplementary materials Teaching notes are available for educators only. Please contact your library to gain login details or email [email protected] to request teaching notes. Subject code CSS 9: Operations and Logistics.


2015 ◽  
Vol 761 ◽  
pp. 104-108
Author(s):  
Adi Saptari ◽  
Jia Xin Leau ◽  
M. Nor Akramin

In Line Balancing principles, the total workload in the assembly process is divided as evenly as possible among the workstations, without violating the sequences and relations in the assembly operations. Line balancing is important in an assembly system as it balances the line and increases the efficiency, as well as the productivity of a system. A case study was conducted in the assembly line of an electrical accessories manufacturer in Malaysia. The cycle time for each station was recorded, and the standard cycle time was estimated. The productivity, as well as the efficiency of the current assembly line, were studied. In terms of the productivity, the performance of the current systems was 500 units/worker/day, while the expected productivity was 600 units/worker/day. An assembly line setting was proposed based on the Line Balancing Method; the productivity for the proposed line increased to 671 units/worker/day, or in rough additional increase around 34%.


2021 ◽  
Author(s):  
Vítor Alcácer ◽  
João Rodrigues ◽  
Helena Carvalho ◽  
Virgílio Machado

Abstract Social, economic, and technological recent developments leading companies to face new production challenges. Companies will need physical and virtual structures allowing cooperation and quick adaptation along all value chain. To this matter, one of the main foundations of industry 4.0 is the use of information and communication technologies systems. Many companies are using information and communication systems without integration with business partners and even also with internal departments. This gap needs to be analyzed and it can be made by measuring the status of the industry 4.0 enabling technologies adoption inside a company using maturity or readiness models transmitting knowledge and pathing initiatives to help on progress and monitorization, looking forward to the future status of the internal value chain. On a qualitative and quantitative matter, this study presents the industry 4.0 enabling technologies readiness level of three departments of an automotive company internal value chain. This case study shows different readiness level on each department and limitations to reach better levels such as potential results if the benefits of industry 4.0 enabling technologies were reach on a company that assumes to be aligned with the industry 4.0 strategy.


Author(s):  
Gunji Venkata Punna Rao ◽  
S. Nallusamy

The objective of this research is to implement the lean techniques over CNC machine cells with standardization and line balancing for reduction of overall lead time. The methodology used for this research is a combination of traditional lean system with ZF production system. The analysis was carried out over CNC machine cells with the objective of standardization and line balancing of the cells. Primarily the standardization of the CNC manufacturing cells were done, so that the process is streamlined and optimized without non-value added activity. Also this study deals with productivity improvement in manufacturing line through continuous improvement using kaizen approach. Observation of cycle time was carried out by video based work study technique. The operational videos such as cycle time of various processes were captured and improvement possibilities were identified. Then line balancing was done to overcome bottlenecks between operations to meet customer TAKT time and to increase overall productivity. The overall output has been improved from 22 to 30 per week for all models of gear box. Lean tools such as standard work procedure and Kaizen were employed and found that the overall cycle time was reduced by about 609 minutes with an improvement of 17.54%.


Entropy ◽  
2021 ◽  
Vol 23 (3) ◽  
pp. 320
Author(s):  
Weng Siew Lam ◽  
Weng Hoe Lam ◽  
Saiful Hafizah Jaaman ◽  
Kah Fai Liew

The construction sector plays an important role in a country’s economic development. The financial performance of a company is a good indicator of its financial health and status. In Malaysia, the government encourages the construction industry to develop an advanced infrastructure related to health, transport, education and housing. In view of the COVID-19 pandemic, the operations and financial performance of construction sector companies have been affected recently. Additionally, uncertainty plays a vital role in the multi-criteria decision-making (MCDM) process. Based on previous studies, there has been no comprehensive study conducted on the evaluation of the financial performance of construction companies by integrating entropy and fuzzy VIKOR models. Therefore, this paper aims to propose an MCDM model to evaluate and compare the financial performance of construction companies with an integrated entropy–fuzzy VIKOR model. A case study is carried out by evaluating the listed construction companies in Malaysia with the proposed model. The findings of this paper indicate that the company ECONBHD achieves the best financial performance over the study period. The significance of this paper is to determine the priority of the financial ratios and ranking of the construction companies with the proposed entropy–fuzzy VIKOR model.


2012 ◽  
Vol 576 ◽  
pp. 742-746 ◽  
Author(s):  
Fredrik Schultheiss ◽  
Bengt Lundqvist ◽  
Jan Eric Ståhl

All companies strive towards lowering their manufacturing costs. Few companies do however succeed in continuously improving their production after the launch of a new production process. This article introduces a method for companies having an established technology to optimize their production in terms of part cost without disrupting the normal, day-to-day production. By incrementally chancing the process parameters such as for example cutting data as a function of the originally selected values, it is possible to optimize the production process. This is closely related to the lean production philosophy and long term sustainability which strives towards efficient use of resources and involvement of all employees in improving the production process. In the case study presented in this article it was found that by adding extra sulfur to the cutting fluid it was possible to decrease the part cost. By using the proposed method the company was able to decrease the part cost when manufacturing a specific part with approximately 5 %.


2021 ◽  
Vol 5 (1) ◽  
pp. 19-29
Author(s):  
Dwi Nurul Izzhati ◽  
Yuli Setyaningsih ◽  
Jazuli .

AbstractPT. PKM is a company engaged in the germant industry. In the production process there are problems related to waste that related to waste that causes the production target not being achieved in Oktober-November 2018 as many as 109, 414 pcs and only able to produce as much as 84,111 pcs. There fore solution with Lean Six Sigma was used consists of: 1). The define phase obtained three wastes including a defect of 13,121 pcs, an idle time of 794 seconds, and a total reworking of 577 seconds for 60 pcs of product rework. 2). Measure Phase in addition, there is also a line balancer efficiency value of 43.96% and a balance delay of 56%. 3). The analysis phase is carried out an analysis of the causal factors towards the type of stich jump and the type of idle bottleneck. The improvement phase is done by designing a new production line using the Line Balancing method and arena simulation that requires improvement with the number of stations reduced from 36 to 20 work stations balancing line efficiency to 79.12%, delaying the balance up to 21%, the number of outputs increasing from 137 pcs to 216 pcs, and bottlenecks decreased from 36% to 2.7%.In the control carried out to help smooth the design of new lines, namely by regulating the cycle time, arrival time and the number of entities, and the number of worker. Keywords: Waste, Lean Six Sigma, Line Balancing, Balance Delay  AbstrakPT. PKM merupakan perusahaan yang bergerak dalam industri garmen. Dalam sistem produksinya terdapat permasalahan terkait pemborosan yang menyebabkan tidak tercapainya target produksi pada bulan Oktober-November 2018 sebanyak 109.414 pcs, dan hanya mampu memproduksi sebanyak 84.111 pcs. Maka dicari solusi dengan pendekatan Lean Six Sigma, yang terdiri: 1). Tahap define diperoleh tiga pemborosan antara lain defect sebanyak 13.121 pcs, idle time sebesar 794 detik, dan total rework sebesar 577 detik untuk 60 pcs produk rework. 2) Tahap measure didapatkan jenis cacat dominan yaitu jump of stich dan jenis idle dominan yaitu bottleneck. Selain itu juga diketahui nilai line balancing eficiency sebesar 43,96% dan balance delay 56%. 3) Tahap analyze dilakukan analisis faktor penyebab terhadap jenis cacat jump of stich dan jenis idle bottleneck. 4). Tahap improve dilakukan perancangan lini produksi baru dengan metode Line Balancing dan simulasi arena didapatkan kondisi perbaikan dengan jumlah stasiun turun dari 36 menjadi 20 stasiun kerja line balancing efficiency menjadi 79,12%, balance delay turun menjadi 21%, jumlah output meningkat dari 137 pcs menjadi 216 pcs, dan bottleneck menurun dari 36% menjadi 2,7%. Pada tahap control dilakukan untuk membantu kelancaran perancangan line baru, yaitu dengan mengontrol waktu siklus, waktu kedatangan dan jumlah entitas, serta jumlah tenaga kerja. Kata kunci: Pemborosan, Lean Six Sigma, Line Balancing, Balance DelayReferensi[1]        Darsono. (2013). Analisis Pengendalian Kualitas Produksi dalam Upaya Mengendalikan tingkat Kerusakan Produk. Jurnal Ekonomi Manajemen Akuntansi.[2]        Nasution, M., N. (2005). Manajemen Mutu Terpadu. Jakarta: Ghalia Indonesia.[3]        Goetsch D. L., S. B. Davis. (1994). Pengertian Kualitas. Jakarta: PT. Prenhalindo.[4]        Purponi P. & D. Andesta. (2009). Integrasi Model Lean Six Sigma untuk Peningkatan Kualitas Produksi. Jurnal Teknik industri, 10 (2), 91-97.[5]        Ahyari, Agus. (1992). Pengertian Pengendalian Kualitas. Yogyakarta:   BPFE Yogyakarta.[6]        Hartini. (2011). Teknik Mencapai Produksi Optimal. Bandung: CV Lubuk Agung.[7]        Gaspersz, V. (2007). Lean Six Sigma for Manufacturing and Service Industries. Jakarta: PT.   Gramedia Pustaka Utama.


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