scholarly journals Applicability of a Combined DAF-MF Process to Respond to Changes in Reservoir Water Quality through a Two-Year Pilot Plant Operation

Membranes ◽  
2021 ◽  
Vol 11 (12) ◽  
pp. 964
Author(s):  
Joon-seok Kang ◽  
Jayeong Seong ◽  
Jewan Yoo ◽  
Pooreum Kim ◽  
Kitae Park ◽  
...  

The optimal operating conditions of a combined dissolved air flotation (DAF)-microfiltration (MF) process to respond to changes in raw water quality were investigated by operating a pilot plant for two years. Without DAF pre-treatment (i.e., MF alone), MF operated stably with a transmembrane pressure (TMP) increase of 0.24 kPa/d when the turbidity of raw water was low and stable (max. 13.4 NTU). However, as the raw water quality deteriorated (max. 76.9 NTU), the rate of TMP increase reached 43.5 kPa/d. When DAF pre-treatment was applied (i.e., the combined DAF-MF process), the MF process operated somewhat stably; however, the rate of TMP increase was relatively high (i.e., 0.64 kPa/d). Residual coagulants and small flocs were not efficiently separated by the DAF process, exacerbating membrane fouling. Based on the particle count analysis of the DAF effluent, the DAF process was optimised based on the coagulant dose and hydraulic loading rate. After optimisation, the rate of TMP increase for the MF process stabilised at 0.17 kPa/d. This study demonstrates that the combined DAF-MF process responded well to substantial changes in raw water quality. In addition, it was suggested that the DAF process must be optimised to avoid excessive membrane fouling.

2011 ◽  
Vol 11 (4) ◽  
pp. 481-489
Author(s):  
S. Krause ◽  
A. Obermayer

The public drinking water supply of southern Germany is characterized by a rather decentralized network. Due to the hydrogeological setting in these parts of Germany many of the small water works with an average capacity of 50 m3/h have to treat raw water extracted from karstic or cliffy aquifers. These raw waters tend to be contaminated with particles and pathogens acquired during snowmelt or after strong rainfalls. In the last decade ultrafiltration has become the technology of choice for the removal of the aforementioned contaminants. Flux decline caused by unanticipated membrane fouling is the main limitation for the application of ultrafiltration membranes. This paper describes how membrane fouling phenomena can be predicted by using a statistical approach based on data from large scale filtration systems in combination with field and lab experiments on raw water quality and membrane performance. The data defines water quality and respective fouling phenomena both in technical scale filtration plants and in lab experiments of eleven different raw waters. The method described here is more economically feasible for small water works when compared to typical pilot experiments that are used for high capacity water works.


1998 ◽  
Vol 37 (2) ◽  
pp. 43-48 ◽  
Author(s):  
Oluf Hoyer ◽  
Helmut Schell

On-line monitoring of turbidity allows effective control of source and finished water quality. Fundamentals for particle destabilisation and removal are outlined and the application of the charge titration method for optimal online adjustment of the flocculant dosage is presented.


Membranes ◽  
2021 ◽  
Vol 11 (8) ◽  
pp. 553
Author(s):  
Dimitra C. Banti ◽  
Manassis Mitrakas ◽  
Petros Samaras

A promising solution for membrane fouling reduction in membrane bioreactors (MBRs) could be the adjustment of operating parameters of the MBR, such as hydraulic retention time (HRT), food/microorganisms (F/M) loading and dissolved oxygen (DO) concentration, aiming to modify the sludge morphology to the direction of improvement of the membrane filtration. In this work, these parameters were investigated in a step-aerating pilot MBR that treated municipal wastewater, in order to control the filamentous population. When F/M loading in the first aeration tank (AT1) was ≤0.65 ± 0.2 g COD/g MLSS/d at 20 ± 3 °C, DO = 2.5 ± 0.1 mg/L and HRT = 1.6 h, the filamentous bacteria were controlled effectively at a moderate filament index of 1.5–3. The moderate population of filamentous bacteria improved the membrane performance, leading to low transmembrane pressure (TMP) at values ≤2 kPa for a great period, while at the control MBR the TMP gradually increased reaching 14 kPa. Soluble microbial products (SMP), were also maintained at low concentrations, contributing additionally to the reduction of ΤΜP. Finally, the step-aerating MBR process and the selected imposed operating conditions of HRT, F/M and DO improved the MBR performance in terms of fouling control, facilitating its future wider application.


2009 ◽  
Vol 34 (13-16) ◽  
pp. 806-811 ◽  
Author(s):  
Md. Pauzi Abdullah ◽  
Lim Fang Yee ◽  
Sadia Ata ◽  
Abass Abdullah ◽  
Basar Ishak ◽  
...  

2012 ◽  
Vol 12 (6) ◽  
pp. 918-925 ◽  
Author(s):  
Y. Sangu ◽  
H. Yokoi ◽  
H. Tadokoro ◽  
T. Tachi

An automatic coagulant dosage control technology for water purification plants was developed to deal with rapid changes of raw water quality parameters. Control logic was developed to decide coagulant dosage based on aluminum concentration in rapid mixing tank water based on results of semi-pilot scale experiments. This logic enabled quick feedback on the excess or lack of coagulant. It was found that the aluminum residual rate, which was proposed as an indicator of coagulation reactions, could be given as a function of coagulant dosage and turbidity. The effectiveness of the control logic was verified in semi-pilot scale experiments. Settled water turbidity was within ±0.5 NTU of target value even when raw water turbidity increased rapidly up to 100 NTU.


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