Upgrade and Operation of Nitrogen and Phosphorus Removal Process in the Sewage Treatment Plant of Jinan City

2013 ◽  
Vol 864-867 ◽  
pp. 1616-1620
Author(s):  
Lin Bo Sun ◽  
Shun Tian ◽  
Wen Juan Chen ◽  
Wei Jian Jia ◽  
Yong Lei Wang

The designed capacity of Jinan Citys wastewater treatment plant (the second sewage treatment plant) is 200,000 m3/d, and the biological treatment process is DE-type oxidation ditch process. Because of self-control requirements, equipment quality and management , alternat-ing operation of anoxia and oxygen can not be achieved. Acting in concert with the engineering of south-to-north water diversion and water quality improvement of the Xiaoqing River, water quality improvement and transformation of nitrogen and phosphorus removal process was condu-cted. By increasing the diversion wall, digestive reflux and other measures, the DE oxidat-ion ditch process was transformed into A2/O process, while the depth of V-efficiency fiber filter processing and chemical phosphorus removal process were increased. After the upgrade, the process is stable, the effluent quality reached an A standard of " discharge standard of pollutants for municipal wastewater treatment plant" (GB18918-2002).

2006 ◽  
Vol 78 (3) ◽  
pp. 284-293 ◽  
Author(s):  
Allen P. Davis ◽  
Mohammad Shokouhian ◽  
Himanshu Sharma ◽  
Christie Minami

1992 ◽  
Vol 25 (4-5) ◽  
pp. 355-362 ◽  
Author(s):  
H. A. Feyen

Because of increased effluent quality standards the central sewage treatment plant (STP) of Stolberg is upgraded into a two stage plant according to the AB-process. Special peculiarities of the rebuilding are several combined technologies for nitrogen and phosphorus removal and for the optimization of sludge treatment including energy recovery. Apart from special features of construction and machinery a remarkable process control system is installed, which operates with several linked personal computers instead of a main frame process computer. At the beginning of the reconstruction tests were carried out in a semitechnical pilot plant. Results of these tests as well as first operation results of the large STP allow a good adjustment of the especially high quality standards to be expected.


2019 ◽  
Vol 1 (2) ◽  
pp. 97-99
Author(s):  
Samaneh Alijantabar aghouzi

Study on ammonia nitrogen and phosphorus removal using sequencing batch reactor Samaneh Alijantabar Aghouzi * Department of Chemical and Environmental Engineering, Faculty of Engineering Universiti Putra Malaysia, Serdang Malaysia   Thomas S. Y. Choong Sustainable Process Engineering Research Center (SPERC) Universiti Putra Malaysia, Serdang Malaysia   Aida Isma M. I. Centre for Water Research, Faculty of Engineering and the Built Environment SEGi University, Kota Damansara Malaysia   *Corrosponding author’s Email: [email protected]                   Peer-review under responsibility of 3rd Asia International Multidisciplanry Conference 2019 editorial board (http://www.utm.my/asia/our-team/) © 2019 Published by Readers Insight Publisher, lat 306 Savoy Residencia, Block 3 F11/1,44000 Islamabad. Pakistan, [email protected] This is an open access article under the CC BY-NC-ND license (http://creativecommons.org/licenses/by-nc-nd/4.0/).     _________________________________________________________   Research Highlights   The highest phosphorus and ammonia nitrogen removal efficiencies were 99.5% and 51%, respectively, in 6 hours. Particle size of sludge reduced from 26 μm to 39.81 μm in 60 days. Fourier transform infrared spectroscopy (FTIR) showed that N-O, N–H, S=O and C=N compunds detected. ___________________________________________________________________________   Research Objectives   Ammonia nitrogen and phosphorus removal have becoming more rigorous in permits making it one of the most important and most difficult processes to maintain in wastewater treatment plants. Sequencing batch reactor is a controlled activated sludge process that is able to tackle ammonia nitrogen and phosphorus issues and has some benefits such as having a small-scale system and low construction cost (1). The main goal of this research is to investigate the ability of SBR in treating sewage containing phosphorus and ammonia nitrogen in 6 hours to achieve the allowable effluent discharge standard set by the Department of Environment Malaysia.     Materials and Methods   In this experiment, a sequencing batch reactor with a total volume of 7 L. The mechanical stirrer was used to avoid sludge settling with a speed of 100 rpm. A fine bubble diffuser was used to supply air. The operation time was controlled based on 1 h and 30 mins anaerobic, 2 h and 10 mins anoxic, 1 h and 50 mins aerobic, making the hydraulic retention time (HRT) of 6 hours. 10 L seed sludge and 30 L raw sewage samples were collected weekly from the sewage treatment plant that was located in Selangor and were kept under 4oC in cold room in order to obtain fresh samples. The sludge volume was 30% of raw sewage volume in the reactor and the reactor refilled with 3.5 liters of raw sewage at the start point of the experiment. The experiment was carried out in room temperature of  27±3 oC with the pH value ranging from 6 to 8 and dissolve oxygen value ranging from 0 to 6 mg/L. Phosphorus and ammonia nitrogen were measured according to the APHA method (2). DO and PH were measured by using DO meter (JPB-70A) and PH meter (CT-6821, Shenzhen Kedida Electronic CO).     Results   The highest ammonia nitrogen removal efficiencies observed to be 31.9 %, 10.3 % and 38.8 % at the respective phases of anaerobic, anoxic and aerobic, respectively. Results showed that the phosphorus removal efficiencies for anaerobic, anoxic and aerobic phases were 70.43 %, 19.16%, and 98.58%, respectively in 6 hours. The highest phosphorus removal efficiency recorded was 98.58% that took place in the aerobic phase because of the absence of sufficient nitrate which can inhibit phosphorus uptake during the aerobic phase. The most sensitive process is nitrification that helps to biological oxidation of ammonia to nitrate, which is performed by two types of microorganisms, i.e. ammonia-oxidizing bacteria (AOB) and nitrite-oxidizing bacteria (NOB) (3). Karl et al. claimed that toxic substances inhibit the metabolism of bacteria (4). Mino et al. (5) also stated that nitrification process will not be accomplished in anaerobic phase without the presence of nitrate. This will affect the phosphorus uptake in the aeration phase.   Findings   FTIR spectrum shows that N-O, N–H, S=O and C=N compounds were identified in the sludge. The presence of these compounds might affect the nitrification and denitrification processes and indirectly affecting the degradation the ammonia nitrogen and phosphorus. Sewage sample might also contain heavy metals as the sewage treatment plant was located in the industrial area.     Acknowledgment   The authors gratefully thank the financial and research support of Universiti Putra Malaysia.   References Sathian, S, M Rajasimman, C S Rathnasabapathy, and C Karthikeyan. 2014. “Journal of Water Process Engineering Performance Evaluation of SBR for the Treatment of Dyeing Wastewater by Simultaneous Biological and Adsorption Processes.” Journal of Water Process Engineering 4: 82–90. APHA. Standard Methods For the examination of water and Wastewater 23rd ed. ed. Washington, D.C.2017. Chang HN, Moon RK, Park BG, Lim S, Choi DW. Simulation of sequential batch reactor ( SBR ) operation for simultaneous removal of nitrogen and phosphorus. 2000;23. Karl DM, States U. Nitrogen Cycle ☆. 3rd ed. Encyclopedia of Ocean Sciences, 3rd Edition. Elsevier Inc.; 2018. 1-10 p. Mino T, Loosdrecht MCM van, Heijnen JJ. Microbiology and biochemistry of the EBPR process. Water Res. 1998;32(11):3193–207.


1987 ◽  
Vol 19 (9) ◽  
pp. 1-7
Author(s):  
K. C. Das

The James River has its head waters in the Allegheny Mountains and flows generally southeasterly to Hampton Roads, Chesapeake Bay and thence to the Atlantic Ocean. Below Richmond, Virginia, the river is tidal with the channel meandering through the coastal plains. Below Hopewell it widens to a broad estuary, with a deep navigable channel bordered by tide marshes. The upper estuary, between Richmond and Hopewell, is heavily used for water supply, recreation, and industrial development. The water entering the estuary a few miles upstream of Richmond is of good quality. However, as one reaches Richmond, the quality of the water deteriorates. There are eleven major discharging municipalities and industries within a stretch of twenty two river miles between Richmond and Hopewell. The major factors contributing to water quality problems below the City of Richmond stem from the intermittent discharge from combined sewer overflows (CSOs) coupled with the continuous discharge from the City's sewage treatment plant. The CSOs contribute a large quantity of soluble BOD, suspended solids, settleable solids, and fecal coliforms to the estuary. The City's sewage treatment plant continuously discharges large quantities of ammonia-nitrogen and phosphorus, in addition to BOD and suspended solids. Rational Management and use of the waters of the upper James estuary appear to be critical. The objectives of this paper, therefore, are the discussion of the present water quality and the wastewater discharge reductions required in order to meet certain water quality and water use objectives.


2008 ◽  
Vol 37 (2) ◽  
Author(s):  
Maciej Walczak

Changes of microbial indices of water quality in the Vistula and Brda rivers as a result of sewage treatment plant operationThis paper reports the results of studies of microbiological changes in the water quality of the Vistula and Brda rivers after the opening of sewage treatment plants in Bydgoszcz. The study involved determining the microbiological parameters of water quality. Based on the results obtained, it was found that the quality of the water in both rivers had improved decidedly after the opening of the plants, although an increased number of individual groups of microorganisms was found at the treated sewage outlet from one of the plants.


2001 ◽  
Vol 43 (11) ◽  
pp. 109-117 ◽  
Author(s):  
D. Bixio ◽  
P. van Hauwermeiren ◽  
C. Thoeye ◽  
P. Ockier

The municipal sewage treatment plant (STP) of the city of Ghent (Belgium) has to be retrofitted to a 43%-increase in the nitrogen treatment capacity and to phosphorus removal. Cold weather, dilute sewage and a critical COD over N ratio make the retrofit a challenge for full biological nutrient removal. The potential for fermentation of primary sludge to alter those critical feed sewage characteristics was experimentally evaluated. The idea was that the pinpoint introduction of fermentate could optimise the available reactors by achieving high-rate denitrification and enhanced biological phosphorus removal. The fermentation process was evaluated with a bench scale apparatus. At 20°C (heated process), the hydrolysis yield - expressed in terms of soluble COD - varied from 11% to 24% of the total sludge COD. The fermentation yield expressed in VFA COD varied from 8% to 13% of the total sludge COD. The efficiency of heated fermentation of primary sludge was lower during cold and wet weather, due to the different sewage characteristics, as a result of extended dilution periods and low temperature. The raw sewage, the primary effluent and the fermentate were fractionated according to the requirements for the IAWQ Activated Sludge Model No. 2d. The results clearly show that fermentation in the sewer played an important role and temperature was the driving parameter for the characteristics of the dissolved COD. Instead, the weather flow conditions were the driving parameter for the characteristics of the suspended COD. The results of the detailed fractionation were used as background for process evaluation. The final scenario choice for the retrofit depends on a cost-efficiency calculation.


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