Roll Casting of Al-25mass%Si

2010 ◽  
Vol 97-101 ◽  
pp. 1057-1060 ◽  
Author(s):  
Ryoji Nakamura ◽  
Masayuki Saito ◽  
Shinji Kumai ◽  
Hisaki Watari

Roll casting of Al-25mass%Si hyper eutectic aluminum alloy strip was tried by an unequal diameter twin roll caster. The casting speed was 10m/min. The thickness of the strip was about 2mm. The eutectic Si and primary crystallized Si were very fine by the effect of the rapid solidification. The size of the primary crystallized Si was not uniform at the thickness direction. The primary crystallized Si at the near surface was finer than that of inside. The eutectic Si was finer than 2μm. The strip could be cold rolled after hot rolling and annealing.

2010 ◽  
Vol 443 ◽  
pp. 128-133 ◽  
Author(s):  
Ryoji Nakamura ◽  
Masakazu Sawai ◽  
Ryoji Nakamura ◽  
Takanori Yamabayashi ◽  
Shinji Kumai ◽  
...  

A roll caster, which could cast the three layers of clad strip directly from the molten metal, was designed, assembled and tested. The base strip was AA3003 aluminum alloy and overlay strips were AA4045 aluminum alloy. An unequal diameter twin roll caster was modified to cast clad strip. Two small rolls were amounted on a large roll. A scraper plate was used to prevent the mixture of the different kinds of melts. The casting of three strips and the connecting of strips could be operated by one roll caster. The interfaces between the strips were clear, and the mixture of the melt did not occur. The clad strip could be cold rolled without the annealing. The clad strip did not peel at connecting surface by the cold rolling and continuous bending. The strips were connected strictly. The casting speed was 20m/min, and this speed was much higher than the casting speed of the conventional twin roll caster for aluminum alloys.


2010 ◽  
Vol 139-141 ◽  
pp. 477-480
Author(s):  
Ryoji Nakamura ◽  
Shuya Hanada ◽  
Shinji Kumai ◽  
Hisaki Watari

An inline hot rolling was operated on 5182 aluminum alloy strip cast using a vertical type high speed caster (VHSTRC) at the speed of 60 m/min. A porosity existing at center line of the thickness and a ripple mark on the surface, these are typical defects of the strip cast by the VHSTRC, could be improved by the inline rolling. The rolling speed was as same as the roll-casting-speed of 60m/min. The temperature of the strip, when the inline rolling was operated, was 450oC. The reduction of the strip of the inline rolling was 35%.


2010 ◽  
Vol 139-141 ◽  
pp. 481-484
Author(s):  
Ryoji Nakamura ◽  
Teppei Nakamura ◽  
Ryoji Nakamura ◽  
Hideto Harada ◽  
Shinji Kumai ◽  
...  

Roll casting of Al-SiCp composite alloy strip was tried using a vertical type high speed twin roll caster equipped with mild steel rolls. The Al-20vol% SiCp and Al-30vol%SiCp alloy could be roll-cast to the strip. The casting speed was 30m/min. The thickness of as-cast strip was thinner than 2.5mm. The SiCp powder was dispersed uniformly at the thickness direction. The as-cast strip could be thin down to 1mm by the hot rolling and the cold rolling without broken.


2006 ◽  
Vol 116-117 ◽  
pp. 379-382 ◽  
Author(s):  
Ryoji Nakamura ◽  
Hideki Inui ◽  
Hisaki Watari ◽  
Shinji Kumai

A356 was cast into the strip by the semisolid strip casting using an unequal diameter twin roll caster. This process was one of the rheocasting. The semisolid slurry was made by a cooling slope. Solid fraction was about 5%. The casting speed was 20 m/min, and the thickness was 4.4 mm. The as-cast strip could be cold rolled down to 1 mm. The result of tension test of 1mm-thickness-T4 heat-treated strip was as below. Tensile stress was 223 MPa, 0.2 proof stress was 123 MPa and elongation was 21.8%. Deep drawing could be operated to 1 mm-thickness T4 sheet, and L.D.R was attained to 2.0. In some condition, 180 degrees bending could be operated without crack at outer surface. These results mean that semisolid roll cast A356 strip may be able to use for press forming.


2017 ◽  
Vol 904 ◽  
pp. 3-8 ◽  
Author(s):  
Toshio Haga ◽  
Kento Ikeda ◽  
Takafumi Nakano

A 400 mm width of clad strip consisting of Al-40%Sn-1%Cu and 1070 aluminum alloy could be cast directly from molten metals at a speed of 10 m/min by an unequal diameter twin roll caster equipped with a scraper. An interface clearly existed between the two strips of the clad strip. As-cast clad strip could be cold rolled down to 1 mm without peeling at the interface. The as-cast clad strip could also be bent in the full contact condition without peeling at the interface.


2011 ◽  
Vol 264-265 ◽  
pp. 1905-1910 ◽  
Author(s):  
Ryoji Nakamura ◽  
Toshio Haga ◽  
Shinji Kumai ◽  
Hisaki Watari

In this study, the roll casting of Al-40%Sn-1%Cu alloy was tried by an unequal diameter twin roll caster. The unequal diameter twin roll caster could continuously cast the strip. The casting load of the roll was small to prevent the flow out of the Sn. The roll-load was 0.1kN/mm(unit width). The roll casting of 400mm-width strip of 8mm-thick was tried, and it was attained. The gravity segregation of Sn did not occur. The as-cast strip could be cold rolled down to 1mm. However, this strip had much porosity. The rapid solidification was useful to prevent the porosity. The copper roll was better than steel roll to increase cooling ability. The copper roll was suitable to prevent the porosity. The temperature of solidified metal was important factor which influenced the porosity. The 4mm-thickness strip with little porosity was could be cast at the speed of 30m/min.


2012 ◽  
Vol 430-432 ◽  
pp. 669-672
Author(s):  
Toshio Haga ◽  
Hideto Harada ◽  
Shinji Kumai ◽  
Hisaki Watari

Strip casting of Al-25%Si strip was tried using an unequal diameter twin roll caster. The diameter of the lower roll (large roll) was 1000mm and the diameter of the upper roll (small roll) was 250mm. Roll material was mild steel. The sound strip could be cast at the speeds ranging from 8 m/min to 12 m/min. The strip did not stick to the roll without the parting material. The primary Si, which existed at centre area of the thickness direction, was larger than that which existed at other area. The size of the primary Si was smaller than 0.2 mm. Eutectic Si was smaller 5μm. The as-cast strip was ranging from 2mm to 3mm thick and its width was 100mm. The as-cast strip could be hot rolled down to 1mm. The hot rolled strip was cold rolled. The primary Si became smaller and the pore occurred around the primary Si after the rolling.


2008 ◽  
Vol 141-143 ◽  
pp. 295-300 ◽  
Author(s):  
Ryoji Nakamura ◽  
T. Asai ◽  
Hisaki Watari ◽  
Shinji Kumai

Rheo-casting of 4045 aluminum alloy bar was operated using an unequal diameter twin roll caster and a cooling slope. The semisolid slurry was made by the cooling slope. The thickness of the bar was 12 mm and width was 100mm. The casting speed was 1m/min. Quantity of the melt poured on the cooling slope was important to make sound bar. The primary crystal became spherical, and its size was about 40μm.


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