phosphorus steel
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2020 ◽  
Vol 992 ◽  
pp. 689-694 ◽  
Author(s):  
O.S. Bondareva ◽  
A.M. Turovsky ◽  
Y.M. Turovsky

Alloying zinc melt with nickel is used to control the thickness of the zinc coating on steels with different contents of silicon and phosphorus. Nickel is involved in the formation of iron-zinc phases in the coating and inhibits their growth. The use of zinc-nickel master alloys is well studied and has a significant disadvantage - the significant wastage of nickel in the bottom dross. The application of nickel tablets avoids wastage, because it allows us to distribute nickel evenly throughout the bath volume. The aim of this work was to determine the working concentration of nickel introduced into the melt from nickel tablets for a wide range of silicon-containing steels and for a galvanizing time of 2-5 minutes. It was found that the nickel concentration of 0.04% leads to the coating thickness decrease and normalization of the variation in coating thickness on steels with a silicon equivalent SiEV 0.12-0.28% at the galvanizing time of 2-5 minutes, and on high-silicon steel (SiEV 0.75%) at the holding time of 3 minutes. A nickel concentration of 0.03% is effective for SiEV steels 0.12-0.18% with a galvanizing time of 2-3 minutes. "Sandeline Peak" is completely smoothed out with a holding time of 3-5 minutes in the melt with a Ni content of 0.05%. The nickel presence in the zinc melt modifies the ζ-phase structure in the coating, making it more dense and uniform in thickness.


Author(s):  
Vartika Gupta ◽  
S K Rajput ◽  
Yashwant Mehta ◽  
Shashee Kant Soni ◽  
Tarun Soota

2018 ◽  
Vol 37 (7) ◽  
pp. 625-633
Author(s):  
Yang Wang ◽  
Shufeng Yang ◽  
Jingshe Li ◽  
Jie Feng ◽  
Feng Wang

AbstractThe double-slag converter steelmaking process can smelt low- and ultra-low-phosphorus steel and reduce lime and dolomite consumption and the amount of final slag simultaneously. Industrial steelmaking tests on a 150-metric ton converter at the Tangsteel Company were carried out to study this principle and its effect on the dephosphorization ratio and material consumption. The results showed that low-temperature stage could be used with a reduced amount of slag in the double-slag steelmaking process to achieve rapid and efficient dephosphorization. A low-basicity slag (~1.5–2.0) in the dephosphorization stage is required in double-slag process. The dephosphorization ratio reached a maximum of 71 % when the slag basicity was 1.7. The end-point phosphorus content after the smelting process was reduced from an average of 0.018 mass% to an average of 0.011 mass% and the dephosphorization efficiency increased by more than 6 %. The dephosphorization slag could be poured out rapidly when the FeO content was controlled at ~16–20 mass% in the double-slag smelting process. Based on key factors such as an efficient dephosphorization and a rapid iron–slag separation, the production efficiency was improved and the smelting cycle increased by only four minutes over the conventional process.


2017 ◽  
Vol 4 (9) ◽  
pp. 9380-9383 ◽  
Author(s):  
A.K. Katiyar ◽  
S.K. Rajput ◽  
Yashwant Mehta

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