First Successful Application of Casing in Casing CiC Refracturing Treatment in Shale Gas Well in China: Case Study

2021 ◽  
Author(s):  
Yaowen Liu ◽  
Yuanzhao Li ◽  
Chi Zhang ◽  
Yue Ming ◽  
Jialin Xiao ◽  
...  

Abstract With active hydraulic fracturing performed since 2012, the Fuling shale gas field in China is one of the largest shale gas fields outside of North America. Recently, a Casing-in-Casing (CiC) refracturing treatment was successfully implemented, resulting in production beyond expectations. This was the first successful application of a CiC refracturing treatment in a horizontal shale gas well in this region, thus providing a new option for refracturing horizontal wells in China. Bullheading diversion refracturing with diverting balls was previously attempted in this field with high initial production observed; however, production was inconsistent and quickly declined. Therefore, the operator decided to attempt a CiC refracturing method in an understimulated candidate well. This involved installing and cementing 3.5-in. casing in 5.5-in. casing to effectively isolate the perforations, which enabled plugging and perforating operations in the reconstructed wellbore for an effective refracturing treatment. A customized refracturing design integrated the production profile, residual recoverable reserves, and the specific 5.5- × 3.5-in. reconstructed wellbore limitation. The length of the 3.5-in. casing was optimized to be as short as possible but still cover the original perforations, and high-performance slickwater was used to reduce pipe friction, thus increasing the treatment rate. An engineered breakdown approach was employed for improved fracture initiation. Additionally, more clusters were added between the original clusters and, based on production profile results, some of the original understimulated clusters with little proppant placement were reperforated. To overcome the impact of depleted fractures, a self-degradable particulate diverting agent was used to propagate new fractures, allowing access to new rock to increase total reserve recovery. The treatment in the reconstructed wellbore was successful, with 21 stages fractured in 12 days, achieving 100% placement of the designed proppant and fluid. A treatment rate of 7 to 12 m3/min from the toe to heel was executed as designed. Test production of 183,800 m3/D was also achieved with a recovery rate of 88.1%. Production has remained consistent and wellhead pressure has remained steady at a high level throughout the first two months of production. CiC refracturing technology helps overcome common disadvantages experienced with traditional refracturing techniques, such as poorly placed proppant and fluid and inconsistent production. CiC refracturing not only allows exploitation of bypassed reserves from original fractures, but also allows precise stimulation of new rock to obtain the highest reserve recovery. The successful implementation of this case study illustrates the reliability of CiC refracturing technology and provides valuable experience to be used during future regional horizontal well refracturing.

2015 ◽  
Vol 8 (1) ◽  
pp. 149-154 ◽  
Author(s):  
Jun Gu ◽  
Ju Huang ◽  
Su Zhang ◽  
Xinzhong Hu ◽  
Hangxiang Gao ◽  
...  

The purpose of this study is to improve the cementing quality of shale gas well by mud cake solidification, as well as to provide the better annular isolation for its hydraulic fracturing development. Based on the self-established experimental method and API RP 10, the effects of mud cake solidifiers on the shear strength at cement-interlayer interface (SSCFI) were evaluated. After curing for 3, 7, 15 and 30 days, SSCFI was remarkably improved by 629.03%, 222.37%, 241.43% and 273.33%, respectively, compared with the original technology. Moreover, the compatibility among the mud cake solidifier, cement slurry, drilling fluid and prepad fluid meets the safety requirements for cementing operation. An application example in a shale gas well (Yuanye HF-1) was also presented. The high quality ratio of cementing quality is 93.49% of the whole well section, while the unqualified ratio of adjacent well (Yuanba 9) is 84.46%. Moreover, the cementing quality of six gas-bearing reservoirs is high. This paper also discussed the mechanism of mud cake solidification. The reactions among H3AlO42- and H3SiO4- from alkali-dissolved reaction, Na+ and H3SiO4- in the mud cake solidifiers, and Ca2+ and OH- from cement slurry form the natrolite and calcium silicate hydrate (C-S-H) with different silicate-calcium ratio. Based on these, SSCFI and cementing quality were improved.


2013 ◽  
Author(s):  
Aimen Amer ◽  
Rolando di Primio ◽  
Robert Ondrak ◽  
Vikram Unnithan

2019 ◽  
Vol 8 (4) ◽  
pp. 2992-2995

The transportation and distribution (T&D) of nascent informal sectors, it is important to have a good performance in operations. In order to achieve high performance, it is necessary to know which operational factors are critical for success and which are less important. Only then can management focus attention on those factors that have a strong effect on performance. In The India a large project has been carried out to find these critical operational success factors. The progress in techniques and management principles improves the moving load, delivery speed, service quality, operation costs, the usage of facilities and energy saving. Transportation takes a crucial part in the manipulation of logistic. The objective of study is the impact on GDP from logistics savings. To measure efficiency gains of drivers in logistics savings, to study the effect of efficiency gains on nominal GDP. The study is case study method adopted based on secondary data and it is concluded that the GDP impact on efficiency gains of transportation and distribution of nascent informal sectors in India exhibited that customers’ final bill remains same; Transport company’s profits go up and customer takes away all the savings


2021 ◽  
Author(s):  
S. An ◽  
X. Liang ◽  
G. Yu ◽  
D. Li ◽  
J. Wu ◽  
...  

2016 ◽  
pp. 624-643
Author(s):  
Arwa Mukhtar Makki ◽  
Tarig Mohamed Ahmed

Risk identification and prioritization is very essential activity in any successful strategic risk management process. Developing a plan for dealing with such problems reduces the impact of unexpected risks and failures while prioritizing risks draws attention, efforts and resources to the risks with great impact on projects success. The aim of this paper, is to identify the critical risk factors in an ERP project through a case study of a successful implementation of an ERP system in a Sudanese organization and to understand how the organization implemented the appropriate controls to minimize its business risks impact. To achieve this objective, a number of key articles were reviewed and analyzed to understand the different critical risk factors influence ERP implementation. New risk factors and controls influence ERP implementation have been identified. A new model of ERP implementation critical risk factors was developed. Furthermore, the risk factors were classified into categories, probability, impact and proximity, then using a prioritizing tool, the results of this study contributes to risks identification and prioritization by pointing to the less priority and the most critical risk factors.


2019 ◽  
Vol 103 ◽  
pp. 114-125 ◽  
Author(s):  
Jizheng Yi ◽  
Hanyong Bao ◽  
Aiwei Zheng ◽  
Boqiao Zhang ◽  
Zhiguo Shu ◽  
...  

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