Operation of a submerged aerobic membrane bioreactor for decentralised municipal wastewater treatment in North Africa

2012 ◽  
Vol 7 (3) ◽  
Author(s):  
George Skouteris ◽  
Tom C. Arnot ◽  
Firas Feki ◽  
Mouna Jraou ◽  
Sami Sayadi

A pilot-scale aerobic membrane bioreactor (MBR) was operated for 6.5 months, alongside a full-sized conventional activated sludge (AS) plant, treating high-strength domestic wastewater originating from Sfax in Tunisia. The main target was to investigate whether or not the MBR could produce effluent suitable for unrestricted crop irrigation in Tunisia, a target that the AS plant fails to achieve. Membrane performance analysis and energy benchmarking were also carried out. The MBR did produce irrigation quality water regardless of the mixed-liquor suspended solids (MLSS) or feed concentrations. The average chemical oxygen demand (COD) removal efficiency was 88% at an average MLSS concentration of 4.59 g L−1, and 89.7% at an average MLSS concentration of 9.52 g L−1. During membrane performance evaluation, a maximum sustainable membrane permeate flux of 12.81 L m−2 h−1, at an average mixed-liquor temperature of 24 °C and an average MLSS concentration of 9.21 g L−1 was maintained. Finally, energy benchmarking was carried out; the average energy consumption rate was 8.95 kWh d−1, corresponding to an average specific energy demand (SED) of 3.82 kWh m−3. This is a relatively high value compared to the AS plant, whose SED value is always lower than 3 kWh m−3, but further energy reduction is possible for the MBR as well as the AS plant effluent requires further treatment in order to be acceptable for unrestricted human crop irrigation; hence, additional energy input. The work demonstrates the potential impact of MBRs in decentralised domestic wastewater treatment in North Africa.

2003 ◽  
Vol 3 (5-6) ◽  
pp. 253-259
Author(s):  
C. Blöcher ◽  
T. Britz ◽  
H.D. Janke ◽  
H. Chmiel

The application of a membrane bioreactor (MBR) was investigated to treat polluted process water from fruit juice processing. The aim was either direct discharge or further treatment by nanofiltration/low pressure reverse osmosis to produce water of drinking quality. The results of a one-year test operation of the process in industrial scale at a fruit juice production plant are presented. Focus was centred on the influence of activated sludge characteristics on membrane performance. Under the operating conditions in place, neither solids content, particle size distribution nor addition of nutrient significantly affected the permeate flux which was considerably lower than expected (based on municipal wastewater treatment with MBRs). Instead, evidence was obtained that the insufficient permeate flux was most likely due to the high content of extracellular polymeric substances. However, it was impossible to relate in detail the substantial flux variations during the test run to AS characteristics or changes in microbial population.


2000 ◽  
Vol 41 (10-11) ◽  
pp. 243-250 ◽  
Author(s):  
X-j. Fan ◽  
V. Urbain ◽  
Y. Qian ◽  
J. Manem

A cross-flow membrane bioreactor (MBR) for raw municipal wastewater treatment, consisting of a suspended growth bioreactor and a ceramic membrane ultrafiltration unit, was run over a period of more than 300 days in a wastewater treatment plant (WWTP). Sludge Retention Times (SRT) of 20, 10 and 5 days, respectively, and Hydraulic Retention Times (HRT) of 15 and 7.5 hours were tested. Membrane fouling was found to be a function of SRT and permeate flux. Under an SRT of 20 days and flux of 71 l/m2\ · h at 30°C, the MBR was successfully run over 70 days without the need for chemical cleaning. However chemical cleaning had to be undertaken every 3–5 days at shorter sludge retention times (typically an SRT of five days and a flux of 143 l/m2\ · h at 30°C). In this study, fouling materials were removed efficiently through chemical cleaning, with an average permeablity recovery of 87±11%.


2018 ◽  
Vol 2017 (2) ◽  
pp. 481-491 ◽  
Author(s):  
Qirong Dong ◽  
Wayne Parker ◽  
Martha Dagnew

Abstract A transient study was conducted at pilot scale to assess the impact of Fe dosage on the dynamics of biological and membrane performance of an anaerobic membrane bioreactor (AnMBR) treating authentic municipal wastewater. A transient model of the AnMBR system was employed to assist with interpretation of the observed responses in the mixed liquor under different FeCl3 dosages. A high dosage (43 mg FeCl3/LSewage) resulted in a significant accumulation of fixed suspended solids and volatile suspended solids (VSS) and reduction of colloidal COD in the mixed liquor. The elevated dosages appeared to reduce the biodegradability of VSS that was present in the raw wastewater. Intermediate dosages of FeCl3 (21–12 mg/L) had less effect on these responses and did not appear to affect VSS biodegradation. Membrane performance was significantly affected by FeCl3 dosage as indicated by reversible resistance (RR) and physically irreversible resistance (IR). RR was closely related to the colloidal COD in the mixed liquor, thus responded quickly to Fe dosage. Physically, IR had a delayed response to changes in the colloidal COD concentrations in the mixed liquor and this was attributed to the effect of slow mass transfer of colloidal matter between the mixed liquor and the membrane.


2014 ◽  
Author(s):  
◽  
Mxolisi Norman Cele

Increased public concern over health and the environment, the need to expand existing wastewater treatment plants due to population increase, and increasingly stringent discharge requirements, have created a need for new innovative technologies that can generate high quality effluent at affordable cost for primary and secondary re-use. The membrane biological reactor (MBR) process is one of the innovative technologies that warrant consideration as a treatment alternative where high quality effluent and/or footprint limitations are a prime consideration. MBR processes have been applied for the treatment of industrial effluent for over ten years (Harrhoff, 1990). In this process, ultrafiltration or microfiltration membranes separate the treated water from the mixed liquor, replacing the secondary settling tanks of the conventional activated sludge process. Historically, energy costs associated with pumping the treated water through the membranes have limited widespread application for the treatment of high volumes of municipal wastewater. However, recent advancements and developments in membrane technology have led to reduced process energy costs and induced wider application for municipal wastewater treatment (Stephenson et al., 2000). This report describes a small and pilot scale demonstration study conducted to test a woven fabric microfiltration immersed membrane bioreactor (WFM-IMBR) process for use in domestic wastewater treatment. The study was conducted at Durban Metro Southern Wastewater Treatment Works, Veolia Plant, South Africa. The main objective of this project was to develop and evaluate the performance of an aerobic woven fabric microfiltration immersed membrane bioreactor (WFM-IMBR) for small scale domestic wastewater treatment. The experiments were oriented towards three sub objectives: to develop the membrane pack for immersed membrane bioreactor based on WF microfilters; to evaluate the hydrodynamics of WF membrane pack for bioreactor applications; and to evaluate the long-term performance and stability of WFM-IMBR in domestic waste water treatment. The literature was reviewed on membrane pack design for established commercial IMBR. The data collected from literature was then screened and used to design the WF membrane pack. Critical flux was used as the instrument to measure the WF membrane pack hydrodynamics. Long-term operation of the WFM-IMBR was in two folds: evaluating the performance and long term stability of WFM-IMBR. The membrane pack of 20 flat sheet rectangular modules (0.56 m by 0.355 m) was developed with the gap of 5 mm between the modules. The effects of parameters such as mixed liquor suspended solids or aeration on critical flux were examined. It was observed that the critical flux decreased with the increase of sludge concentration and it could be enhanced by improving the aeration intensity as expected and in agreement with the literature. Hence the operating point for long term subcritical operation was selected to be at a critical flux of 30 LMH and 7.5 L/min/module of aeration. Prior to the long term subcritical flux of WFM-IMBR, the operating point was chosen based on the hydrodynamic study of the WF membrane pack. The pilot scale WFM-IMBR demonstrated over a period of 30 days that it can operate for a prolonged period without a need for cleaning. Under subcritical operation, it was observed that there was no rise in TMP over the entire period of experimentation. Theoretically this was expected but it was never investigated before. Good permeate quality was achieved with 95% COD removal and 100% MLSS removal. The permeate turbidity was found to be less than 1 NTU and it decreased with an increase in time and eventually stabilized over a prolonged time. Woven fibre membranes have demonstrated great potential in wastewater treatment resulting in excellent COD and MLSS removal; low permeate turbidity and long term stability operation. From the literature surveyed, this is the first study which investigated the use of WF membranes in IMBRs. The study found that the small scale WFM-IMBR unit can be employed in fifty equivalence person and generate effluent that is free of suspended solids, having high levels of solid rejection and has acceptable discharge COD for recycle. Future work should be conducted on energy reduction strategies that can be implemented in WFM-IMBR for wastewater treatment since high energy requirements have been reported by commercial IMBRs.


Membranes ◽  
2021 ◽  
Vol 11 (6) ◽  
pp. 388
Author(s):  
Ihtisham Ul Haq Shami ◽  
Bing Wu

In this study, three gravity-driven membrane (GDM) reactors with flat sheet membrane modules and various biocarriers (synthetic fibers, lava stones, and sands) were operated for municipal wastewater treatment. The effects of water head, periodically cleaning protocol, and operation temperature on the GDM reactor performance were illustrated in terms of membrane performance and water quality. The results indicated that: (1) the cake layer fouling was predominant (>~85%), regardless of reactor configuration and operation conditions; (2) under lower water head, variable water head benefited in achieving higher permeate fluxes due to effective relaxation of the compacted cake layers; (3) the short-term chemical cleaning (30–60 min per 3–4 days) improved membrane performance, especially when additional physical shear force was implemented; (4) the lower temperature had negligible effect on the GDM reactors packed with Icelandic lava stones and sands. Furthermore, the wastewater treatment costs of the three GDM reactors were estimated, ranging between 0.31 and 0.37 EUR/m3, which was greatly lower than that of conventional membrane bioreactors under lower population scenarios. This sheds light on the technical and economic feasibility of biocarrier-facilitated GDM systems for decentralized wastewater treatment in Iceland.


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