THE IMPACT OF OVERBALANCED DRILLING FROM EXPLORATION/APPRAISAL WELLS TO FIELD DEVELOPMENT PLAN

2021 ◽  
Author(s):  
Mohammadhossein Mohammadlou ◽  
◽  
Matthew Guy Reppert ◽  
Roxane Del Negro ◽  
George Jones ◽  
...  

During well planning, drillers and petrophysicists have different principle objectives. The petrophysicist’s aim is to acquire critical well data, but this can lead to increased operational risk. The driller is focused on optimizing the well design, which can result in compromised data quality. In extreme cases, the impact of well design on petrophysical data can lead to erroneous post-well results that impact the entire value-chain assessment and decision making toward field development. In this paper, we present a case study from a syn-rift, Upper Jurassic reservoir in the Norwegian Sea where well design significantly impacted reservoir characterization. Three wells (exploration, appraisal, and geopilot) are compared in order to demonstrate the impact of overbalanced drilling on well data from both logs and core. Implications for reservoir quality assessment, volume estimates, and the errors introduced into both a static geomodel and dynamic reservoir simulation are discussed. This case study highlights the importance of optimizing well design for petrophysical data collection and demonstrates the potential for value creation. Extensive data collection was initially carried out in both exploration and appraisal wells, including full sets of logging while drilling (LWD), wireline logging, fluid sampling, and extensive coring. Both wells were drilled with considerable overbalanced mud weights due to the risk of overpressured reservoirs in the region. The log data was subsequently corrected for significant mud-filtration invasion, with calibration to core measurements guiding the interpretation. Geological and reservoir models were built based on results from the two wells, and development wells were planned accordingly. A thorough investigation of core material raised suspicion that there could also be a significant adverse effect of core properties resulting from overbalanced drilling. The implications were so significant for the reservoir volume that a strategic decision was made to drill a geopilot well close to the initial exploration well, prior to field development drilling. The well was drilled six years after the initial exploration phase with considerably lower overbalance. Extensive well data, including one core, were acquired. The recovered core was crucial in order to compare the reservoir properties for comparable facies between all three wells. The results from the core demonstrate distinctly different rock quality characteristics, especially at the high end of the reservoir quality spectrum. Results of the core study confirmed the initial hypothesis that overbalanced drilling had significantly impacted the properties of the core as well as the well logs. The study concluded that the updated reservoir model properties would significantly increase the in-place volumes compared to the pre-geopilot estimate. This study shows how well design adversely affected petrophysical measurements and how errors in these data compromised geological and reservoir models, leading to a suboptimal field development plan that eroded significant value. This example provides a case study that can be used to improve the well design so that petrophysicists and drillers can both be part of the same value creation result. Future work will include further laboratory investigations on the effects of high overbalanced drilling on core and possible “root causes” for compromised core integrity.

Author(s):  
Mohammadhossein Mohammadlou ◽  
◽  
Matthew Guy Reppert ◽  
Roxane Del Negro ◽  
George Jones ◽  
...  

During well planning, drillers and petrophysicists have different principle objectives. The petrophysicist’s aim is to acquire critical well data, but this can lead to increased operational risk. The driller is focused on optimizing the well design, which can result in compromised data quality. In extreme cases, the impact of well design on petrophysical data can lead to erroneous post-well results that impact the entire value-chain assessment and decision making toward field development. This paper presents a case study from an Upper Jurassic reservoir in the Norwegian Sea where well design significantly impacted reservoir characterization. Three wells (exploration, appraisal, and geopilot) are compared to demonstrate the impact of overbalanced drilling on both log and core data. Implications for reservoir quality assessment and volume estimates are discussed. Extensive data collection was initially carried out in both exploration and appraisal wells, including full sets of logging while drilling (LWD), wireline logging, fluid sampling, and extensive coring. Both wells were drilled with considerable overbalanced mud weights due to the risk of overpressured reservoirs in the region. The log data were subsequently corrected for significant mud-filtration and fines invasion, with calibration to core measurements guiding the interpretation. A thorough investigation of core material raised suspicion that there could also be significant adverse effects on core properties resulting from overbalanced drilling. The implications were so significant for the reservoir volume that a strategic decision was made to drill a geopilot well close to the initial exploration well prior to field development drilling. The well was drilled 6 years after the initial exploration phase with considerably lower overbalance. Extensive well data, including one core, were acquired. The recovered core was crucial in order to compare the reservoir properties for comparable facies between all three wells. The results from the core demonstrate distinctly different rock quality characteristics, especially at the high end of the reservoir quality spectrum. Results of the core study confirmed the initial hypothesis that overbalanced drilling had significantly impacted the properties of the core and well logs. This study shows how well design adversely affected petrophysical measurements and how errors in these data compromised geological and reservoir models, leading to a suboptimal field development plan that eroded significant value. This example provides a case study that can be used to improve well designs so that petrophysicists and drillers can both be part of the same value creation result.


2016 ◽  
Vol 19 (03) ◽  
pp. 391-402
Author(s):  
Sunday Amoyedo ◽  
Emmanuel Ekut ◽  
Rasaki Salami ◽  
Liliana Goncalves-Ferreira ◽  
Pascal Desegaulx

Summary This paper presents case studies focused on the interpretation and integration of seismic reservoir monitoring from several fields in conventional offshore and deepwater Niger Delta. The fields are characterized by different geological settings and development-maturity stages. We show different applications varying from qualitative to quantitative use of time-lapse (4D) seismic information. In the first case study, which is in shallow water, the field has specific reservoir-development challenges, simple geology, and is in phased development. On this field, 4D seismic, which was acquired several years ago, is characterized by poor seismic repeatability. Nevertheless, we show that because of improvements from seismic reprocessing, 4D seismic makes qualitative contributions to the ongoing field development. In the second case study, the field is characterized by complex geological settings. The 4D seismic is affected by overburden with strong lateral variations in velocity and steeply dipping structure (up to 40°). Prestack-depth-imaging (PSDM) 4D seismic is used in a more-qualitative manner to monitor gas injection, validate the geologic/reservoir models, optimize infill injector placement, and consequently, enhance field-development economics. The third case study presents a deep offshore field characterized by a complex depositional system for some reservoirs. In this example, good 4D-seismic repeatability (sum of source- and receiver-placement differences between surveys, dS+dR) is achieved, leading to an increased quantitative use of 4D monitoring for the assessment of sand/sand communication, mapping of oil/water (OWC) front, pressure evolution, and dynamic calibration of petro-elastic model (PEM), and also as a seismic-based production-logging tool. In addition, 4D seismic is used to update seismic interpretation, provide a better understanding of internal architecture of the reservoirs units, and, thereby, yield a more-robust reservoir model. The 4D seismic in this field is a key tool for field-development optimization and reservoir management. The last case study illustrates the need for seismic-feasibility studies to detect 4D responses related to production. In addition to assessing the impact of the field environment on the 4D- seismic signal, these studies also help in choosing the optimum seismic-survey type, design, and acquisition parameters. These studies would possibly lead to the adoption of new technologies such as broad-band streamer or nodes acquisition in the near future.


2020 ◽  
Author(s):  
Okiemute Amuboh ◽  
Suleiman Ahmed ◽  
Dolapo Enya ◽  
Gbolade Ibikunle ◽  
Imonite Imorame ◽  
...  

2013 ◽  
Vol 3 (6) ◽  
pp. 1-11
Author(s):  
Amalia E. Maulana ◽  
Pandu Jati Kuncoro ◽  
Lexi Z. Hikmah

Subject area Reverse positioning, market segmentation, customer-centric organization. Study level/applicability Postgraduate program; Master in strategic marketing and Master in business administration. Case overview Declining radio listenership is triggered by lack of attention of the radio managers to the desires of radio listeners. Delta FM radio, as part of Masima Media Group, is a radio that realized the need for revitalization. They changed their target audience and positioning to regain its former glory. Delta FM radio get back to the core benefit with the tagline: “100% Great Songs”. Shifting from highlighting the emotional benefits to functional benefits and to cut a variety of benefits is called “reverse positioning”. Expected learning outcomes The objective of this case study is to give deeper comprehension a new concept called reverse positioning or reverse branding. It is an example of the dynamic of hyper competition in media market in practice, in the emerging market such as Indonesia. It provides clear picture of the difference between listener oriented vs advertiser oriented company and the impact of the imbalance portion between them. Supplementary materials Teaching notes are available for educators only. Please contact your library to gain login details or email [email protected] to request teaching notes.


2019 ◽  
Vol 31 (2) ◽  
pp. 203-220 ◽  
Author(s):  
Martin Kunc ◽  
David Menival ◽  
Steve Charters

PurposeThe traditional view of the process of value creation suggests that it occurs inside the firm through its activities or resources. However, there are special cases where firms create value using external shared resources, e.g. a territorial brand. The purpose of this study is to demonstrate how the combination of both internal and external resources co-create value in wine regions.Design/methodology/approachAn in-depth case study of nine firms covering different co-creation processes in Champagne, France. The selection of interviews was designed to cover the diversity of firms within the area with different market positioning. Most firms in the region have been selling champagne for more than 50 years, so they have established long-standing relationships with their markets.FindingsWhile there is only one value, Champagne, firms create many different values based on owners’ perceptions with diverse effects on the process of value co-creation in the territorial brand. Some firms have strategies which could deteriorate the value of shared resource. This threat needs institutional changes with unknown consequences on the territorial brand.Research limitations/implicationsThe research only involved one case study with a highly developed territorial brand system. There are multiple wine regions that have considered managing either implicitly or explicitly their shared strategic resources (e.g. a territorial brand). Consequently, the findings may not be applicable to all wine regions but it can provide a “gold standard” for regions and wineries that do not realize the impact that their value creation actions can have on the wine region.Practical implicationsCollective management of shared strategic resources, such as a territorial brand, can be a powerful action to sustain competitive advantage rather than individual actions to develop individual brands. However, it can work only with an institutional organization managing the collective process.Originality/valueThe paper offers lessons from a comprehensive and well-known case study where resource bundles co-create value with a territorial brand.


2021 ◽  
Author(s):  
Yuan Liu ◽  
Bin Li ◽  
Hongjie Zhang ◽  
Fan Yang ◽  
Guan Wang ◽  
...  

Abstract The economics of tight gas fields highly depend on the consistency between expected production and the actual well performance. A mismatch between the reservoir quality and the well production often leads to a review of the individual well. However, such mismatch may vary from case to case, and it is hard to perform a field-level analysis based on individual well reviews. We introduce a new method based on data mining to assist the field-level diagnosis. LX gas field is located the in eastern Ordos basin. Compared to the main gas field in the center of the basin, LX field is less predictable in well performance. This predictability issue hinders field development in LX field because the field economics are substantially jeopardized by the inconsistency between the reservoir quality and the production performance. The traditional workflow to understand this issue at the field level is to review the details of a large number of individual wells in the area. This is typically an intense task, and too much detail from multiple disciplines may hide the true pattern of the field behavior. To resolve this issue, we applied data mining in our field development diagnosis workflow. Our new workflow in LX area started with the existing field datasheet, including logging summaries, completion treatment reports, and flowback testing datasheets. With the data extracted from these different sources, we visualized the consolidated information in various plots and graphs based on regression analysis, which revealed the relation between flowback ratio and the production, the flowback rate consistency from the different service suppliers, and the impact of water productions. The data mining approach helped to generate new understandings in LX gas field. With the in-depth analysis of the flowback data together with reservoir properties and operation parameters, the key problems in the field were identified for further development optimization, and the field economics can be significantly improved. The diagnosis method can be easily adapted and applied to any field with similar problems, and data mining can be useful for almost all large-scale field development optimizations.


2018 ◽  
Vol 14 (1) ◽  
pp. 74-85
Author(s):  
Wiktoria Wojtyra

Summary This article considers the impact of counterfactual strategies on the most recent Polish theatrical practices dealing with biographies of “historical” figures. The re-occurrence of these past agents on the stage will be viewed in light of the biographical turn in the humanities as well as from the perspective of Jacques Derrida’s concept of hauntology. Seemingly, both trends share a need to create an alternative space for the expression of a contemporary self which is marked by disunity and disintegration. Subjects of current semi-biographical projects are those whose voices have once been neglected, marginalised, or oppressed because of their gender, social background, or political views. This account examines the ways in which counterfactual strategies enable us to grasp the polyphonic condition of a modern subject and to see, in traces left by different Other(s), touchstones for social and political change. By taking the play Tu Wersalu nie będzie! (No Versailles over here!) by Rabih Mroué as the core case study of the analysis, I aim to demonstrate how counterfactual strategies animate emancipatory potential ascribed to the arrival of the phantom of controversial Polish politician Andrzej Lepper. His death in unknown circumstances becomes a point of divergence in which Lepper’s existence layers into counterfactual scenarios. Counterfactual strategies enable many approaches to view Lepper’s figure without the ethically dubious act of speaking in his name. By unsettling claims of truth, counterfactual strategies unravel how “facts” about Lepper resurfaced in mass media, thereby constructing his stereotyped and over-generalised image. The play has a form of investigation which, by employment of counterfactualism, reenacts the oppression of a mainstream media discourse against the disturbing Other epitomised by Lepper.


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