Optimization of performance and operational cost for a dual mode diesel-natural gas RCCI and diesel combustion engine

2018 ◽  
Vol 231 ◽  
pp. 549-561 ◽  
Author(s):  
Ehsan Ansari ◽  
Mahdi Shahbakhti ◽  
Jeffrey Naber
Author(s):  
A. P. Shaikin ◽  
I. R. Galiev

The article analyzes the influence of chemical composition of hythane (a mixture of natural gas with hydrogen) on pressure in an engine combustion chamber. A review of the literature has showed the relevance of using hythane in transport energy industry, and also revealed a number of scientific papers devoted to studying the effect of hythane on environmental and traction-dynamic characteristics of the engine. We have studied a single-cylinder spark-ignited internal combustion engine. In the experiments, the varying factors are: engine speed (600 and 900 min-1), excess air ratio and hydrogen concentration in natural gas which are 29, 47 and 58% (volume).The article shows that at idling engine speed maximum pressure in combustion chamber depends on excess air ratio and proportion hydrogen in the air-fuel mixture – the poorer air-fuel mixture and greater addition of hydrogen is, the more intense pressure increases. The positive effect of hydrogen on pressure is explained by the fact that addition of hydrogen contributes to increase in heat of combustion fuel and rate propagation of the flame. As a result, during combustion, more heat is released, and the fuel itself burns in a smaller volume. Thus, the addition of hydrogen can ensure stable combustion of a lean air-fuel mixture without loss of engine power. Moreover, the article shows that, despite the change in engine speed, addition of hydrogen, excess air ratio, type of fuel (natural gas and gasoline), there is a power-law dependence of the maximum pressure in engine cylinder on combustion chamber volume. Processing and analysis of the results of the foreign and domestic researchers have showed that patterns we discovered are applicable to engines of different designs, operating at different speeds and using different hydrocarbon fuels. The results research presented allow us to reduce the time and material costs when creating new power plants using hythane and meeting modern requirements for power, economy and toxicity.


Author(s):  
J Harrod ◽  
P J Mago

Due to the soaring costs and demand of energy in recent years, combined cooling, heating, and power (CCHP) systems have arisen as an alternative to conventional power generation based on their potential to provide reductions in cost, primary energy consumption, and emissions. However, the application of these systems is commonly limited to internal combustion engine prime movers that use natural gas as the primary fuel source. Investigation of more efficient prime movers and renewable fuel applications is an integral part of improving CCHP technology. Therefore, the objective of this study is to analyse the performance of a CCHP system driven by a biomass fired Stirling engine. The study is carried out by considering an hour-by-hour CCHP simulation for a small office building located in Atlanta, Georgia. The hourly thermal and electrical demands for the building were obtained using the EnergyPlus software. Results for burning waste wood chip biomass are compared to results obtained burning natural gas to illustrate the effects of fuel choice and prime mover power output on the overall CCHP system performance. Based on the specified utility rates and including excess production buyback, the results suggest that fuel prices of less than $23/MWh must be maintained for savings in cost compared to the conventional case. In addition, the performance of the CCHP system using the Stirling engine is compared with the conventional system performance. This comparison is based on operational cost and primary energy consumption. When electricity can be sold back to the grid, results indicate that a wood chip fired system yields a potential cost savings of up to 50 per cent and a 20 per cent increase in primary energy consumption as compared with the conventional system. On the other hand, a natural gas fired system is shown to be ineffective for cost and primary energy consumption savings with increases of up to 85 per cent and 24 per cent compared to the conventional case, respectively. The variations in the operational cost and primary energy consumption are also shown to be sensitive to the electricity excess production and buyback rate.


2014 ◽  
Author(s):  
Martina Janovcová ◽  
Jozef Jandačka ◽  
Roman Kiš

2015 ◽  
Vol 23 (1) ◽  
pp. 18-24
Author(s):  
Andrej Chríbik ◽  
Marián Polóni ◽  
Ján Lach ◽  
Ľubomír Jančošek ◽  
Peter Kunc ◽  
...  

Abstract The article discusses the application of synthesis gas from pyrolysis of plastics in petrol engine. The appropriate experimental measurements were performed on a combustion engine LGW 702 designated for micro-cogeneration unit. The power parameters, economic and internal parameters of the engine were compared to the engine running on the reference fuel - natural gas and synthesis gas. Burning synthesis gas leads to decreased performance by about 5% and to increased mass hourly consumption by 120%. In terms of burning, synthesis gas has similar properties as natural gas. More significant changes are observed in even burning of fuel in consecutive cycles.


2021 ◽  
Vol 315 ◽  
pp. 03011
Author(s):  
Georgiy Dubov ◽  
Alexander Bogomolov ◽  
Sergey Azikhanov ◽  
Pavel Strelnikov ◽  
Sergey Nokhrin

The issue of a comparative study of fuel consumption and temperature characteristics of gas-diesel BelAZ 75131 mining dump trucks equipped with an on-board cryogenic fuel system and hauling rock mass at the Kuzbass open-pit coal mine is considered in the article. A brief analysis of the efficiency of using liquefied natural gas (LNG) - methane - as a motor fuel for mining dump trucks is carried out. It is noted that the use of LNG fuel for heavy-duty dump trucks is one of the most promising ways to improve the environmental and economic performance during the operation of this type of mining equipment. The technique and instrumental base for conducting research are presented. The relationship between natural ratios of diesel fuel replacement with natural gas and the energy charge of these replacement is studied. The following data are presented: data on the consumption of vaporous (gaseous superheated) natural gas (hereinafter gaseous natural gas) during field operation of gas-diesel BelAZ 75131 mining dump trucks; flow rate of gaseous natural gas in pipelines; consumption of antifreeze at the inlet to the liquefied natural gas evaporator, as well as antifreeze temperature at the inlet and outlet of the evaporator; temperature of gaseous natural gas at the outlet of the reducer after the evaporator; data on the comparison of temperature profiles in the cylinders of CUMMINS KTA 50 internal combustion engine under diesel and gas-diesel operation.


Author(s):  
Derek Johnson ◽  
Marc Besch ◽  
Nathaniel Fowler ◽  
Robert Heltzel ◽  
April Covington

Emissions compliance is a driving factor for internal combustion engine research pertaining to both new and old technologies. New standards and compliance requirements for off-road spark ignited engines are currently under review and include greenhouse gases. To continue operation of legacy natural gas engines, research is required to increase or maintain engine efficiency, while reducing emissions of carbon monoxide, oxides of nitrogen, and volatile organic compounds such as formaldehyde. A variety of technologies can be found on legacy, large-bore natural gas engines that allow them to meet current emissions standards — these include exhaust after-treatment, advanced ignition technologies, and fuel delivery methods. The natural gas industry uses a variety of spark plugs and tuning methods to improve engine performance or decrease emissions of existing engines. The focus of this study was to examine the effects of various spark plug configurations along with spark timing to examine any potential benefits. Spark plugs with varied electrode diameter, number of ground electrodes, and heat ranges were evaluated against efficiency and exhaust emissions. Combustion analyses were also conducted to examine peak firing pressure, location of peak firing pressure, and indicated mean effective pressure. The test platform was an AJAX-E42 engine. The engine has a bore and stroke of 0.216 × 0.254 meters (m), respectively. The engine displacement was 9.29 liters (L) with a compression ratio of 6:1. The engine was modified to include electronic spark plug timing capabilities along with a mass flow controller to ensure accurate fuel delivery. Each spark plug configuration was examined at ignition timings of 17, 14, 11, 8, and 5 crank angle degrees before top dead center. The various configurations were examined to identify optimal conditions for each plug comparing trade-offs among brake specific fuel consumption, oxides of nitrogen, methane, formaldehyde, and combustion stability.


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