Modernization and structural evaluation of the improved Overhead Cable System
A modernized Overhead Cable System prototype for a 689 ft (210 m) Improved Ribbon Bridge crossing was designed, assembled, and structurally tested. Two independent structural tests were executed, i.e., a component-level compression test of the BSS tower was performed to determine its load capacity and failure mode; and a system-level ‘dry’ test of the improved OCS prototype was conducted to determine the limit state and failure mode of the entire OCS. In the component-level compression test of the BSS tower, the compressive capacity was determined to be 102 kips, and the failure mode was localized buckling in the legs of the tower section. During system-level testing, the prototype performed well up to 40.5 kips of simulated drag load, which corresponds to a uniformly distributed current velocity of 10.7 ft/s. If a more realistic, less conservative parabolic velocity distribution is assumed instead, the drag load for an 11 ft/s current is 21.1 kips. Under this assumption, the improved OCS prototype has a factor of safety of 1.9, based on a 689-ft crossing and 11-ft/s current. The OCS failed when one of the tower guy wires pulled out of the ground, causing the tower to overturn.