Retrofitting and Operation of Small Extended Aeration Plants for Advanced Treatment – Some Experiences in Japan

1993 ◽  
Vol 28 (10) ◽  
pp. 377-385 ◽  
Author(s):  
K. Moriyama ◽  
M. Takahashi ◽  
Y. Harada

Some experiences concerning a retrofit design and operation for nutrients removal in small extended aeration plants are presented. In this study a new biological phosphorus removal process as well as a biological nitrogen removal process based on a sequential oxic-anoxic-oxic process is investigated. The denitrification in the first oxic zone has a high removing effect for nitrogen, and the oxidation reduction potential (ORP) value and dissolved oxygen (DO) concentration are useful indexes to maintain the optimum conditions of the first oxic zone for simultaneous denitrification. It is verified that the simultaneous denitrification can alleviate the alkalinity deficit problem against full nitrification by a stoichiometric analysis of alkalinity throughout the entire process. Additionally, a biological phosphorus removal process which uses a sludge blanket zone of secondary settling tank for phosphorus release is proposed.

2013 ◽  
Vol 69 (8) ◽  
pp. 1612-1619 ◽  
Author(s):  
Paraschos Melidis ◽  
Anastasios G. Kapagiannidis ◽  
Spyridon Ntougias ◽  
Konstantina Davididou ◽  
Alexander Aivasidis

A novel enhanced biological phosphorus removal (EBPR) system, which combined the intermittent feeding design with an anaerobic selector, was examined using on-line oxidation reduction potential (ORP), nitrate and ammonium probes. Two experimental periods were investigated: the aerobic and anoxic phases were set at 40 and 20 minutes respectively for period I, and set at 30 and 30 minutes for period II. Chemical oxygen demand (COD), biochemical oxygen demand (BOD5) and P removal were measured as high as 87%, 96% and 93% respectively, while total Kjeldahl nitrogen (TKN) and NH4+ removal averaged 85% and 91%. Two specific denitrification rates (SDNRs), which corresponded to the consumption of the readily biodegradable and slowly biodegradable COD, were determined. SDNR-1 and SDNR-2 during period I were 0.235 and 0.059 g N g−1 volatile suspended solids (VSS) d−1 respectively, while the respective rates during period II were 0.105 and 0.042 g N g−1 VSS d−1. The specific nitrate formation and ammonium oxidizing rates were 0.076 and 0.064 g N g−1 VSS d−1 for period I and 0.065 and 0.081 g N g−1 VSS d−1 for period II respectively. The specific P release rates were 2.79 and 4.02 mg P g−1 VSS h−1 during period I and II, while the respective anoxic/aerobic uptake rates were 0.42 and 0.55 mg P g−1 VSS h−1. This is the first report on an EBPR scheme using the intermittent feeding strategy.


1995 ◽  
Vol 22 (2) ◽  
pp. 260-269 ◽  
Author(s):  
D. G. Wareham ◽  
K. J. Hall ◽  
D. S. Mavinic

This research discusses two strategies for adding acetate to sequencing batch reactors operating as biological removal (Bio-P) systems. The control (fixed-time) reactor adds the acetate at a set time of 1 h 25 min, which is an assumed time for complete denitrification. The experimental (real-time) reactor adds the acetate when a computer detects the disappearance of nitrates, as indicated by a distinctive "breakpoint" or "kink" in the oxidation-reduction potential versus time profile. This control strategy is therefore based upon a known time for complete denitrification. The time-of-occurrence of the nitrate breakpoint is utilized in the development of a screening protocol for interpreting the behaviour (in terms of nitrate reactions) for reactors operating in biological phosphorus removal mode. The protocol involves categorizing the timing of the nitrate breakpoint into two groupings. A "failure" category corresponds to acetate being added prior to the breakpoint, because, in these cases, the acetate is used partially for denitrification and partially for Bio-P carbon storage. A "success" category corresponds to breakpoints occurring prior to the addition of acetate. In such cases, acetate is used solely for carbon storage by Bio-P organisms. Key words: oxidation-reduction potential, biological phosphorus removal, sequencing batch reactor, real-time computer control.


1992 ◽  
Vol 25 (12) ◽  
pp. 165-174 ◽  
Author(s):  
R. Franci Gonçalves ◽  
F. Rogalla

Possible procedures to achieve biological phosphorus removal in a fixed film reactor are discussed and the feasibility of phosphorus removal process in a fixed film reactor under continous flow is demonstrated. The behaviour of an upflow aerated filter operating under continuous feed and alternate aerobic/anaerobic conditions is analyzed. The influence of the duration of anaerobic and aerobic contact periods and of organic substrate loadings on the phosphorus removal process is verified. During the anaerobic state, the longer the duration, or the higher the substrate load, the better the phosphorus release and consequently the higher the uptake in the aerobic phase. The excess of accumulated phosphorus in the aerobic phase over released phosphorus in the anaerobic phase approaches 33 %. For each mg of phosphorus released, 5 mg filtered COD are consumed. Continuous phosphorus removal on two biofilters in series was performed by alternating aeration conditions, always introducing the influent to the anaerobic reactor.The tests carried out on laboratory scale showed that this system carrys out complete nitrification and removal of 80% of the phosphorus with a maximum hydraulic retention time of 5 hours. The hydraulic retention time and the residence time of the biomass in the reactor are independent and, therefore, the time the bacteria are exposed to alternate A/O conditions can be optimized. The very low concentrations of suspended solids in the effluent of the biofilter enable residual levels below 1 mg PO4-P/l to be obtained. Further investigations are carried out on full scale and to introduce denitrification in the same reactor.


2018 ◽  
Vol 78 (10) ◽  
pp. 2119-2130 ◽  
Author(s):  
Erika Varga ◽  
Hélène Hauduc ◽  
James Barnard ◽  
Patrick Dunlap ◽  
Jose Jimenez ◽  
...  

Abstract This paper summarizes recent developments in biological phosphorus removal modelling, with special attention to side-stream enhanced biological phosphorus removal (S2EBPR) systems on which previous models proved to be ineffective without case-by-case parameter adjustments. Through the research and experience of experts and practitioners, a new bio-kinetic model was developed including an additional group of biomass (glycogen accumulating organisms – GAOs) and new processes (such as aerobic and anoxic maintenance for PAO and GAO; enhanced denitrification processes; fermentation by PAOs which – along with PAO selection – is driven by oxidation-reduction potential (ORP)). This model successfully described various conditions in laboratory measurements and full plant data. The calibration data set is provided by Clean Water Services from Rock Creek Facility (Hillsboro, OR) including two parallel trains: conventional A2O and Westbank configurations, allowing the model to be verified on conventional and side-stream EBPR systems as well.


1985 ◽  
Vol 17 (11-12) ◽  
pp. 297-298 ◽  
Author(s):  
Takao Murakami ◽  
Atsushi Miyairi ◽  
Kazuhiro Tanaka

In Japan various biological phosphorus removal processes have recently been researched by laboratory or pilot plant scale studies and most of them have shown good results. Based on these results, the Japan Sewage Works Agency has conducted a full scale study of the biological phosphorus removal process from June 1982 until February 1983, which was the first full scale operation of this process in Japan. The main purpose of the study was to evaluate phosphorus removal efficiency and also nitrogen removal efficiency of the process and in addition, to ascertain the important operating factors of the process. For the study a treatment train of a large scale sewage treatment plant was remodelled. The aeration tank of 3.825 m3 volume was divided into four equal cells. The whole train including return sludge line was operated entirely independently of the other trains. During the experiment the train was operated under two different modes, Mode 1 and Mode 2. In Mode 1, the train was operated as an A/O process, the first cell of the aeration tank being anaerobic and the other cells oxic. In Mode 2, the train was operated as a Modified Phoredox process. In this case, the first cell was anaerobic, but the second cell was anoxic and nitrified liquor was returned to it from the end of the oxic cells. Mode 1 and Mode 2 were further divided into many ‘runs' and the flow rate varied between 12,550 m3 d−1 and 25,270 m3 d−1 , corresponding to retention times of 7.3 hours and 3.6 hours, respectively. Throughout the experimental period the mean value of influent (primary effluent) total-P concentration was 3.38 mg 1−1 , and that of the final effluent was 0.47 mg 1−1 . A cumulated frequency curve of the data showed that about 93% of measured effluent total-P was below 1.0 mg l−1 . Therefore, it can be concluded that with these influent total-P levels, biological phosphorus removal processes can sufficiently satisfy the effluent standard of 1 mg 1−1 total-P. Even when the process was operated as a Modified Phoredox Process, no obstruction to phosphorus removal because of nitrification was observed and phosphorus removal remained good. However, since the sewage treatment plant treated influent from a combined sewerage system, phosphorus removal was sometimes affected by heavy rainfalls. In such cases phosphorus release in the anaerobic cell was insufficient because of increased influent NOx concentration and accordingly increased denitrification level in the anaerobic cell. Therefore, as a result, enhanced phosphorus uptake in the following cells could not be observed. Higher process stability can be expected if an effective countermeasure to high influent NOx concentration can be made. Influence of flow rate fluctuation on the process was also studied. The treatment train was operated for a week under a daily flow rate fluctuation pattern which ranged between 460 m3 hr−1 and 820 m3 hr−1 . Nevertheless, the effluent total-P concentration showed no increase and stayed constantly lower than 0.5 mg 1−1. The oxidation reduction potential (ORP) was an effective control index to evaluate the degree of phosphorus release in the anaerobic cell. Water temperature did not affect phosphorus release and uptake rates.


2018 ◽  
Vol 2018 (5) ◽  
pp. 223-239
Author(s):  
Nicholas B Tooker ◽  
Guangyu Li ◽  
Varun Srinivasan ◽  
James L Barnard ◽  
Charles Bott ◽  
...  

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