Full Scale Study of Biological Phosphorus Removal Processes

1985 ◽  
Vol 17 (11-12) ◽  
pp. 297-298 ◽  
Author(s):  
Takao Murakami ◽  
Atsushi Miyairi ◽  
Kazuhiro Tanaka

In Japan various biological phosphorus removal processes have recently been researched by laboratory or pilot plant scale studies and most of them have shown good results. Based on these results, the Japan Sewage Works Agency has conducted a full scale study of the biological phosphorus removal process from June 1982 until February 1983, which was the first full scale operation of this process in Japan. The main purpose of the study was to evaluate phosphorus removal efficiency and also nitrogen removal efficiency of the process and in addition, to ascertain the important operating factors of the process. For the study a treatment train of a large scale sewage treatment plant was remodelled. The aeration tank of 3.825 m3 volume was divided into four equal cells. The whole train including return sludge line was operated entirely independently of the other trains. During the experiment the train was operated under two different modes, Mode 1 and Mode 2. In Mode 1, the train was operated as an A/O process, the first cell of the aeration tank being anaerobic and the other cells oxic. In Mode 2, the train was operated as a Modified Phoredox process. In this case, the first cell was anaerobic, but the second cell was anoxic and nitrified liquor was returned to it from the end of the oxic cells. Mode 1 and Mode 2 were further divided into many ‘runs' and the flow rate varied between 12,550 m3 d−1 and 25,270 m3 d−1 , corresponding to retention times of 7.3 hours and 3.6 hours, respectively. Throughout the experimental period the mean value of influent (primary effluent) total-P concentration was 3.38 mg 1−1 , and that of the final effluent was 0.47 mg 1−1 . A cumulated frequency curve of the data showed that about 93% of measured effluent total-P was below 1.0 mg l−1 . Therefore, it can be concluded that with these influent total-P levels, biological phosphorus removal processes can sufficiently satisfy the effluent standard of 1 mg 1−1 total-P. Even when the process was operated as a Modified Phoredox Process, no obstruction to phosphorus removal because of nitrification was observed and phosphorus removal remained good. However, since the sewage treatment plant treated influent from a combined sewerage system, phosphorus removal was sometimes affected by heavy rainfalls. In such cases phosphorus release in the anaerobic cell was insufficient because of increased influent NOx concentration and accordingly increased denitrification level in the anaerobic cell. Therefore, as a result, enhanced phosphorus uptake in the following cells could not be observed. Higher process stability can be expected if an effective countermeasure to high influent NOx concentration can be made. Influence of flow rate fluctuation on the process was also studied. The treatment train was operated for a week under a daily flow rate fluctuation pattern which ranged between 460 m3 hr−1 and 820 m3 hr−1 . Nevertheless, the effluent total-P concentration showed no increase and stayed constantly lower than 0.5 mg 1−1. The oxidation reduction potential (ORP) was an effective control index to evaluate the degree of phosphorus release in the anaerobic cell. Water temperature did not affect phosphorus release and uptake rates.

1993 ◽  
Vol 27 (5-6) ◽  
pp. 241-252 ◽  
Author(s):  
T. Kuba ◽  
G. Smolders ◽  
M. C. M. van Loosdrecht ◽  
J. J. Heijnen

In this study an anaerobic-anoxic SBR (sequencing batch reactor) was used in order to investigate the possibility of phosphorus removal utilizing nitrate as an electron acceptor, instead of oxygen in biological phosphorus removal processes. The reactor was supplied with synthetic wastewater, in which acetic acid (HAc) and phosphate were added at concentrations of 400 mg-COD/l and 15 mg-P/l. A conventional anaerobic-aerobic SBR was also operated to compare with the anaerobic-anoxic SBR. The objectives of this research are to examine (i) feasibility and stability of the systems, (ii) kinetics and stoichiometry of phosphorus release and uptake. The anaerobic-anoxic SBR operation resulted in a stable phosphorus removal and accumulation of phosphorus removing bacteria using nitrate as an electron acceptor. Immediately after inoculation from a phosphorus removing plant (Renpho system) phosphorus uptake was observed, indicating that phosphorus removing bacteria which are able to utilize nitrate were already present in conventional phosphorus removing sludge. Comparison of stoichiometry and kinetics with the conventional anaerobic-aerobic SBR system shows a similar potential for phosphorus removal by denitrifying organisms. Therefore in the design of phosphorus removal processes one should not be afraid of nitrate, but use it.


1990 ◽  
Vol 22 (7-8) ◽  
pp. 35-43
Author(s):  
K. D. Tracy ◽  
S. N. Hong

The anaerobic selector of the A/0™ process offers many advantages over conventional activated sludge processes with respect to process performance and operational stability. This high-rate, single-sludge process has been successfully demonstrated in full-scale operations for biological phosphorus removal and total nitrogen control in addition to BOD and TSS removal. This process can be easily utilized in upgrading existing treatment plants to meet stringent discharge limitations and to provide capacity expansion. Upgrades of two full-scale installations are described and performance data from the two facilities are presented.


1994 ◽  
Vol 29 (7) ◽  
pp. 153-156 ◽  
Author(s):  
D. Wedi ◽  
P. A. Wilderer

Most of the fundamental processes responsible for enhanced biological phosphorus removal (EBPR) were obtained through laboratory tests under defined conditions with pure or enriched cultures. Acinetobacter sp. was identified as the most important group of bacteria responsible for bio-P removal. Full scale data showed, however, that laboratory results do not match full scale results well enough. There is a lack of data on the effects of sub-optimal process conditions such as inadequate availability of volatile fatty acids (VFA), high nitrate recycle, storm water inflow or low temperatures. In this paper the results of full scale experiments on P-release are presented and compared with theoretical values. Measurements at a full scale Phoredox-system showed a surprisingly low P-release in the anaerobic reactor. Only 4 to 10% of the phosphorus in the activated sludge was released in the bulk liquid. With laboratory batch-tests, a maximum of 20% of the P in the sludge could be released. It is assumed that under the prevailing process conditions either the fraction of Acinetobacter sp. was very small, or bacteria other than Acinetobacter sp. were responsible for the P-removal, or most of the phosphorus was bound chemically but mediated by biological processes.


2000 ◽  
Vol 41 (4-5) ◽  
pp. 503-508 ◽  
Author(s):  
R.F. Gonçalves ◽  
F. Rogalla

This work describes laboratory scale research about Enhanced Biological Phosphorus Removal (EBPR) in a submerged biofilter under Anaerobic/Oxic (A/O) alternation and continuous feed. Its main purpose is to detail the behaviour of the reactor throughout the anaerobic and the aerobic phases of the A/O cycle, to study the importance of the anaerobic phase in the selection of the EBPR bacteria in the biofilm and to evaluate the consumption and the importance of the organic substrate during the anaerobic phase. The mass balance over the Phosphorus (P) element indicates that long anaerobic phases (6 h) are more efficient than short ones (3 h) as a selector of EBPR bacteria in biofilms. In both comparisons, thespecific mass of P released in a 6 h period represents almost 50% more than the amount of P release in the shorter period (3 h). However, the presence of rapidly biodegradable COD in the influent of the anaerobic phase is a more effective selector, more important than the duration of the anaerobic phase: by doubling the amount of acetic acid in the influent, a similar 50% increase of P-release can be achieved at short anaerobic periods of 3 h. The effect of the strategy adopted in this study, focusing on selecting EBPR bacteria in biofilm, is shown by the P levels of 4% (total P/SST) in the sludge removed from the BF by backwashing in all periods.


2001 ◽  
Vol 2001 (9) ◽  
pp. 596-629
Author(s):  
Cesar R. Mota ◽  
Jacimaria R. Batista ◽  
Richard R. Unz ◽  
Heinrich Buch ◽  
Walter Johnson

1992 ◽  
Vol 26 (9-11) ◽  
pp. 2253-2256 ◽  
Author(s):  
M. C. Goronszy

The performance of three full-scale cyclic activated sludge facilities, operated for biological phosphorus removal is demonstrated. The facilities are operated without formal mixed anoxic or anaerobic sequences in a variable volume mode. The system is independent of fill-ratio operation for filamentous sludge bulking control.


1993 ◽  
Vol 28 (10) ◽  
pp. 377-385 ◽  
Author(s):  
K. Moriyama ◽  
M. Takahashi ◽  
Y. Harada

Some experiences concerning a retrofit design and operation for nutrients removal in small extended aeration plants are presented. In this study a new biological phosphorus removal process as well as a biological nitrogen removal process based on a sequential oxic-anoxic-oxic process is investigated. The denitrification in the first oxic zone has a high removing effect for nitrogen, and the oxidation reduction potential (ORP) value and dissolved oxygen (DO) concentration are useful indexes to maintain the optimum conditions of the first oxic zone for simultaneous denitrification. It is verified that the simultaneous denitrification can alleviate the alkalinity deficit problem against full nitrification by a stoichiometric analysis of alkalinity throughout the entire process. Additionally, a biological phosphorus removal process which uses a sludge blanket zone of secondary settling tank for phosphorus release is proposed.


1983 ◽  
Vol 15 (3-4) ◽  
pp. 1-13 ◽  
Author(s):  
James L Barnard

This paper briefly summarizes the early work on phosphorus removal in activated sludge plants in the U.S.A. and observed that such removals only occurred in low SRT plants of the plug flow type and in the Phostrip plants, neither designed for full nitrification. The discovery of simultaneous nitrogen and phosphorus removal, as well as full-scale experiments are discussed. The Phoredox process was proposed utilizing internal recycling for the removal of nitrates and an anaerobic first stage in which the incoming feed is used to obtain the necessary anaerobic conditions, essential as a conditioning step for the uptake of phosphorus. Proposed mechanisms are discussed.


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