scholarly journals PENGHILANGAN POLUTAN ORGANIK DAN PADATAN TERRSUSPENSI DI DALAM AIR LIMBAH DOMESTIK DENGAN PROSES MOVING BED BIOFILM REACTOR (MBBR)

2018 ◽  
Vol 8 (1) ◽  
Author(s):  
Nusa Idaman Said ◽  
Teguh Iman Santoso

One of the alternative technologies that could be used for domestic waste water treatment is the Moving Bed Biofilm Reactor (MBBR). MBBR in principle is activated sludge that is increased by adding media in to the reactor, so there are two treatments process happened inside, suspended growth and attached growth. This research is using bioball as a media which has surface area of ±210 m2/m3 by 20% volume of reactor volume. Wastewater treatment by MBBR uses variations of Hydraulic Retention time (HRT) 12, 8, 6, and 4 hours, then the parameters measured were BOD, COD, TSS, temperature, and pH. Result of the study shows that within HRT for 12 hours in aeration tank, removal efficiency of COD is 81,37%, BOD is 82,4%, and TSS is 90,05%. HRT for 8 hours, COD removal efficiency is 88,72%, BOD is 89,7%, and TSS is 92,06%. HRT for 6 hours, COD removal efficiency is 85,48%, BOD is 80,15%, and TSS is 94,85%. HRT for 4 hours, COD removal efficiency is 81,07%, BOD is 87,88%, and TSS is 94,86%. With a retention time of 4 hours, the effluent results domestic wastewater treatment using MBBR has met quality standards in accordance with KEPMEN LH no. 112 of 2003 on Domestic Wastewater Quality Standard and Jakarta Governor Regulation no. 122 of 2005 on Domestic Wastewater Management in Special Province of Jakarta. Keywords: Domestic wastewater, MBBR, bioball.

2018 ◽  
Vol 7 (1) ◽  
Author(s):  
Nusa Idaman Said ◽  
Muhammad Rizki Syabani

The treatment process of wastewater contains organic pollutant which used in Indonesia especially in Jakarta is generaly activated sludge process. The problem is its treated water quality which frequently does not yet fulfilled to effluent standard of wastewater. Some affecting factors  are hydraulic retention time (HRT) too short, the fluctuation of wastewater flow rate, unfavorable function of aeration process and also which do not less important is operational mistake caused by insufficient knowledge of operator. To overcome the mentioned problems it is needed technological innovation to increase efficiency of wastewater treatment process especially activated sludge process. Moving Bed Biofilm Reactor (MBBR) technology is one of the  effective alternative for treating wastewater containing organic pollutants. In principle, MBBR is a modification of the activated sludge process is enhanced by adding the media into the aeration tank.This paper describes the study of domestic waste water treatment  using MBBR process which is filled with bioball plastic media which has specific surface 210 m2/m3 as much as 20 % of the volume of the aeration tank for attaching microorganism to increase efficiency and  keep stability of process.Result of the study shows that within 12 hours, 8 hours, 6 hours and 4 hours of hydraulic retention time (HRT) in aeration tank and sludge circulation ratio 0f R = 1.0 Q, the removal efficiency of ammonia were 94.05 %, 93.42 %, 89 %, and 79.6 % respectively. In ammonia loading 0.106 – 0.302 kg/m3.day, the removal efficiency of ammonia were 95.54 – 83.01 %. The greater ammonia loading,  removal efficiency of  ammonia  is getting smaller. Optimal residence time is 6 hours with ammonia removal efficiency reached 89 %, and the average concentration of ammonia in the effluent of 8.3 mg per litre.  Keyword : Domestic wastewater, ammonia, bioball, MBBR.


2002 ◽  
Vol 45 (12) ◽  
pp. 321-328 ◽  
Author(s):  
G. Andreottola ◽  
P. Foladori ◽  
M. Ragazzi ◽  
R. Villa

Dairy raw wastewater is characterised by high concentrations and fluctuations of organic matter and nutrient loads related to the discontinuity in the cheese production cycle and machinery washing. The applicability of a Moving Bed Biofilm Reactor (MBBR) filled with FLOCOR-RMP® plastic media to the treatment of dairy wastewater was evaluated in a pilot-plant. COD fractionation of influent wastewater, MBBR performance on COD and nutrient removal were investigated. A removal efficiency of total COD over 80% was obtained with an applied load up to 52.7 gCOD m−2 d−1 (corresponding to 5 kgCOD m−3d−1). The COD removal kinetics for the MBBR system was assessed. The order of the kinetics resulted very close to half-order in the case of a biofilm partially penetrated by the substrate. The nitrogen removal efficiency varied widely between 13.3 and 96.2% due to the bacterial synthesis requirement. The application of a MBBR system to dairy wastewater treatment may be appropriate when upgrading overloaded activated sludge plants or in order to minimise reactor volumes in a pre-treatment.


2019 ◽  
Vol 25 (5) ◽  
pp. 652-658
Author(s):  
Huynh Tan Nhut ◽  
Nguyen Tri Quang Hung ◽  
Tran Cong Sac ◽  
Nguyen Huynh Khanh Bang ◽  
Tran Quang Tri ◽  
...  

This study evaluates the efficiency of domestic wastewater treatment via Sponge-Based Moving Bed Biofilm Reactor (S-MBBR). The laboratory-based treatment plan uses polyurethane sponge with a specific surface area was 260 m<sup>2</sup>/m<sup>3</sup> as a carrier. The treatment plan operated under four different organic load rate: OLR1 = 0.4 kg BOD/m<sup>3</sup>.day; OLR2 = 0.6 kg BOD/m<sup>3</sup>.day; OLR3 = 0.8 kg BOD/m<sup>3</sup>.day; and OLR4 = 1.0 kg BOD/m<sup>3</sup>.day. During 80 d of the experiment, the highest treatment efficiency was at the organic load rate of 0.4 kg BOD/m<sup>3</sup>.day, with COD, SS, TN and TP were found to be 85.0 ± 12.9%, 85.7 ± 5.3%, 68.9 ± 1.7%, and 40.3 ± 0.2%, respectively. In which, the influent SS concentration were from 117.3 to 126.0 mg/L, the effluent concentration were in ranged 18.0 to 34.22 mg/L, respectively. The values of influent and effluent COD were 298.8 ± 12.88 and 44.8 ± 3.78 mg/L in turn. The OLR1 influent TN, TP concentrations were respectively 47.9 ± 2.11 and 3.6 ± 0.15 mg/L; the effluent TN, TP concentration were 14.9 ± 0.18 and 2.2 ± 0.06 mg/L, respectively. The study suggests that the effluent is within the allowable limits of National technical regulation on domestic wastewater (Column B1), indicating the applicability of S-MBBR for the domestic wastewater treatment plant.


2003 ◽  
Vol 47 (1) ◽  
pp. 105-111 ◽  
Author(s):  
D.D. Sun ◽  
J.L. Zeng ◽  
J.H. Tay

A 4 L submerged tubular ceramic membrane bioreactor (MBR) was applied in laboratory scale to treat 2,400 mg-COD/L high strength wastewater. A prolonged sludge retention time (SRT) of 200 day, in contrast to the conventional SRT of 5 to 15 days, was explored in this study, aiming to reduce substantially the amount of disposed sludge. The MBR system was operated for a period of 142 days in four runs, differentiated by specific oxygen utilization rate (SOUR) and hydraulic retention time (HRT). It was found that the MBR system produced more than 99% of suspended solid reduction. Mixed liquor suspended solids (MLSS) was found to be adversely proportional to HRT, and in general higher than the value from a conventional wastewater treatment plant. A chemical oxygen demand (COD) removal efficiency was achieved as high as 98% in Run 1, when SOUR was in the range of 100-200 mg-O/g-MLVSS/hr. Unexpectedly, the COD removal efficiency in Run 2 to 4 was higher than 92%, on average, where higher HRT and abnormally low SOUR of 20-30 mg-O/g-MLVSS/hr prevailed. It was noted that the ceramic membrane presented a significant soluble nutrient rejection when the microbial metabolism of biological treatment broke down.


2017 ◽  
Vol 77 (4) ◽  
pp. 1027-1034 ◽  
Author(s):  
Yan-Xiang Cui ◽  
Di Wu ◽  
Hamish R. Mackey ◽  
Ho-Kwong Chui ◽  
Guang-Hao Chen

Abstract Sulfur-oxidizing autotrophic denitrification (SO-AD) was investigated in a laboratory-scale moving-bed biofilm reactor (MBBR) at a sewage temperature of 22 °C. A synthetic wastewater with nitrate, sulfide and thiosulfate was fed into the MBBR. After 20 days' acclimation, the reduced sulfur compounds were completely oxidized and nitrogen removal efficiency achieved up to 82%. The operation proceeded to examine the denitrification by decreasing hydraulic retention time (HRT) from 12 to 4 h in stages. At steady state, this laboratory-scale SO-AD MBBR achieved the nitrogen removal efficiency of 94% at the volumetric loading rate of 0.18 kg N·(mreactor3·d)−1. The biofilm formation was examined periodically: the attached volatile solids (AVS) gradually increased corresponding to the decrease of HRT and stabilized at about 1,300 mg AVS·Lreactor−1 at steady state. This study demonstrated that without adding external organic carbon, SO-AD can be successfully applied in moving-bed carriers. The application of SO-AD MBBR has shown the potential for sulfur-containing industrial wastewater treatment, brackish wastewater treatment and the upgrading of the activated sludge system. Moreover, the study provides direct design information for the full-scale MBBR application of the sulfur-cycle based SANI process.


2015 ◽  
Vol 1113 ◽  
pp. 806-811 ◽  
Author(s):  
Lariyah Mohd Sidek ◽  
Hairun Aishah Mohiyaden ◽  
Hidayah Basri ◽  
Gasim Hayder Ahmed Salih ◽  
Ahmad Hussein Birima ◽  
...  

Moving Bed Biofilm Reactor (MBBR) systems have been proven as an effective technology for water treatment and have been used for Biochemical Oxygen Demand/Chemical Oxygen Demand (BOD/COD-removal), as well as for nitrification and denitrification in municipal and industrial wastewater treatment. Conventional Activated Sludge (CAS), in particular, has been extensively used in wastewater treatment since decades ago. In this study, physical performance results for both MBBR and CAS were compared and evaluated on laboratory scale basis. The study aims to identify the best system performance in terms of constituent removal efficiency for effective management of the river purification plant. A novel parallel MBBR and CAS pilot plant were fabricated and operated to compare the physical performance of MBBR and CAS. Analysis of the performances for MBBR and CAS show, MBBR has higher COD (85%), AN (75%) and TSS (80%) removal rate compared to CAS COD (53%), AN (53%) and TSS (69%). For BOD removal rate, CAS shows 68% removal rate whereas MBBR shows only 65%. Thus CAS has shown slightly higher removal rate than MBBR. In terms of sludge production, MBBR sludge is less than CAS. Overall performance proves that MBBR has better rate of constituent removal efficiency compared to CAS in the laboratory basis study.


Author(s):  
Bruno de Oliveira Freitas ◽  
Luan de Souza Leite ◽  
Maria Teresa Hoffmann ◽  
Antonio Wagner Lamon ◽  
Luiz Antonio Daniel

Abstract Biological reactors with immobilized biomass on free carriers have provided new perspectives for wastewater treatment, once they reduce the system size and increase the treatment capacity. In this study, the performance of three Moving Bed Biofilm Reactors (MBBR) using different carriers (with and without protected surface area) were evaluated for domestic wastewater treatment in continuous flow. Each MBBRs (i.e., R1, R2, and R3) was filled at a ratio of 50% with high-density polyethylene carriers with different characteristics: both R1-K1 and R2-Corrugated tube with protected surface and R3-HDPE flakes without protected surface. Chemical oxygen demand (COD) removal of 80 ± 5.0, 80 ± 3.5, and 78 ± 2.4% was achieved by R1, R2, and R3, respectively. The oxygen uptake by biofilm attached on the carriers was 0.0079 ± 0.0013, 0.0033 ± 0.0015, and 0.0031 ± 0.0026 μg DO·mm−2 for the K1, corrugated tube, and HDPE flakes, respectively. No significant differences were observed between the performance of the three MBBRs in terms of physico-chemical parameters (alkalinity, pH, and dissolved inorganic carbon) and COD removal. Results showed that the carrier type and its characteristics (total area and with/without protected area) did not affect the organic matter removal. Thus, the carrier without a protected surface in MBBR could be a promising low-cost option for domestic wastewater treatment.


2021 ◽  
Vol 9 (2) ◽  
pp. 051
Author(s):  
Dhuhan Dhuhan ◽  
Laili Fitria ◽  
Ulli Kadaria

Abstract The increase in the number of hotels in Pontianak City has a impact, namely the increase in the generation of wastewater. The hotel wastewater treatment process is widely used by hotels in Pontianak, especially at the Aston hotel, which already has a sewage treatment plant with suspended biological treatment. The processed water often does not meet the quality standards of wastewater which may be disposed of in accordance with PERMEN/LH/68/2016 concerning domestic wastewater quality standards. In this study, the parameters measured were BOD, TSS and pH. The purpose of this study was to determine the efficiency of Aston hotel wastewater treatment using an attached reactorMBBR (moving bed biofilm reactor) with Kaldnes K3 media in reducing BOD and TSS parameters. Growing microorganisms and biofilms on adhesive media for 14 days. Giving Kaldnes K3 adhesive media as much as 30%. Based on the research results of Aston hotel wastewater treatment with attached reactor MBBR able to reduce BOD and TSS parameters. Best lowering efficiency in attached reactor MBBR with the best time of 7 days was able to reduce the BOD parameter from 109.81 mg/L became 7.28 mg/L with an efficiency of 93.37%, and the TSS parameter decreased from the initial concentration of 78 mg/L to 8 mg/L and the efficiency was 89.74%.  Keywords : BOD, Kaldnes, Hotel Waste Waste, MBBR, TSS Abstrak Peningkatan jumlah hotel di Kota Pontianak memberi dampak, yaitu meningkatnya timbulan limbah cair. Proses pengolahan air limbah hotel banyak digunakan hotel-hotel di Pontianak. Hotel Aston telah memiliki instalasi pengolahan limbah dengan pengolahan biologi tersuspensi. Air hasil olahannya sering kali belum memenuhi baku mutu air limbah yang boleh dibuang sesuai dengan PERMEN/ LH/ 68/ 2016 tentang baku mutu air limbah domestik. Pada penelitian ini parameter yang diukur yaitu BOD, TSS dan pH. Tujuan dari penelitian ini adalah untuk mengetahui efisiensi pengolahan limbah cair hotel Aston menggunakan reaktor terlekat MBBR (moving bed biofilm reactor) dengan media Kaldnes K3 dalam menurunkan parameter BOD dan TSS. Dilakukan penumbuhan mikroorganisme dan biofilm pada media lekat K3 selama 14 hari. Pemberian media lekat Kaldnes K3 sebanyak 30% dari volume reaktor. Berdasarkan hasil penelitian, pengolahan limbah cair hotel Aston dengan reaktor terlekat MBBR mampu menurunkan parameter BOD dan TSS. Efisiensi penurunan terbaik pada reaktor terlekat MBBR dengan waktu 7 hari, mampu menurunkan parameter BOD dari 109,81 mg/L menjadi 7,28 mg/L dengan efisiensi 93,37 %, dan penurunan parameter TSS dari konsentrasi awal 78 mg/L menjadi 8 mg/L (efisiensi 89,74%). Kata Kunci : BOD, Kaldnes, Limbah Cair Hotel, MBBR, TSS.


2020 ◽  
Vol 6 ◽  
pp. 340-344
Author(s):  
Andreia D. Santos ◽  
Rui C. Martins ◽  
Rosa M. Quinta-Ferreira ◽  
Luis M. Castro

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