scholarly journals Upgrading municipal lagoons in temperate and cold climates: Total nitrogen removal and phosphorus assimilation at ultra‐low temperatures

Author(s):  
Patrick M. D’Aoust ◽  
Simon Vincent ◽  
Guillaume LeBlond ◽  
Raheleh Arabgol ◽  
Richard Hérard ◽  
...  
2021 ◽  
Author(s):  
Patrick M. D'Aoust ◽  
Simon Vincent ◽  
Guillaume Leblond ◽  
Raheleh Arabgol ◽  
Richard Hérard ◽  
...  

In this study, a municipal lagoon with high wintertime effluent total ammonia nitrogen (TAN) concentrations was upgraded with a pilot-scale NIT-NIT-DENIT moving bed biofilm reactor (MBBR) treatment train to characterize its effluent over wintertime operation, investigate the feasibility of upgrading lagoons to achieve substantial biological total nitrogen removal across ultra-low temperatures (0.6 – 3.0°C) and investigate nitrification inhibition pathways in facultative lagoon systems at ultra-low temperatures. Throughout the study, it was observed that the system substantially reduced total nitrogen (TN) and total phosphorus (TP) effluent concentrations by an average of 69.0 ± 24.5% and 74.7 ± 20.1%, respectively, with average TN and TP concentrations exiting the treatment train of 7.60 ± 5.60 mg-N/L and 0.05 ± 0.02 mg-P/L, respectively, indicating the feasibility of upgrading municipal lagoons to meet increasing stringent effluent standards to ensure the perenniality of water resources. Furthermore, it was observed that sulfide toxicity may play an important role in the inhibition of nitrifying organisms in lagoons.


RSC Advances ◽  
2015 ◽  
Vol 5 (73) ◽  
pp. 59326-59334 ◽  
Author(s):  
A. Chen ◽  
Y. Chen ◽  
C. Ding ◽  
H. Liang ◽  
B. Yang

The presence of 2 and 5 mg L−1of tetracycline decreased total nitrogen removal. Tetracycline induced EPS release and decreased its protective role on cells. Denitrifiers instead of nitrifiers were negatively affected by tetracycline.


2010 ◽  
Vol 61 (9) ◽  
pp. 2259-2266 ◽  
Author(s):  
Styliani Kantartzi ◽  
Paraschos Melidis ◽  
Alexander Aivasidis

In the present study, a laboratory scale system, consisting of a primary settling tank, a continuous stirred tank reactor and a clarifier were constructed and operated, using wastewater from the municipal wastewater treatment plant in Xanthi, Greece. The system operated under intermittent aeration in aerobic/anoxic conditions and feeding of the wastewater once in every cycle. The unit was inoculated with sludge, which originated from the recirculation stream of the local wastewater treatment plant. The wastewater was processed with hydraulic retention time (HRT) of 12 h, in which various experimental states were studied regarding the combination of aerobic and anoxic intervals. The wastewater was fed in limited time once in every cycle of aerobic/anoxic conditions at the beginning of the anoxic period. The two states that exhibited highest performance in nitrification and total nitrogen removal were, then, repeated with HRT of 10 h. The results show that, regarding the nitrification stage and the organic load removal, the intermittent system achieved optimum efficiency, with an overall removal of biological oxygen demand (BOD5) and ammonium nitrogen in the range of 93–96% and 91–95% respectively. As far as the total nitrogen removal is concerned, and if the stage of the denitrification is taken into account, the performance of the intermittent system surpassed other methods, as it is shown by the total Kjeldahl nitrogen (TKN) removal efficiency of 85–87%. These operating conditions suppressed the growth of filamentous organisms, a fact reflected at the SVI values, which were lower than 150 ml/g.


2007 ◽  
Vol 55 (8-9) ◽  
pp. 59-65 ◽  
Author(s):  
A. Onnis-Hayden ◽  
P.B. Pedros ◽  
J. Reade

An experimental study investigating the nitrogen removal efficiency from the recycle stream generated in the dewatering facility of the anaerobically digested sludge at the Deer Island wastewater treatment plant (WWTP) in Boston was conducted using a single submerged attached growth bioreactor (SAGB), designed for simultaneous nitrification and denitrification. The applied nitrogen loading to the reactor ranged from 0.7 to 2.27 kg-N/m3·d, and the corresponding total nitrogen (TN) removal rate ranged from 0.38 to 1.8 kg-N/m3·d. The observed nitrification rates varied from 0.42 kg-N/m3·d to 1.45 kg-N/m3·d with an ammonia load of 0.5 kg-N/m3·d and 1.8 kg-N/m3·d, respectively. An average nitrification efficiency of 91% was achieved throughout the experiment. Denitrification efficiency varied from 55%, obtained without any addition of carbon source, to 95% when methanol was added in order to obtain a methanol/nitrate ratio of about 3 kg methanol/kg NO3−-N.


2021 ◽  
Vol 401 ◽  
pp. 123232
Author(s):  
Changhui Zhou ◽  
Jing Bai ◽  
Yan Zhang ◽  
Jinhua Li ◽  
Zhijing Li ◽  
...  

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