A full-scale operation of a novel activated sludge process without excess sludge production

1996 ◽  
Vol 34 (3-4) ◽  
pp. 395-404 ◽  
Author(s):  
H. Yasui ◽  
K. Nakamura ◽  
S. Sakuma ◽  
M. Iwasaki ◽  
Y. Sakai

The authors have presented a new concept of excess sludge elimination treatment with recirculation of sludge via ozonation in the activated sludge process. This paper is intended to clarify the potential application of the process to municipal and industrial wastewater treatments. In a full-scale operational experiment lasting 10 months under 550 kg/d of BOD loading, no excess sludge was needed to be withdrawn and no significant accumulation of inorganic solids occurred in the aeration tank. Most of the inorganic compounds in the sludge were released to the soluble phase. Material balance indicated that one-third of ozonated sludge was mineralized via the recirculation treatment, and thereby the requirement of sludge mass to be treated was 3.3 times as much as sludge to be eliminated. Effluent TOC was slightly higher than under the conventional activated sludge process, indicating that refractory TOC was released from the sludge eliminated by treatment. The amount of released TOC corresponded to less than 2 weight % of eliminated sludge under recirculation rates below 30% of total biomass in the aeration tank in a day, but increased at higher recirculation rates. The operation costs associated with the process were estimated to be lower than those of conventional dewatering and disposal.

1994 ◽  
Vol 30 (9) ◽  
pp. 11-20 ◽  
Author(s):  
H. Yasui ◽  
M. Shibata

A new process has been developed to reduce excess sludge production, in which both excess sludge digestion and wastewater treatment are conducted simultaneously in the same aeration tank. The ozonation enhances biological degradation of the activated sludge, which is decomposed in a subsequent biological treatment. A considerable amount of biomass is mineralized biologically in proportion to the amount of recirculated biomass from the ozonation stage to the biological stage. It was observed that the amount of excess sludge is reduced to nearly zero when 1.2 kg/m3-aeration tank volume of biomass is recirculated in a day from the biological stage to the ozonation stage at a BOD loading of 1.0 kg/m3/d. A biomass concentration of 4200 mg/L was maintained at 1.0 kg-BOD/m3/d without drawing excess sludge for 6 weeks of experimental period under ozone dose of 0.05 g-O3/g-SS and recirculation rate at 0.3 d−1. Only a limited difference in the effluent quality was observed between the new process and the conventional activated sludge process.


2001 ◽  
Vol 44 (10) ◽  
pp. 203-208 ◽  
Author(s):  
G.-H. Chen ◽  
S. Saby ◽  
M. Djafer ◽  
H.-K. Mo

This paper presents three new approaches to reduce excess sludge production in activated sludge systems: 1) modification of conventional activated sludge process with insertion of a sludge holding tank in the sludge return line; 2) chlorination of excess sludge so as to minimize excess sludge production; and 3) utilization of a metabolic uncoupler, 3, 3′, 4′, 5-Tetrachlorosalicylanilide (TCS) to maximize futile activity of sludge microorganisms thereby leading to a reduction of sludge growth. Pilot study was carried out to evaluate this modified activated sludge process (OSA). It has been confirmed that the OSA process is effective in reducing excess sludge; particularly when the ORP level in the sludge holding tank was kept at -250 mV, more than 50% of the excess sludge was reduced. This process can maintain the effluent quality and even perform with a better sludge settleability than a conventional system. Experimental work on the second approach showed that chlorination treatment of excess sludge at a chlorine dose of 0.066 g Cl2/g MLSS reduced the excess sludge by 60%, while concentration of THMS was found below 200 ppb in the treated sludge. However, such sludge chlorination treatment sacrificed sludge settleability. Thus, it is not feasible to introduce the chlorination step to a conventional system. The third approach confirmed that addition of TCS could reduce sludge growth effectively if the TCS concentration is greater than 0.4 ppm. A 0.8-ppm concentration of TCS actually reduced excess sludge by 45%. It was also experimentally demonstrated that presence of TCS increases the portion of active sludge microorganisms over the entire microbial population.


2006 ◽  
Vol 54 (5) ◽  
pp. 69-76 ◽  
Author(s):  
G.W. Strünkmann ◽  
J.A. Müller ◽  
F. Albert ◽  
J. Schwedes

The usability of mechanical disintegration techniques for the reduction of excess sludge production in the activated sludge process was investigated. Using three different disintegration devices (ultrasonic homogeniser, stirred media mill, high pressure homogeniser) and different operational parameters of the disintegration, the effect of mechanical disintegration on the excess sludge production and on the effluent quality was studied within a continuously operated, laboratory scale wastewater treatment system with pre-denitrification. Depending on the operational conditions and the disintegration device used, a reduction of excess sludge production of up to 70% was achieved. A combination of mechanical disintegration with a membrane bioreactor process with high sludge age is more energy effective concerning reduction of sludge production than with a conventional activated sludge process at lower sludge ages. Depending on the disintegration parameters, the disintegration has no, or only minor, negative effect on the soluble effluent COD and on the COD-removal capacity of the activated sludge process. Nitrogen-removal was slightly deteriorated by the disintegration, whereas the system used was not optimised for nitrogen removal before disintegration was implemented.


1997 ◽  
Vol 36 (11) ◽  
pp. 163-170 ◽  
Author(s):  
Yoshio Sakai ◽  
Tetsuro Fukase ◽  
Hidenari Yasui ◽  
Masahide Shibata

An activated sludge process which produces no excess sludge was developed. The process is very simple as a small amount of return sludge is ozonated and then returned to the aeration tank. The ozonation enhances biodegradability of activated sludge, which is biologically oxidized in the aeration tank. A full-scale plant for treating 450m3/d of municipal wastewater was constructed and has been operated successfully for 9 months. The amount of excess sludge eliminated is directly proportional to the amount of ozone dosed to the sludge. At the ozone dosing rate of 0.034 kg/kg-SS, complete elimination of excess sludge has been achieved when 4 times more amount of sludge is ozonated than that of the excess sludge expected in the treatment without ozonation. After 5 months of operation without any withdrawal of excess sludge, small amount of inorganic substances like sand and silt accumulated in the sludge. On the other hand, inert organic substances does not seem to accumulate. As for effluent quality, BOD and nitrogen were kept good. Although effluent SS was 2–15 mg/l higher compared to a control without ozonation, it has been well below the discharge limit.


2002 ◽  
Vol 46 (11-12) ◽  
pp. 71-76 ◽  
Author(s):  
M.R. Alavi Moghaddam ◽  
H. Satoh ◽  
T. Mino

A coarse pore filter can be applied inside the aeration tank to facilitate the separation of sludge from liquid instead of sedimentation. This filter has pores, which are irregular in shape, and the pore size is bigger than those of MF. The objectives of the study were to maintain as much as MLSS in the activated sludge process with coarse pore filter and to investigate the performance under high MLSS condition. Small-scale reactor results so far show good quality of effluent specially after starting the sludge bulking in the system in terms of SS, TOC, DOC and turbidity. The average carbon removal for 62 days operation of this system was about 94% (based on effluent DOC) and 87% (based on effluent TOC). The average sludge yield in this system is about 0.44 kg MLSS/kg TOC which is about 0.24 kg MLSS/kg BOD. This amount is less than those of conventional activated sludge and trickling filter.


1996 ◽  
Vol 33 (1) ◽  
pp. 311-323 ◽  
Author(s):  
A. Witteborg ◽  
A. van der Last ◽  
R. Hamming ◽  
I. Hemmers

A method is presented for determining influent readily biodegradable substrate concentration (SS). The method is based on three different respiration rates, which can be measured with a continuous respiration meter which is operated in a cyclic way. Within the respiration meter nitrification is inhibited through the addition of ATU. Simulations were used to develop the respirometry set-up and decide upon the experimental design. The method was tested as part of a large measurement programme executed at a full-scale plant. The proposed respirometry set-up has been shown to be suitable for a semi-on-line determination of an influent SS which is fully based on the IAWQ #1 vision of the activated sludge process. The YH and the KS play a major role in the principle, and should be measured directly from the process.


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