scholarly journals OPTIMATION OF FIRE EXTINGUISHMENT SYSTEMS IN X STATION CENTER OF CRUDE OIL AND GAS STORAGE

2021 ◽  
Vol 15 (1) ◽  
Author(s):  
Amiral Aziz ◽  
Andre Nugroho

This paper discusses some research results that were carried out to optimize the fire extinguishment system of X Station in South Sumatera. To optimize the fire extinguishing system at station X, a system modification has been done, which included: changes in the number of stockpile tank units, changes in capacity and dimensions of oil tanks, and changes in fire wall construction. With the change in capacity and dimensions, especially the storage tank unit, it is necessary to recalculate whether the water demand in the fire protection system is still sufficient according to the existing system condition. From this research, it can be concluded that the maximum flow rate of foam under the existing condition is 1631.6 gpm while the optimum ondition is 65% smaller than the existing system condition at 570.54 gpm. The cooling water flow rate of 615.09 gpm at optimum ondition is lower than the existing system conditions of 1409.33 gpm. The required water to the fire extinguishment system is 250 gpm; this value is smaller than the existing system capacity of 2074 gpm. By using performance curves of Grundfos Data Booklet, for the capacity of pump 1250 gpm, the total head pump and pump efficiency are obtained 103.48 m and 77.5 %, respectively. Keywords: optimation; tank; water; foam; pump

2001 ◽  
Author(s):  
E. D. Rogdakis ◽  
V. D. Papaefthimiou

Abstract It is a general trend today, the old centrifugal machines to be replaced by new absorption machines. The mass flow rate of the cooling water in the centrifugal machines is normally 30% less than that in the two-stage absorption chiller for the same refrigerating capacity. Some absorption chillers manufacturers have updated and improved the double-effect technology increasing the cooling water temperature difference from the typical value of 5.5°C to 7.4°C and reducing the cooling water flow rate by about 30%. Using such a modern double effect absorption unit to replace a centrifugal chiller the same cooling water circuit can be used and the total cost of the retrofit is minimized. In this case a new flow pattern of the cooling tower is developed, and in this paper the design of a new tower fill is predicted taking into account the new factors characterizing the operating conditions and the required performance of the tower. As an example, the operational curves of a modified cooling tower (1500 KW cooling power) used by a 240 RT double-effect absorption chiller are presented.


2015 ◽  
Vol 812 ◽  
pp. 112-117
Author(s):  
K.M. Kumar ◽  
P. Venkateswaran ◽  
P. Suresh

The coolant (water) pump assumes an important role of cooling system in IC engines. With upgrading of the engine power by turbocharging and turbo inter cooling, the water pump capacity needs to be increased corresponding to the power. This capacity enhancement has to be achieved without calling for a major change in the existing water pump, envelop and related fitment details. This requires a clear understanding of centrifugal pump for its performance parameter. One such engine is upgraded by turbocharging from 195PS to 240PS @2200 rpm. Improving water pump flow by changing the impeller dimensions, impeller casing, increase the suction, delivery pipe diameter had been done. Validation of the water pump in its actual engine installation was taken up as a part of the research work. Flow rate comparison of the new pump with the existing pump was made and the results were analyzed. The new water pump gives better flow rates for the engine speeds up to1800 rpm, beyond which the flow rate is slightly lesser than the existing pump.


2020 ◽  
Author(s):  
Sofi Hesti Fathia ◽  
Inkasandra Faranisa Kolang ◽  
Ricky Putro Satrio Wicaksono ◽  
Achmad Riadi ◽  
Yulianto Sulistyo Nugroho

2020 ◽  
Vol 1008 ◽  
pp. 177-185
Author(s):  
Hamed Abbady ◽  
Mahmoud Salem Ahmed ◽  
Hamdy Hassan ◽  
A.S.A. Mohamed

In this paper, an experimental work studies the principal operating parameters of a proposed desalination process using air humidification-dehumidification method. The major objective of this work is to determine the humid air behavior through the desalination system. Different operating conditions including the effect of the water temperature at the entry to the humidifier, the ratio of the mass of water to the air, the air/water flow rate, and cooling water at entry the dehumidifier on the desalination performance were studied. The results show that the freshwater increases with increasing the water temperature at the inlet of the humidifier, the ratio of the mass of water to air, and cooling water flow rate in the dehumidifier. Cooling water outlet temperature at the condenser increases with increasing the water temperature at humidifier inlet. Also, it decreases as increasing cooling water flow rate while the ratio of the mass of water to air achieves the highest productivity and gained output ratio (GOR). The achieved mass ratio (MR) is 4.5 and the mass flow rate of air is 0.8 kg/min.


Author(s):  
Farshad Farahbod ◽  
Sara Farahmand

Pretreatment, solar pond (SP), and forced circulation crystallizer (FCC) are the basic stages of one option to provide the goals of zero discharge desalination (ZDD) process. This work represents the performance of a solar pond that is coupled with forced circulation crystallizer as second and third stages of proposed zero discharge desalination process. The purpose of ZDD in this paper is gathering fresh water and saline crystals from effluent wastewater of the desalination unit of Mobin petrochemical complex. So, the SP unit is constructed after the pretreatment unit to concentrate the treated wastewater to about 20 wt. % as a suited feed for the FCC unit. Effects of solar insolation rate are investigated experimentally, during a year. In addition, the effect of cooling water flow rate of FCC on quality of effluent stream from SP as feed crystallizer is studied in this paper. The experimental results show the maximum evaporation rate from SP is obtained 5 l/(m2·d) when the insolation rate was about 2.5 × 104 kJ/(m2·d). Experiments show the suitable range of crystals growth (710 μm to 830 μm) in FCC is occurred when the cooling water flow rate in condenser is 9 kg/min. The size and the color of produced salt crystals will be optimized in this flow rate and energy consumption is measured as 6.98 kW·h.


2012 ◽  
Vol 246-247 ◽  
pp. 341-345
Author(s):  
Shi Lun Zuo

In order to improve design efficiency and reduce design cost, a new method combining numerical simulation with experimental verification was proposed in this study. Firstly, controllable process parameters such as continuous casting speed and cooling water flow rate, are robustly designed according to the numerical simulation results of flow field, process experiments were subsequently done on a newly developed continuous casting machine of lead slice, then the robust optimal design for the continuous casting process were gained. The results show that the cooling water flow significantly affects axial thickness of the lead slice, while the casting speed determines mainly its circumferential thickness. When the casting speed is between 280L/min and 320L/min, and the cooling water flow rate is between 950r/min and 1100r/min at the same time, the axial thickness and circumferential thickness can been kept respectively in1.0±0.03mm and 1.0±0.1mm, which meet the robust design requirements.


Energies ◽  
2020 ◽  
Vol 13 (14) ◽  
pp. 3589
Author(s):  
Shaowu Yin ◽  
Feiyang Xue ◽  
Xu Wang ◽  
Lige Tong ◽  
Li Wang ◽  
...  

Experimental heat transfer equipment with a buried tube granular bed was set up for waste heat recovery of flue gas. The effects of flue gas inlet temperature (1096.65–1286.45 K) and cooling water flow rate (2.6–5.1 m3/h) were studied through experiment and computational fluid dynamics’ (CFD) method. On the basis of logarithmic mean temperature difference method, the total heat transfer coefficient of the granular bed was used to characterize its heat transfer performance. Experimental results showed that the waste heat recovery rate of the equipment exceeded 72%. An increase in the cooling water flow rate and inlet gas temperature was beneficial to recovering waste heat. The cooling water flow rate increases from 2.6 m3/h to 5.1 m3/h and the recovery rate of waste heat increases by 1.9%. Moreover, the heat transfer coefficient of the granular bed increased by 4.4% and the inlet gas temperature increased from 1096.65 K to 1286.45 K. The recovery rate of waste heat increased by 1.7% and the heat transfer coefficient of the granular bed rose by 26.6%. Therefore, experimental correlations between the total heat transfer coefficient of a granular bed and the cooling water flow rate and inlet temperature of dusty gas were proposed. The CFD method was used to simulate the heat transfer in the granular bed, and the effect of gas temperature on the heat transfer coefficient of granular bed was studied. Results showed that the relative error was less than 2%.


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