scholarly journals A Bioreactor Designed for Restricting Oversize of Aerobic Granular Sludge

Processes ◽  
2021 ◽  
Vol 9 (2) ◽  
pp. 374
Author(s):  
Hongbo Feng ◽  
Honggang Yang ◽  
Jianlong Sheng ◽  
Zengrui Pan ◽  
Jun Li

Aerobic granular sludge (AGS) with oversized diameter commonly affects its stability and pollutant removal. In order to effectively restrict the particle size of AGS, a sequencing batch reactor (SBR) with a spiny aeration device was put forward. A conventional SBR (R1) and an SBR (R2) with the spiny aeration device treating tannery wastewater were compared in the laboratory. The result indicates that the size of the granular sludge from R2 was smaller than that from R1 with sludge granulation. The spines and air bubbles could effectively restrict the particle size of AGS by collision and abrasion. Nevertheless, there was no significant change in mixed liquor suspended solids (MLSS) and the sludge volume index (SVI) in either bioreactors. The removal (%) of chemical oxygen demand (COD) and ammonia nitrogen (NH4+-N) in these two bioreactors did not differ from each other greatly. The analysis of biological composition displays that the proportion of Proteobacteria decreased slightly in R2. The X-ray fluorescence (XRF) analysis revealed less accumulation of Fe and Ca in smaller granules. Furthermore, a pilot-scale SBR with a spiny aeration device was successfully utilized to restrict the diameter of granules at about 300 μm.

2015 ◽  
Vol 13 (3) ◽  
pp. 746-757 ◽  
Author(s):  
Bei Long ◽  
Chang-zhu Yang ◽  
Wen-hong Pu ◽  
Jia-kuan Yang ◽  
Guo-sheng Jiang ◽  
...  

Mature aerobic granular sludge (AGS) was inoculated for the start-up of a pilot-scale sequencing batch reactor for the treatment of high concentration solvent recovery raffinate (SRR). The proportion of simulated wastewater (SW) (w/w) in the influent gradually decreased to zero during the operation, while volume of SRR gradually increased from zero to 10.84 L. AGS was successfully domesticated after 48 days, which maintained its structure during the operation. The domesticated AGS was orange, irregular, smooth and compact. Sludge volume index (SVI), SV30/SV5, mixed liquor volatile suspended solids/mixed liquor suspended solids (MLVSS/MLSS), extracellular polymeric substances, proteins/polysaccharides, average particle size, granulation rate, specific oxygen utilization rates (SOUR)H and (SOUR)N of AGS were about 38 mL/g, 0.97, 0.52, 39.73 mg/g MLVSS, 1.17, 1.51 mm, 96.66%, 47.40 mg O2/h g volatile suspended solids (VSS) and 8.96 mg O2/h g VSS, respectively. Good removal effect was achieved by the reactor. Finally, the removal rates of chemical oxygen demand (COD), total inorganic nitrogen (TIN), NH4+-N and total phosphorus (TP) were more than 98%, 96%, 97% and 97%, respectively. The result indicated gradually increasing the proportion of real wastewater in influent was a useful domestication method, and the feasibility of AGS for treatment of high C/N ratio industrial wastewater.


2011 ◽  
Vol 255-260 ◽  
pp. 3037-3041 ◽  
Author(s):  
Kui Zu Su ◽  
Chang Wang ◽  
Hui Fang

Aerobic granules were cultivated in the sequencing batch reactor at 15-25°C, pH 7.0 ± 0.1. Settling time decreased from 5 minutes to 1 minute gradually. As increasing the chemical oxygen demand (COD) and NH3-N in influent, COD removal efficiency and mixed liquid suspended solids of the reactor increased. Sludge volume index decreased continuously for a few days and then stabilized at 22 ml g-1. Selective pressure induced by settling velocity was proved to play a crucial role in activated sludge granulation. Based on the continuously measured data, the granulation process was divided into three phases, granules namely initiating, developing and maturating.


Author(s):  
Nurazizah Mahmod ◽  
Norhaliza Abdul Wahab

Aerobic Granular Sludge (AGS) technology is a promising development in the field of aerobic wastewater treatment system. Aerobic granulation usually happened in sequencing batch reactors (SBRs) system. Most available models for the system are structurally complex with the nonlinearity and uncertainty of the system makes it hard to predict. A reliable model of AGS is essential in order to provide a tool for predicting its performance. This paper proposes a dynamic neural network approach to predict the dynamic behavior of aerobic granular sludge SBRs. The developed model will be applied to predict the performance of AGS in terms of the removal of Chemical Oxygen Demand (COD). The simulation uses the experimental data obtained from the sequencing batch reactor under three different conditions of temperature (30˚C, 40˚C and 50˚C). The overall results indicated that the dynamic of aerobic granular sludge SBR can be successfully estimated using dynamic neural network model, particularly at high temperature.


2006 ◽  
Vol 6 (6) ◽  
pp. 81-87 ◽  
Author(s):  
J. Wang ◽  
H.Q. Yu

In this study a two-step strategy was adopted to cultivate Polyhydroxybutyrate (PHB)-rich aerobic granular sludge in a sequencing batch reactor (SBR) fed with a synthetic wastewater. In the first step both oxygen and ammonia were initially limited, in order to enhance the PHB-storage ability of sludge. In the second step granular sludge was cultivated to get a high PHB volumetric productivity. The PHB content of sludge increased to 43.1±2.0% in the first step. During the sludge granulation, the PHB content was constant at 40±4.6%. With the granulation, the settling ability of the PHB-rich sludge continuously improved, as evidenced by a decreased sludge volume index. The matured PHB-rich granular sludge presented a buff color and regular morphology with elliptical and flat shape.


2012 ◽  
Vol 518-523 ◽  
pp. 5347-5350
Author(s):  
Jia Xie ◽  
Xiao Xiang Zhao ◽  
Xin Shan Song ◽  
Jun Hu Wei

The successful cultivation of aerobic granular sludge used for simultaneous nitrogen and phosphorus removal in sequencing batch reactor (SBR) was performed using a synthetic domestic wastewater and conventional flocculent activated sludge as seeding sludge. The removal efficiency of sludge for chemical oxygen demand (COD),ammonia nitrogen and phosphate was 92.4%,88.1% and 95.9%, respectively. After screening, a strain was obtained with high efficient in nitrogen and phosphorus removal. By analyzing, the strain was identified as Raoultella ornithinolytica. After strain accumulation, the strain cultured at 30°C for 24h. The ammonia nitrogen and phosphate removal efficiency were 78.3% and 92%, respectively.


Author(s):  
Xiaoying Zheng ◽  
Yuan Zhang ◽  
Wei Chen ◽  
Weihong Wang ◽  
Hang Xu ◽  
...  

Due to the increased use of cerium oxide nanoparticles (CeO2 NPs), their potential environmental risks have caused concern. However, their effects on the aerobic granular sludge (AGS) process and the later recovery of AGS are still unclear. In this study, we comprehensively determined the changes in pollutant removal and the levels of extracellular polymeric substances (EPS) in AGS that were exposed to CeO2 NP treatments (0 (the control, R0), 1 (R1), and 5 (R5) mg/L), following an increase in the influent chemical oxygen demand (COD). An increase in the CeO2 NP concentration enhanced their inhibitory effect on the removal of total nitrogen (TN) and total phosphorus (TP), and promoted the production of polysaccharides (PS) and proteins (PN) in loosely bound EPS (LB-EPS) or tightly bound EPS (TB-EPS), as well as the dissolved organic carbon (DOC) components in EPS, but had no long-term effects on the removal of organic matter. When the addition of CeO2 NPs was stopped and the concentration of influent COD increased, the TN and TP removal efficiencies in R1 and R5 slowly increased and recovered. In R1, they were only 4.55 ± 0.55% and 2.71 ± 0.58% lower than in R0, respectively, while the corresponding values for R5 were 5.06 ± 0.46% and 6.20 ± 0.63%. Despite the LB-EPS and TB-EPS concentrations in the R1 and R5 treatments recovering and being similar to the levels in the control when no CeO2 NPs were added, they were still slightly higher than in the R0, which indicating that the negative effects of CeO2 NPs could not be completely eliminated due to the residual CeO2 NP levels in AGS.


2006 ◽  
Vol 53 (9) ◽  
pp. 79-85 ◽  
Author(s):  
Z.H. Li ◽  
T. Kuba ◽  
T. Kusuda

In order to evaluate the characteristics of aerobic granular sludge, a sequencing batch reactor, feeding with synthetic wastewater at the organic loading rate of 8 kg COD/m3 d, was employed on the laboratory scale. Granules occurred in the reactor within 1 week after the inoculation from conventional flocculent sludge. Aerobic granular sludge was characterised by the outstanding settling properties and considerable contaminates removal efficiencies. The SVI30 values were in the range of 20 to 40 ml g−1. However, the sludge volume index of short settling time (e.g. SVI10 – 10 min) is suggested to describe the fast settling properties of aerobic granular sludge. The potential application in the decentralised system is evaluated from the point view of footprint and high bioactivity. The occurrence of sloughing, resulting from the outgrowth of filamentous organisms, would be responsible for the instability of aerobic granules. The starvation phase should therefore be carefully controlled for the maintenance and stability of aerobic granular sludge system.


2015 ◽  
Vol 71 (3) ◽  
pp. 440-445 ◽  
Author(s):  
C. Bumbac ◽  
I. A. Ionescu ◽  
O. Tiron ◽  
V. R. Badescu

The focus of this study was to assess the treatment performance and granule progression over time within a continuous flow reactor. A continuous flow airlift reactor was seeded with aerobic granules from a laboratory scale sequencing batch reactor (SBR) and fed with dairy wastewater. Stereomicroscopic investigations showed that the granules maintained their integrity during the experimental period. Laser diffraction investigation showed proof of new granules formation with 100–500 μm diameter after only 2 weeks of operation. The treatment performances were satisfactory and more or less similar to the ones obtained from the SBR. Thus, removal efficiencies of 81–93% and 85–94% were observed for chemical oxygen demand and biological oxygen demand, respectively. The N-NH+4 was nitrified with removal efficiencies of 83–99% while the nitrate produced was simultaneously denitrified – highest nitrate concentration determined in the effluent was 4.2 mg/L. The removal efficiency of total nitrogen was between 52 and 80% depending on influent nitrogen load (39.3–76.2 mg/L). Phosphate removal efficiencies ranged between 65 and above 99% depending on the influent phosphate concentration, which varied between 11.2 and 28.3 mg/L.


Sign in / Sign up

Export Citation Format

Share Document