scholarly journals Study on the Performance Improvement of Axial Flow Pump’s Saddle Zone by Using a Double Inlet Nozzle

Water ◽  
2020 ◽  
Vol 12 (5) ◽  
pp. 1493
Author(s):  
Weidong Cao ◽  
Wei Li

The operating range of axial flow pumps is often constrained by the onset of rotating stall. An improved method using a double inlet nozzle to stabilize the performance curve is presented in the current study; a single inlet nozzle and three kinds of double inlet nozzle with different rib gap widths at the inlet of axial flow pump impeller were designed. Three dimensional (3D) incompressible flow fields were simulated, and the distributions of turbulence kinetic energy and velocity at different flow rates located at the inlet section, as well as the pressure and streamline in the impeller, were obtained at the same time. The single inlet nozzle scheme and a double inlet nozzle scheme were studied; the experimental and numerical performance results show that although the cross section is partly blocked in the double inlet nozzle, the head and efficiency do not decline at stable operation flow rate. On small flow rate condition, the double inlet nozzle scheme effectively stabilized the head-flow performance, whereby the block induced by the backflow before the impeller was markedly improved by using a double inlet nozzle. It has also been found that the rib gap width impacts the efficiency curve of the axial flow pump.

Author(s):  
Desheng Zhang ◽  
Weidong Shi ◽  
Suqing Wu ◽  
Dazhi Pan ◽  
Peipei Shao ◽  
...  

In this paper, the tip leakage vortex (TLV) structures in an axial flow pump were investigated by numerical and experimental methods. Based on the comparisons of different blade tip clearance size (i.e., 0.5 mm, 1mm and 1.5mm) and different flow rate conditions, TLV trajectories were obtained by Swirling Strength method, and simulated by modified SST k-ω turbulence model with refined high-quality structured grids. A high-speed photography test was carried out to capture the tip leakage vortex cavitation in an axial flow pump with transparent casing. Numerical results were compared with the experimental leakage vortex trajectories, and a good agreement is presented. The detailed trajectories show that the start point of tip leakage vortex appears near the leading edge at small flow rate, and it moves from trailing edge to about 30% chord span at rated flow rate. At the larger flow rate condition, the starting point of TLV shifts to the middle of chord, and the direction of TLV moves parallel to the blade hydrofoil. As the increasing of the tip size, the start point of TLV trajectories moves to the central of chord and the minimum pressure in vortex core is gradually reduced.


1983 ◽  
Vol 105 (3) ◽  
pp. 277-283 ◽  
Author(s):  
M. Murakami ◽  
K. Minemura

Motion of air bubbles in a high-specific-speed axial-flow pump impeller was analyzed on the basis of measured streak lines of air bubbles in the impeller. The results were compared with those obtained by a numerical solution of the bubble motion equations for three dimensional flow. Governing factors of the bubble motion are the drag force due to the surrounding water and the force due to the pressure gradient. Trajectories of the bubbles deviate somewhat from the streamlines of water, and the amount of the deviation is dependent on the bubble diameter and also on specific-speeds of the pumps and flow rate of water.


Author(s):  
Shuichi Yamashita ◽  
Satoshi Watanabe ◽  
Kusuo Okuma ◽  
Kyota Shirasawa ◽  
Akinori Furukawa

An application of contra-rotating rotors, in which a rear rotor is employed in tandem with a front one and these rotors rotate in the opposite direction each other, has been proposed against a demand for developing higher specific speed axial flow pump. The internal flow field of pump should be considered in the design for higher performance and more stable operation. The flow field in contra-rotating axial flow pump was measured with LDV and wall pressure measurements. In the present paper, the experimental results are shown and the flow behaviors would be discussed.


Author(s):  
S Sarkar

The results presented here are part of a detailed programme measuring the aerodynamics of a high specific speed mixed flow pump impeller over a wide range of operating conditions, including its behaviour in the unsteady stalled regime. The aim is to elucidate the physics of the flow through such an impeller. The noticeable features are the formation of part-span rotating stall cells having no periodicity and organized structure at reduced flow and also the shifting positions of reversal flow pockets as the flowrate changes. Measurements of loss and its variation with span-wise positions and flowrates enable the variation of local efficiency to be determined. The overall flow picture is similar to that expected in an axial flow impeller, though the present impeller displays a narrow stall hysteresis loop almost right through its operating range.


Author(s):  
Takaharu Tanaka

There is a correlation between the efficiency of the pump to the head produced. On the axial flow pump, whose efficiency characteristic is favorable, the pressure head gradient between the impeller inlet and the outlet sections, at an equivalent flow rate, may become larger than that for the less favorable axial flow pump. This fundamental interrelation may be held in the flow passage regardless to the flow rate whichever they are operated at design or off design flow rate. There may be a direct correlation between the efficiency of an axial flow pump and the ratio of the discharge valve cross section divided by the pipeline cross section. The smaller this ratio is the better the pressure head gradient is for the same flow rates. This ratio may be useful to estimate relative grade of heads, pressure head gradients, internal flow conditions, and efficiency characteristics among axial flow pumps.


2016 ◽  
Vol 2016 ◽  
pp. 1-10 ◽  
Author(s):  
Fan Yang ◽  
Hao-ru Zhao ◽  
Chao Liu

In order to investigate the influence of adjustable outlet guide vane on the hydraulic performance of axial-flow pump at part loads, the axial-flow pump with 7 different outlet guide vane adjustable angles was simulated based on the RNG k-ε turbulent model and Reynolds time-averaged equations. The Vector graphs of airfoil flow were analyzed in the different operating conditions for different adjustable angles of guide vane. BP-ANN prediction model was established about the effect of adjustable outlet guide vane on the hydraulic performance of axial-flow pump based on the numerical results. The effectiveness of prediction model was verified by theoretical analysis and numerical simulation. The results show that, with the adjustable angle of guide vane increasing along clockwise, the high efficiency area moves to the large flow rate direction; otherwise, that moves to the small flow rate direction. The internal flow field of guide vane is improved by adjusting angle, and the flow separation of tail and guide vane inlet ledge are decreased or eliminated, so that the hydraulic efficiency of pumping system will be improved. The prediction accuracy of BP-ANN model is 1%, which can meet the requirement of practical engineering.


Author(s):  
Fang-Ping Tang ◽  
Chao Liu ◽  
Ji-Ren Zhou ◽  
Hua Yang ◽  
Li Cheng

In this study, an axial flow pump impeller without guide vanes is experimentally investigated. The impeller used in the experiments consists of four blades. The particle image velocimetry technique and a five-hole probe have been used. Measurements of flow velocities in the outer part of the impeller have been made. PIV measurements have been realized in 12 meridian planes between blade-to-blade for design and off-design operating conditions. The meridian velocity is obtained with phase averaged method and the total circumferential mean velocity is obtained with an arithmetical average over the 12 circumferential data. The calculation is based on the CFX-TASC flow CFD code solving the three-dimensional Reynolds-averaged Navier-Stokes equation with RNG k–ε model of turbulence. The paper focuses on the comparisons of the results. Difference for the flow field between numerical and experimental results is small at large and design flow rate, while big difference occurs at small flow rate. It indicates that the numerical model is not suitable for separation flow.


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