Preswirl and Mixed-Flow (Mainly Liquid) Effects on Rotordynamic Performance of a Long (L/D = 0.75) Smooth Seal

Author(s):  
Dung L. Tran ◽  
Dara W. Childs ◽  
Hari Shrestha ◽  
Min Zhang

Abstract Measured results are presented for rotordynamic coefficients and mass leakage rates of a long smooth annular seal (length-to-diameter ratio L/D = 0.75, diameter D = 114.686 mm, and radial clearance Cr = 0.200 mm) tested with a mixture of silicone oil (PSF-5cSt) and air. The test seal is centered, the seal exit pressure is maintained at 6.9 bars-g while the fluid inlet temperature is controlled within 37.8–40.6 °C. It is tested with three inlet-preswirl inserts, namely, zero, medium, and high (the preswirl ratios (PSRs), i.e., the ratio between the fluid's circumferential velocity and the shaft surface's velocity, are in ranges of 0.10–0.18, 0.30–0.65, and 0.65–1.40 for zero, medium, and high preswirls, respectively), six inlet gas-volume fractions GVFi (0%, 2%, 4%, 6%, 8%, and 10%), four pressure drops PDs (20.7, 27.6, 34.5, and 41.4 bars), and three speeds ω (3, 4, and 5 krpm). The targeted test matrix could not be achieved for the medium- and high-preswirl inserts at PD ≥ 27.6 bars due to the test-rig stator's dynamic instability issues. Spargers were used to inject air into the oil, and GVFi values higher than 0.10 could not be consistently achieved because of unsteady surging flow downstream from the sparger mixing section. Leakage mass flow rate m˙ and rotordynamic coefficients are measured, and the effect of changing inlet preswirl and GVFi is studied. The test results are then compared with predictions from a two-phase, homogeneous-mixture, bulk-flow model developed in 2011. Generally, both measurements and predictions show little change in m˙ as inlet preswirl changes. Measured m˙ remains unchanged or slightly increases with increasing GVFi, but predicted m˙ decreases. Measured m˙ is comparable to predicted values but consistently lower. Dynamic-stiffness coefficients are measured using an ensemble of excitation frequencies and curve-fitted well by frequency-independent stiffness Kij, damping Cij, and virtual mass Mij coefficients. Planned tests with the medium- and high-preswirl inserts could not be accomplished at PD = 34.5 and 41.4 bars because the seal stator became unstable with any finite injection of air. The test results show that the instability arose because the seal's direct stiffness K became negative and increased in magnitude with increasing GVFi. The model predicts a drop in K as GVFi increases, but the test results dropped substantially more rapidly than predicted. Also, the model does not predict the observed strong tendency for K to drop with an increase in preswirl in moving from the zero-to-medium and medium-to-high preswirl inserts. The authors believe that the observed drop in K due to increasing GVFi is not explained by either (a) a reverse Lomakin effect from operating in the transition flow regime or (b) the predicted drop in K at higher GVFi values from the model. A separate and as yet unidentified two-phase flow phenomenon probably causes the observed results. The negative K results due to increasing GVFi and moving from the zero to medium, and medium to high preswirl observed here could explain the instability issue (sudden subsynchronous vibration) on a high-differential-pressure helico-axial multiphase pump (MPP), reported in 2013. Effective damping Ceff combines the stabilizing effect of direct damping C, the destabilizing effect of cross-coupled stiffness k, and the influence of cross-coupled mass mq. As predicted and measured, increasing inlet preswirl significantly increases k and decreases Ceff, which decreases the seal's stabilizing properties. Ceff increases with increasing GVFi—becomes more stable.

Author(s):  
Dung L. Tran ◽  
Dara W. Childs ◽  
Hari Shrestha ◽  
Min Zhang

Abstract Measured results are presented for rotordynamic coefficients and mass leakage rates of a long smooth annular seal (length-to-diameter ratio L/D = 0.75, diameter D = 114.686 mm, and radial clearance Cr = 0.200 mm) tested with a mixture of silicone oil (PSF-5cSt) and air. The test seal is centered, the seal exit pressure is maintained at 6.9 bars-g while the fluid inlet temperature is controlled within 37.8–40.6°C. It is tested with 3 inlet-preswirl inserts, namely, zero, medium, and high (the preswirl ratios, i.e., the ratio between the fluid’s circumferential velocity and the shaft surface’s velocity, are in ranges of 0.10–0.18, 0.30–0.65, and 0.65–1.40 for zero, medium, and high preswirls, respectively), 6 inlet gas-volume-fractions GVFi (0%, 2%, 4%, 6%, 8%, 10%), 4 pressure drops PD (20.7, 27.6, 34.5, 41.4 bars), and 3 speeds ω (3, 4, 5 krpm). The targeted test matrix could not be achieved for the medium- and high-preswirl inserts at PD ≥ 27.6 bars due to the test-rig stator’s dynamic instability issues. Spargers were used to inject air into the oil, and GVFi values higher than 0.10 could not be consistently achieved because of unsteady surging flow downstream from the sparger mixing section. Leakage mass flow rate ṁ and rotordynamic coefficients are measured, and the effect of changing inlet preswirl and GVFi are studied. The test results are then compared with predictions from a 2-phase, homogeneous-mixture, bulk-flow model developed in 2011. Generally, both measurements and predictions show little change in ṁ as inlet preswirl changes. Measured ṁ remains unchanged or slightly increases with increasing GVFi, but predicted ṁ decreases. Measured ṁ is comparable to predicted values but consistently lower. Dynamic-stiffness coefficients are measured using an ensemble of excitation frequencies and curve-fitted well by frequency-independent stiffness Kij, damping Cij, and virtual mass Mij coefficients. Planned tests with the medium and high-preswirl inserts could not be accomplished at PD = 34.5 and 41.4 bars because the seal stator became unstable with any finite injection of air. The test results show that the instability arose because the seal’s direct stiffness K became negative and increased in magnitude with increasing GVFi. The model predicts a drop in K as GVFi increases, but the test results dropped substantially more rapidly than predicted. Also, the model does not predict the observed strong tendency for K to drop with an increase in preswirl in moving from the zero-to-medium, and medium-to-high preswirl inserts. The authors believe that the observed drop in K due to increasing GVFi is not explained by either: (a) A reverse Lomakin effect from operating in the transition flow regime, or (b) The predicted drop in K at higher GVFi values from the model. A separate and as yet unidentified 2-phase flow phenomenon probably causes the observed results. The negative K results due to increasing GVFi and moving from the zero to medium, and medium to high preswirl observed here could explain the instability issue (sudden nonsynchronous vibration) on a high-differential-pressure helico-axial multiphase pump, reported in 2013. Effective damping Ceff combines the stabilizing effect of direct damping C, the destabilizing effect of cross-coupled stiffness k, and the influence of cross-coupled mass mq. As predicted and measured, increasing inlet preswirl significantly increases k and decreases Ceff, which decrease the seal’s stabilizing properties. Ceff increases with increasing GVFi — becomes more stable.


Author(s):  
Min Zhang ◽  
Dara W. Childs ◽  
Dung L. Tran ◽  
Hari Shrestha

Abstract This paper conducts a comprehensive study on the effects of the presence of air in the oil on the leakage and rotordynamic coefficients of a long-smooth seal (inner diameter D = 89.306 mm, radial clearance Cr = 0.140 mm, and length-diameter ratio L/D = 0.65) under laminar-two-phase flow conditions. The mixture consists of air and silicone oil with inlet gas volume fraction (GVF) up to 10%. Tests are performed at inlet temperature Ti = 39.4 °C, exit pressure Pe = 6.9 bars, pressure drop PD = 31, and 37.9 bars, and rotor speed ω = 5, 7.5, and 10 krpm. The test seal is always concentric with the rotor, and no intentional fluid prerotation is provided at the seal inlet. The complex dynamic stiffness coefficients Hij of the test seal are measured and fitted by the frequency-independent direct stiffness K, cross-coupled stiffness k, direct damping C, cross-coupled damping c, direct virtual-mass M, and cross-coupled virtual-mass mq coefficients. Under laminar flow conditions, increasing inlet GVF has negligible effects on K, k, C, and effective damping Ceff, while it decreases c and M. These trends are correctly predicted by San Andrés's bulk-flow model with laminar flow friction formula. As inlet GVF increases, measured leakage flow rate m˙ increases slightly. In general, the predictions of K, k, C, c, Ceff, and m˙ are reasonably close to measurements.


Author(s):  
Min Zhang ◽  
Dara W. Childs ◽  
Dung L. Tran ◽  
Hari Shrestha

Abstract This paper conducts a comprehensive study on the effects of the air presence in the oil on the leakage and rotordynamic coefficients of a long-smooth seal (inner diameter D = 89.306 mm, radial clearance Cr = 0.140 mm, and length-diameter ratio L/D = 0.65) under laminar-two-phase flow conditions. The mixture consists of air and silicone oil with inlet GVF (gas volume fraction) up to 10%. Tests are performed at inlet temperature Ti = 39.4 °C, exit pressure Pe = 6.9 bars, pressure drop PD = 31 and 37.9 bars, and rotor speed ω = 5, 7.5, and 10 krpm. The test seal is always concentric with the rotor, and no intentional fluid pre-rotation is provided at the seal inlet. The complex dynamic stiffness coefficients Hij of the test seal are measured and fitted by the frequency-independent direct stiffness K, cross-coupled stiffness k, direct damping C, cross-coupled damping c, direct virtual-mass M, and cross-coupled virtual-mass mq coefficients. Under laminar flow conditions, increasing inlet GVF has negligible effects on K, k, C, and effective damping Ceff, while it decreases c and M. These trends are correctly predicted by San Andrés’s bulk-flow model with laminar flow friction formula. As inlet GVF increases, measured leakage flow rate ṁ increases slightly. In general, the predictions of K, k, C, c, Ceff, and ṁ are reasonably close to measurements.


Author(s):  
Min Zhang ◽  
James E. Mclean ◽  
Dara W. Childs

A two-phase annular seal stand (2PASS) has been developed at the Turbomachinery Laboratory of Texas A&M University to measure the leakage and rotordynamic coefficients of division wall or balance-piston annular seals in centrifugal compressors. 2PASS was modified from an existing pure-air annular seal test rig. A special mixer has been designed to inject the oil into the compressed air, aiming to make a homogenous air-rich mixture. Test results are presented for a smooth seal with an inner diameter D of 89.306 mm, a radial clearance Cr of 0.188 mm, and a length-to-diameter ratio (L/D) of 0.65. The test fluid is a mixture of air and silicone oil (PSF-5cSt). Tests are conducted with inlet liquid volume fraction (LVF) = 0%, 2%, 5%, and 8%, shaft speed ω = 10, 15, and 20 krpm, and pressure ratio (PR) = 0.43, 0.5, and 0.57. The test seal is concentric with the shaft (centered), and the inlet pressure is 62.1 bar. Complex dynamic-stiffness coefficients are measured for the seal. The real parts are generally too dependent on excitation frequency Ω to be modeled by constant stiffness and virtual-mass coefficients. The direct real dynamic-stiffness coefficients are denoted as KΩ; the cross-coupled real dynamic-stiffness coefficients are denoted as kΩ. The imaginary parts of the dynamic-stiffness coefficients are modeled by frequency-independent direct C and cross-coupled c damping coefficients. Test results show that the leakage and rotordynamic coefficients are remarkable impacted by changes in inlet LVF. Leakage mass flow rate m˙ drops slightly as inlet LVF increases from zero to 2% and then increases with further increasing inlet LVF to 8%. As inlet LVF increases from zero to 8%, KΩ generally decreases except it increases as inlet LVF increases from zero to 2% when PR = 0.43. kΩ increases virtually with increasing inlet LVF from zero to 2%. As inlet LVF further increases to 8%, kΩ decreases or remains unchanged. C increases as inlet LVF increases; however, its rate of increase drops significantly at inlet LVF = 2%. Effective damping Ceff combines the stabilizing impact of C and the destabilizing impact of kΩ. Ceff is negative (destabilizing) for lower Ω values and becomes more destabilizing as inlet LVF increases from zero to 2%. It then becomes less destabilizing as inlet LVF is further increased to 8%. Measured m˙ and rotordynamic coefficients are compared with predictions from XLHseal_mix, a program developed by San Andrés (2011, “Rotordynamic Force Coefficients of Bubbly Mixture Annular Pressure Seals,” ASME J. Eng. Gas Turbines Power, 134(2), p. 022503) based on a bulk-flow model, using the Moody wall-friction model while assuming constant temperature and a homogenous mixture. Predicted m˙ values are close to measurements when inlet LVF = 0% and 2% and are smaller than test results by about 17% when inlet LVF = 5% and 8%. As with measurements, predicted m˙ drops slightly as inlet LVF increases from zero to 2% and then increases with increasing inlet LVF further to 8%. However, in the inlet LVF range of 2–8%, the predicted effects of inlet LVF on m˙ are weaker than measurements. XLHseal_mix poorly predicts KΩ in most test cases. For all test cases, predicted KΩ decreases as inlet LVF increases from zero to 8%. The increase of KΩ induced by increasing inlet LVF from zero to 2% at PR = 0.43 is not predicted. C is reasonably predicted, and predicted C values are consistently smaller than measured results by 14–34%. Both predicted and measured C increase as inlet LVF increases. kΩ and Ceff are predicted adequately at pure-air conditions, but not at most mainly air conditions. The significant increase of kΩ induced by changing inlet LVF from zero to 2% is predicted. As inlet LVF increases from 2% to 8%, predicted kΩ continues increasing versus that measured kΩ typically decreases. As with measurements, increasing inlet LVF from zero to 2% decreases the predicted negative values of Ceff, making the test seal more destabilizing. However, as inlet LVF increases further to 8%, the predicted negative values of Ceff drop versus measured values increase. For high inlet LVF values (5% and 8%), the predicted negative values of Ceff are smaller than measurements. So, the seal is more stabilizing than predicted for high inlet LVF cases.


Author(s):  
Hari Shrestha ◽  
Dara W. Childs ◽  
Dung L. Tran ◽  
Min Zhang

AbstractA two-phase annular-seal stand at the Turbomachinery Laboratory of Texas A&M University is utilized to experimentally investigate a labyrinth seal operating under two-phase flow conditions (a mixture of silicone oil and air). A long labyrinth seal (length-to-diameter ratio L/D = 0.75, diameter D = 114.729 mm, and radial clearance Cr = 0.213 mm) is tested at a supply pressure of 62 bars-g with inlet gas volume fraction GVFi ranging from 90 to 100%. Tests were conducted at three pressure ratios PR (0.3, 0.4, 0.5), three rotating speeds (5, 10, 15 krpm), six GVFi (90%, 92%, 94%, 96%, 98%, and 100%), and three inlet-preswirl inserts, namely, zero, medium, and high. Specifically, the ratio between the fluid's circumferential velocity and the shaft surface's velocity are in ranges of 0.0–0.2, 0.5–1.6, and 0.5–2.7 for the zero, medium, and high preswirls respectively. The direct dynamic stiffness KΩ is negative. As GVFi decreases (more liquid), KΩ becomes more negative for the zero preswirl. The effect of changing GVFi on KΩ for the medium and high preswirls is not as clear as for the zero preswirl. For the zero preswirl, as GVFi decreases, the cross-coupled dynamic stiffness kΩ and direct damping C damping increase. However, the effective damping Ceff values converge to almost the same positive value for higher frequencies. Hence, there is no significant effect of change in GVFi for the zero preswirl. For the high preswirl, as GVFi decreases, kΩ decreases and C increases. As GVFi decreases, Ceff becomes less negative and eventually becomes positive for frequencies higher than Ωc. This result indicates that at certain frequencies, the presence of liquid can make the labyrinth seals with high preswirl more stable. For the seal tested, a compressor running at 15 krpm and PR (ratio of seal exit pressure and seal inlet pressure) = 0.5 with the first critical speed of 7500 rpm (125 Hz) would experience an increase in stability with presence of liquid in the flow stream for the medium and high preswirls. However, for the range of GVFi considered here, if swirl brakes are used in a compressor application to reduce the preswirl, there would be no impact of liquid presence on the stability of the compressor. Concerning static measurements, leakage rate m˙ increases with decreases in GVFi but remains unchanged with increasing preswirl.


Author(s):  
Hari Shrestha ◽  
Dara W. Childs ◽  
Dung L. Tran ◽  
Min Zhang

Abstract A 2-phase annular-seal stand (2PASS) at the Turbomachinery Laboratory of Texas A&M University is utilized to experimentally investigate a labyrinth seal operating under 2-phase flow conditions (a mixture of silicone oil and air). A long labyrinth seal (length-to-diameter ratio L/D = 0.75, diameter D = 114.729 mm, and radial clearance Cr = 0.213 mm) is tested at a supply pressure of 62 bars-g with inlet gas volume fraction GVFi ranging from 90–100%. Tests were conducted at three pressure ratios PR (0.3, 0.4, 0.5), three rotating speeds (5, 10, 15 krpm), six GVFi (90%, 92%, 94%, 96%, 98%, 100%), and three inlet-preswirl inserts, namely, zero, medium, and high. Specifically, the ratio between the fluid’s circumferential velocity and the shaft surface’s velocity, are in ranges of 0.0–0.2, 0.5–1.6, and 0.5–2.7 for the zero, medium, and high preswirls, respectively. The direct dynamic stiffness KΩ is negative. As GVFi decreases (more liquid), KΩ becomes more negative for the zero preswirl. The effect of changing GVFi on KΩ for the medium and high preswirls is not as clear as for the zero preswirl. For the zero preswirl, as GVFi decreases, the cross-coupled dynamic stiffness kΩ and direct damping C damping increases. However, the effective damping Ceff values converge to almost the same positive value for higher frequencies. Hence, there is no significant effect of change in GVFi for the zero preswirl. For the high preswirl, as GVFi decreases, kΩ decreases and C increases. As GVFi decreases, Ceff becomes less negative and eventually becomes positive for frequencies higher than Ωc. This result indicates that at certain frequencies, the presence of liquid can make the labyrinth seals with high preswirl more stable. For the seal tested, a compressor running at 15 krpm and PR (ratio of seal exit pressure and seal inlet pressure) = 0.5 with the first critical speed of 7500 rpm (125 Hz) would experience an increase in stability with presence of liquid in the flow stream for the medium and high preswirls. However, for the range of GVFi considered here, if swirl brakes are used in a compressor application to reduce the preswirl, there would be no impact of liquid presence on the stability of the compressor. Concerning static measurements, leakage rate ṁ increases with decreases in GVFi but remains unchanged with increasing preswirl.


Author(s):  
Min Zhang ◽  
James E. Mclean ◽  
Dara W. Childs

A 2-phase annular seal stand (2PASS) has been developed at the Turbomachinery Laboratory of Texas A&M University to measure the leakage and rotordynamic coefficients of division wall or balance-piston annular seals in centrifugal compressors. 2PASS was modified from an existing pure-air annular seal test rig. A special mixer has been designed to inject the oil into the compressed air, aiming to make a homogenous air-rich mixture. Test results are presented for a smooth seal with an inner diameter D of 89.306 mm, a radial clearance Cr of 0.188 mm, and a length-to-diameter ratio L/D of 0.65. The test fluid is a mixture of air and Silicone oil (PSF-5cSt). Tests are conducted with inlet LVF = 0%, 2%, 5%, and 8%, shaft speed ω = 10, 15, and 20 krpm, and pressure ratio PR = 0.43, 0.5, and 0.57. The test seal is concentric with the shaft (centered), and the inlet pressure is 62.1 bars. Complex dynamic stiffness coefficients are measured for the seal. The real parts are generally too dependent on excitation frequency Ω to be modeled by constant stiffness and virtual mass coefficients. The direct real dynamic stiffness coefficients are denoted as KΩ; the cross-coupled real dynamic stiffness coefficients are denoted as kΩ. The imaginary parts of the dynamic stiffness coefficients are modeled by frequency-independent direct C and cross-coupled c damping coefficients. Test results show that the leakage and rotordynamic coefficients are remarkable impacted by changes in inlet LVF. Leakage mass flow rate ṁ drops slightly as inlet LVF increases from zero to 2%, and then increases with further increasing inlet LVF to 8%. As inlet LVF increases from zero to 8%, KΩ generally decreases except it increases as inlet LVF increases from zero to 2% when PR = 0.43. kΩ increases virtually with increasing inlet LVF from zero to 2%. As inlet LVF further increases to 8%, kΩ decreases or remains unchanged. C increases as inlet LVF increases; however, its rate of increase drops significantly at inlet LVF = 2%. Effective damping Ceff combines the stabilizing impact of C and the destabilizing impact of kΩ. Ceff is negative (destabilizing) for lower Ω values and becomes more destabilizing as inlet LVF increases from zero to 2%. It then becomes less destabilizing as inlet LVF is further increased to 8%. Measured ṁ and rotordynamic coefficients are compared with predictions from XLHseal_mix, a program developed by San Andrés [1] based on a bulk-flow model, using the Moody wall-friction model while assuming constant temperature and a homogenous mixture. Predicted ṁ values are close to measurements when inlet LVF = 0 and 2%, and are larger than measured values when inlet LVF = 5% and 8%. As with measurements, predicted ṁ drops slightly as inlet LVF increases from zero to 2%, and then increases with increasing inlet LVF further to 8%. However, in the inlet LVF range of 2∼8%, the predicted effects of inlet LVF on ṁ are weaker than measurements. XLHseal_mix poorly predicts KΩ in most test cases. For all test cases, predicted KΩ decreases as inlet LVF increases from zero to 8%. The increase of KΩ induced by increasing inlet LVF from zero to 2% at PR = 0.43 is not predicted. C is reasonably predicted, and predicted C values are consistently smaller than measured results by 14∼34%. Both predicted and measured C increase as inlet LVF increases. kΩ and Ceff are predicted adequately at pure-air conditions, but not at most mainly-air conditions. The significant increase of kΩ induced by changing inlet LVF from zero to 2% is predicted. As inlet LVF increases 2% to 8%, predicted kΩ continue increasing versus that measured kΩ typically decreases. As with measurements, increasing inlet LVF from zero to 2% decreases the predicted negative values of Ceff, making the test seal more destabilizing. However, as inlet LVF increases further to 8%, the predicted negative values of Ceff drops versus measured values increase. For high inlet LVF values (5% and 8%), the predicted negative values of Ceff are smaller than measurements. So, the seal is actually more stable than predicted for high inlet LVF cases.


2018 ◽  
Vol 140 (10) ◽  
Author(s):  
J. Alex Moreland ◽  
Dara W. Childs ◽  
Joshua T. Bullock

Electric submersible pumps (ESPs) utilize grooved-rotor/smooth-stator (SS/GR) seals to reduce leakage and break up contaminants within the pumped fluid. Additionally, due to their decreased surface area (when compared to a smooth seal), grooved seals decrease the chance of seizure in the case of rotor-stator rubs. Despite their use in industry, the literature does not contain rotordynamic measurements for smooth-stator/circumferentially grooved-rotor liquid annular seals. This paper presents test results consisting of leakage measurements and rotordynamic coefficients for a SS/GR liquid annular sdeal. Both static and dynamic variables are investigated for various imposed preswirl ratios (PSRs), static eccentricity ratios (0–0.8), axial pressure drops (2–8 bars), and running speeds (2–8 krpm). The seals' static and dynamic features are compared to those of a smooth seal with the same length, diameter, and minimum radial clearance. Results show that the grooves reduce leakage at lower speeds (less than 5 krpm) and higher axial pressure drops, but does little at higher speeds. The grooved seal's direct stiffness is generally negative, which would be detrimental to pump rotordynamics. As expected, increasing preswirl increases the magnitude of cross-coupled stiffness and increases the whirl frequency ratio (WFR). When compared to the smooth seal, the grooved seal has smaller effective damping coefficients, indicative of poorer stability characteristics.


2007 ◽  
Vol 129 (2) ◽  
pp. 398-406 ◽  
Author(s):  
Dara W. Childs ◽  
Matthew Graviss ◽  
Luis E. Rodriguez

Test results are presented for a smooth seal and three centrally grooved seals that are representative of buffered-flow oil seals in centrifugal compressors. The seals are short (L∕D≅0.21), with a diameter of 117mm and a nominal radial clearance of 0.085mm, netting the clearance-to-radius ratio 0.0015. The grooves have groove depth to clearance ratios (Dg∕Cr) of 5, 10, and 15. Test conditions include three shaft speeds from 4000rpm to 10,000rpm, three inlet oil pressures from 24bar to 70bar, and seal eccentricity ratios from 0 (centered) to 0.7. Dynamic results include stiffness, damping, and added-mass coefficients; static results include stator position, attitude angles, and seal leakage. Stiffness, damping, and mass coefficients plus leakage are compared for the seal geometries. Results show that all rotordynamic coefficients consistently decrease with increasing seal groove depths, and seal leakage is largely unchanged. Comparisons are also made between experimental results and predictions from a computer program based on a Reynolds + energy equation model. The model includes the assumption that a groove is large enough to create separate lands within the seal, creating a zero or negligible pressure perturbation within the groove. Test results show that even the deepest groove depth tested is not deep enough to satisfy this assumption.


Author(s):  
Dung L. Tran ◽  
Dara W. Childs ◽  
Hari Shrestha ◽  
Min Zhang

Abstract Recent multiphase-pump developments encountered several rotordynamic issues with smooth balance-piston seals, creating a need to better understand the performance of annular seals under multiphase-flow operation. This paper presents measurements of static and dynamic characteristics of a long smooth seal (L/D = 0.75, D = 114.686 mm, and Cr = 0.200 mm) operating under pure- and mainly air condition in which air is mixed with silicone oil (PSF-5cSt). Tests are performed at a supply pressure of 62.1 bars-a, three rotation speeds (5, 10, 15 krpm), three pressure ratios (PRs) (0.6, 0.5, 0.4), for a range of inlet liquid volume fraction (LVFi) from 0% to 8%. The results are then compared to: (1) the previous test reported by Zhang et al. (2017, “Experimental Study of the Static and Dynamic Characteristics of a Long Smooth Seal with Two-Phase, Mainly-air Mixtures,” J. Eng. Gas Turbines Power, 139(12), p. 122504) with similar testing condition but a different seal geometry (L/D = 0.65, D = 89.306 mm, and Cr = 0.188 mm) and (2) the predictions from a bulk-flow model developed by San Andrés (2012, “Rotordynamic Force Coefficients of Bubbly Mixture Annular Pressure Seals,” ASME J. Eng. Gas Turbines Power, 134(2), p. 022503). Results show a significant increase of direct dynamic stiffness KΩ as LVFi increases, especially at low PR. Test results reported by Zhang et al. (2017) has an opposite tendency of KΩ as an impact of increasing LVFi. Concerning cross-coupled dynamic stiffness kΩ and cross-coupled damping c, the results from Zhang et al. (2017) and the present results agree to the effects of changing speed, PR, and LVFi under pure- and mainly air conditions. As LVFi increases, direct damping C increases while test results reported by Zhang et al. (2017) showed no significant increase. Except for the direct dynamic stiffness and the impact of changing LVFi on the cross-coupled dynamic stiffness, the bulk-flow model of San Andrés (2012) predicts decently the tendencies and magnitudes of the rotordynamic coefficients.


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