Flow mixing inside a control-rod guide tube – Experimental tests and CFD simulations

2011 ◽  
Vol 241 (12) ◽  
pp. 4803-4812 ◽  
Author(s):  
Kristian Angele ◽  
Ylva Odemark ◽  
Mathias Cehlin ◽  
Bengt Hemström ◽  
Carl-Maikel Högström ◽  
...  
Author(s):  
Hernan Tinoco ◽  
Hans Lindqvist ◽  
Ylva Odemark ◽  
Carl-Maikel Ho¨gstro¨m ◽  
Kristian Angele

Two broken control rods and a large number of rods with cracks were found at the inspection carried out during the refueling outage of the twin reactors Oskarshamn 3 and Forsmark 3 in the fall of 2008. As a part of an extensive damage investigation, time dependent CFD simulations of the flow and the heat transfer in the annular region formed by the guide tube and control rod stem were carried out, [1]. The simulations together with metallurgical and structural analyses indicated that the cracks were initiated by thermal fatigue. The knowledge assembled at this stage was sufficient to permit the restart of both reactors at the end of year 2008 conditioned to that further studies to be carried out for clarifying all remaining matters. Additionally, all control rods were inserted 14% to protect the welding region of the stem. Unfortunately, this measure led to new cracks a few months later. This matter will be explained in the second part of this work, [2]. As a part of the accomplished complementary work, new CFD models were developed in conformity with the guidelines of references [3] and [4]. The new results establish the simulation requirements needed to accomplish accurate conjugate heat transfer predictions. Those requirements are much more rigorous than the ones needed for flow simulations without heat transfer. In the present case, URANS simulations, which are less resource consuming than LES simulations, seem to rather accurately describe the mixing process occurring inside the control rod guide tube. Structure mechanics analyses based on the CFD simulations show that the cracks are initiated by thermal fatigue and that their propagation and growth are probably enhanced by mechanical vibrations.


Author(s):  
Kristian Angele ◽  
Mathias Cehlin ◽  
Carl-Maikel Ho¨gstro¨m ◽  
Ylva Odemark ◽  
Mats Henriksson ◽  
...  

A large number of control rod cracks were detected during the refuelling outage of the twin reactors Oskarshamn 3 and Forsmark 3 in the fall of 2008. The extensive damage investigation finally lead to the restart of both reactors at the end of 2008 under the condition that further studies would be conducted in order to clarify all remaining matters. Also, all control rods were inserted 14% in order to locate the welding region of the control rod stem away from the thermal mixing region of the flow. Unfortunately, this measure led to new cracks a few months later due to a combination of surface finish of the new stems and the changed flow conditions after the partial insertion of the control rods. The experimental evidence reported here shows an increase in the extension of the mixing region and in the intensity of the thermal fluctuations. As a part of the complementary work associated with the restart of the reactors, and to verify the CFD simulations, experimental work of the flow in the annular region formed by the guide tube and control rod stem was carried out. Two full-scale setups were developed, one in a Plexiglass model at atmospheric conditions (in order to be able to visualize the mixing process) and one in a steel model to allow for a higher temperature difference and heating of the control rod guide tube. The experimental results corroborate the general information obtained through CFD simulations, namely that the mixing region between the cold crud-removal flow and warm by-pass flow is perturbed by flow structures coming from above. The process is characterized by low frequent, high amplitude temperature fluctuations. The process is basically hydrodynamic, caused by the downward transport of flow structures originated at the upper bypass inlets. The damping thermal effects through buoyancy is of secondary importance, as also the scaling analysis shows, however a slight damping of the temperature fluctuations can be seen due to natural convection due to a pre-heating of the cold crud-removal flow. The comparison between numerical and experimental results shows a rather good agreement, indicating that experiments with plant conditions are not necessary since, through the existing scaling laws and CFD-calculations, the obtained results may be extrapolated to plant conditions. The problem of conjugate heat transfer has not yet been addressed experimentally since complex and difficult measurements of the heat transfer have to be carried out. This type of measurements constitutes one of the main challenges to be dealt with in the future work.


Author(s):  
Eric Lillberg

The cracked control rods shafts found in two Swedish NPPs were subjected to thermal fatigue due to mixing of cold purge flow with hot bypass water in the upper part of the top tube on which the control rod guide tubes rests. The interaction between the jets formed at the bypass water inlets is the main source of oscillation resulting in low frequency downward motion of hot bypass water into the cold purge flow. This ultimately causes thermal fatigue in the control rod shaft in the region below the four lower bypass water inlets. The transient analyses shown in this report were done to further investigate this oscillating phenomenon and compare to experimental measurements of water temperatures inside the control rod guide tube. The simulated results show good agreement with experimental data regarding all important variables for the estimation of thermal fatigue such as peak-to-peak temperature range, frequency of oscillation and duration of the temperature peaks. The results presented in this report show that CFD using LES methodology and the open source toolbox OpenFOAM is a viable tool for predicting complex turbulent mixing flows and thermal loads.


Energies ◽  
2021 ◽  
Vol 14 (20) ◽  
pp. 6661
Author(s):  
Vladimir Anatolyevich Markov ◽  
Bowen Sa ◽  
Sergey Nikolaevich Devyanin ◽  
Anatoly Anatolyevich Zherdev ◽  
Pablo Ramon Vallejo Maldonado ◽  
...  

The article discusses the possibility of using blended biofuels from rapeseed oil (RO) as fuel for a diesel engine. RO blended diesel fuel (DF) and emulsified multicomponent biofuels have been investigated. Fuel physicochemical properties have been analyzed. Experimental tests of a diesel engine D-245 in the operating conditions of the external characteristic curve and the 13-mode test cycle have been conducted to investigate the effect of these fuels on engine performances. CFD simulations of the nozzle inner flow were performed for DF and ethanol-emulsified RO. The possibility of a significant improvement in brake thermal efficiency of the engine has been noted. The efficiency of using blended biofuels from RO as a motor fuel for diesel engines has been evaluated based on the experimental test results. It was shown that in comparison with the presence of RO in emulsified multicomponent biofuel, the presence of water has a more significant effect on NOx emission reduction. The content of RO and the content of water in the investigated emulsified fuels have a comparable influence on exhaust smoke reduction. Nozzle inner flow simulations show that the emulsification of RO changes its flow behaviors and cavitation regime.


PLoS ONE ◽  
2021 ◽  
Vol 16 (5) ◽  
pp. e0251817
Author(s):  
Paulo Roberto Freitas Neves ◽  
Turan Dias Oliveira ◽  
Tarcísio Faustino Magalhães ◽  
Paulo Roberto Santana dos Reis ◽  
Luzia Aparecida Tofaneli ◽  
...  

The transmission of SARS-CoV-2 through contact with contaminated surfaces or objects is an important form of transmissibility. Thus, in this study, we evaluated the performance of a disinfection chamber designed for instantaneous dispersion of the biocidal agent solution, in order to characterize a new device that can be used to protect individuals by reducing the transmissibility of the disease through contaminated surfaces. We proposed the necessary adjustments in the configuration to improve the dispersion on surfaces and the effectiveness of the developed equipment. Computational Fluid Dynamics (CFD) simulations of the present technology with a chamber having six nebulizer nozzles were performed and validated through qualitative and quantitative comparisons, and experimental tests were conducted using the method Water-Sensitive Paper (WSP), with an exposure to the biocidal agent for 10 and 30 s. After evaluation, a new passage procedure for the chamber with six nozzles and a new configuration of the disinfection chamber were proposed. In the chamber with six nozzles, a deficiency was identified in its central region, where the suspended droplet concentration was close to zero. However, with the new passage procedure, there was a significant increase in wettability of the surface. With the proposition of the chamber with 12 nozzles, the suspended droplet concentration in different regions increased, with an average increase of 266%. The experimental results of the new configuration proved that there was an increase in wettability at all times of exposure, and it was more significant for an exposure of 30 s. Additionally, even in different passage procedures, there were no significant differences in the results for an exposure of 10 s, thereby showing the effectiveness of the new configuration or improved spraying and wettability by the biocidal agent, as well as in minimizing the impact caused by human factor in the performance of the disinfection technology.


Author(s):  
Ronghua Chen ◽  
Lie Chen ◽  
Wenxi Tian ◽  
Guanghui Su ◽  
Suizheng Qiu

In the typical boiling water reactor (BWR), each control rod guide tube supports four fuel assemblies via an orificed fuel support piece in which a channel is designed to be a potential corium relocation path from the core region to the lower head under severe accident conditions. In this study, the improved Moving Particle Semi-implicit (MPS) method was adopted to analyze the melt flow and ablation behavior in this region during a severe accident of BWR. A three-dimensional particle configuration was constructed for analyzing the melt flow behavior within the fuel support piece. Considering the symmetry of the fuel support piece, only one fourth of the fuel support was simulated. The eutectic reaction between Zr (the material of the corium) and stainless steel (the material of the fuel support piece) was taken into consideration. The typical melt flow and freezing behaviors within the fuel support piece were successfully reproduced by MPS method. In all the simulation cases, the melt discharged from the hole of the fuel support piece instead of plugging the fuel support piece. The results indicate that MPS method has the capacity to analyze the melt flow and solidification behavior in the fuel support piece.


Author(s):  
Hidemasa Yamano ◽  
Yoshiharu Tobita

This paper describes experimental analyses using SIMMER-III/IV, which are two/three-dimensional multi-component multi-phase Eulerian fluid-dynamics codes, for the purpose of the code validation. Two topics of key phenomena in core disruptive accidents were presented in this paper: duct-wall failure and fuel discharge/relocation behavior. To analyze the duct-wall failure behavior, the SCARABEE BE+3 in-pile experiments were selected. The SIMMER-III calculation was in good agreement with the overall event progression; which was characterized by coolant boiling, clad melting, fuel failure, molten pool formation, duct-wall failure, etc.; observed in the experiment. The CAMEL C6 experiment investigated the fuel discharge and relocation behavior through a simulated control rod guide tube, which is important in evaluating the neutronic reactivity. SIMMER-IV well simulated fuel-coolant interaction, sodium voiding, fuel relocation behavior observed in the experiment. These experimental analyses indicated the validity of the SIMMER-III/IV computer code for the duct wall failure and fuel discharge/relocation behavior.


Processes ◽  
2020 ◽  
Vol 8 (11) ◽  
pp. 1511
Author(s):  
Blaž Oblak ◽  
Simon Babnik ◽  
Vivian Erklavec-Zajec ◽  
Blaž Likozar ◽  
Andrej Pohar

Computational fluid dynamics simulations (CFD) were used to evaluate mixing in baffled and unbaffled vessels. The Reynolds-averaged Navier−Stokes k–ε model was implemented in OpenFOAM for obtaining the fluid flow field. The 95% homogenization times were determined by tracer tests. Experimental tests were conducted by injecting sodium chloride into the vessel and measuring the conductivity with two conductivity probes, while the simulations replicated the experimental conditions with the calculation of the transport of species. It was found that the geometry of the system had a great effect on the mixing time, since the irregular flow distribution, which can be obtained with baffles, can lead to local stagnation zones, which will increase the time needed to achieve the homogenization of the solute. It was also found that measuring local, pointwise concentrations can lead to a high underestimation of the global mixing time required for the homogenization of the entire vessel. Dissolution of sucrose was also studied experimentally and by mathematical modeling. The dissolution of sucrose was found to be kinetically limited and a very good agreement was found between the experiments and the modeling approach. The extent of the applicability of CFD simulations was evaluated for enabling rapid process design via simulations.


Author(s):  
Walter Villanueva ◽  
Chi-Thanh Tran ◽  
Pavel Kudinov

An in-vessel stage of a severe core melt accident in a Nordic type Boiling Water Reactor (BWR) is considered wherein a decay-heated pool of corium melt inflicts thermal and mechanical loads on the lower-head vessel wall. This process induces creep leading to a mechanical failure of the reactor vessel wall. The focus of this study is to investigate the effect of Control Rod Guide Tube (CRGT) and top cooling on the modes of global vessel failure of the lower head. A coupled thermo-mechanical creep analysis of the lower head is performed and cases with and without CRGT and top cooling are compared. The debris bed heat-up, re-melting, melt pool formation, and heat transfer are calculated using the Phase-change Effective Convectivity Model and transient heat transfer characteristics are provided for thermo-mechanical strength calculations. The creep analysis is performed with the modified time hardening creep model and both thermal and integral mechanical loads on the reactor vessel wall are taken into account. Known material properties of the reactor vessel as a function of temperature, including the creep curves, are used as an input data for the creep analysis. It is found that a global vessel failure is imminent regardless of activation of CRGT and top cooling. However, if CRGT and top cooling is activated, the mode and timing of failure is different compared to the case with no CRGT and top cooling. More specifically, with CRGT and top cooling, there are two modes of global vessel failure depending on the size of the melt pool: (a) ‘ballooning’ of the vessel bottom for smaller pools, and (b) ‘localized creep’ concentrated within the vicinity of the top surface of the melt pool for larger pools. Without CRGT and top cooling, only a ballooning mode of global vessel failure is observed. Furthermore, a considerable delay (about 1.4 h) on the global vessel failure is observed for the roughly 30-ton debris case if CRGT and top cooling is implemented. For a much larger pool (roughly 200-ton debris), no significant delay on the global vessel failure is observed when CRGT and top cooling is implemented, however, the liquid melt fraction and melt superheat are considerably higher in non-cooling case.


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