Optimising the A/O cycle for phosphorus removal in a submerged biofilter under continuous feed

2000 ◽  
Vol 41 (4-5) ◽  
pp. 503-508 ◽  
Author(s):  
R.F. Gonçalves ◽  
F. Rogalla

This work describes laboratory scale research about Enhanced Biological Phosphorus Removal (EBPR) in a submerged biofilter under Anaerobic/Oxic (A/O) alternation and continuous feed. Its main purpose is to detail the behaviour of the reactor throughout the anaerobic and the aerobic phases of the A/O cycle, to study the importance of the anaerobic phase in the selection of the EBPR bacteria in the biofilm and to evaluate the consumption and the importance of the organic substrate during the anaerobic phase. The mass balance over the Phosphorus (P) element indicates that long anaerobic phases (6 h) are more efficient than short ones (3 h) as a selector of EBPR bacteria in biofilms. In both comparisons, thespecific mass of P released in a 6 h period represents almost 50% more than the amount of P release in the shorter period (3 h). However, the presence of rapidly biodegradable COD in the influent of the anaerobic phase is a more effective selector, more important than the duration of the anaerobic phase: by doubling the amount of acetic acid in the influent, a similar 50% increase of P-release can be achieved at short anaerobic periods of 3 h. The effect of the strategy adopted in this study, focusing on selecting EBPR bacteria in biofilm, is shown by the P levels of 4% (total P/SST) in the sludge removed from the BF by backwashing in all periods.

1994 ◽  
Vol 29 (7) ◽  
pp. 153-156 ◽  
Author(s):  
D. Wedi ◽  
P. A. Wilderer

Most of the fundamental processes responsible for enhanced biological phosphorus removal (EBPR) were obtained through laboratory tests under defined conditions with pure or enriched cultures. Acinetobacter sp. was identified as the most important group of bacteria responsible for bio-P removal. Full scale data showed, however, that laboratory results do not match full scale results well enough. There is a lack of data on the effects of sub-optimal process conditions such as inadequate availability of volatile fatty acids (VFA), high nitrate recycle, storm water inflow or low temperatures. In this paper the results of full scale experiments on P-release are presented and compared with theoretical values. Measurements at a full scale Phoredox-system showed a surprisingly low P-release in the anaerobic reactor. Only 4 to 10% of the phosphorus in the activated sludge was released in the bulk liquid. With laboratory batch-tests, a maximum of 20% of the P in the sludge could be released. It is assumed that under the prevailing process conditions either the fraction of Acinetobacter sp. was very small, or bacteria other than Acinetobacter sp. were responsible for the P-removal, or most of the phosphorus was bound chemically but mediated by biological processes.


2002 ◽  
Vol 46 (4-5) ◽  
pp. 193-200 ◽  
Author(s):  
D. Brandt ◽  
C. Sieker ◽  
W. Hegemann

The sorption-denitrification-P-removal (S-DN-P) process combines biological excess P-removal (BEPR) and denitrification using immobilized biomass. The accumulation of denitrifying polyP organisms is achieved by sequencing anaerobic/anoxic conditions. The immobilized biomass is in alternating contact with primary treated wastewater (anaerobic sorption-phase) and nitrified wastewater (denitrification phase). In the sorption phase, P-release takes place and readily biodegradable organic substrate, e.g. volatile fatty acid, is taken up and stored by polyP accumulating organisms (PAO). In addition to this, other organic matter is physically/chemically adsorbed in the biofilm structures. In the denitrification phase, the biomass denitrifies the stored and adsorbed organic substrate and, at the same time, P-uptake and polyP formation occurs. This paper presents results of investigations at laboratory and half-technical scale. At laboratory scale different types of carriers were tested regarding their suitability for the S-DN-P-process. In half-technical scale a biofilter and a moving bed reactor (MBR) were tested. In the biofilter a stable removal of nitrate and phosphate was achieved. However, it was not possible to achieve similar results in the MBR process. Especially the release and uptake of phosphate showed no clear tendency although the uptake of acetate was good. Reasons for this could be the accumulation of glycogen accumulating organisms which impair the metabolism of PAO.


1998 ◽  
Vol 38 (1) ◽  
pp. 97-105 ◽  
Author(s):  
J. Meinhold ◽  
H. Pedersen ◽  
E. Arnold ◽  
S. Isaacs ◽  
M. Henze

The continuous introduction of a biological phosphorus removal (BPR) promoting organic substrate to the denitrifying reactor of a BPR process is examined through a series of batch experiments using acetate as model organic substrate. Several observations are made regarding the influence of substrate availability on PHA storage/utilization and phosphate uptake/release. Under anoxic conditions PHB is utilized and phosphate is taken up, indicating that at least a fraction of the PAO can denitrify. The rates of anoxic P-uptake, PHB utilization and denitrification are found to increase with increasing initial PHB level. At low acetate addition rates the P-uptake and PHB utilization rates are reduced compared to when no acetate is available. At higher acetate addition rates a net P-release occurs and PHB is accumulated. For certain intermediate acetate addition rates the PHB level can increase while a net P-release occurs. Whether the introduction of BPR promoting organic substrates to the denitrifying reactor is detrimental to overall P-removal appears to be dependent on the interaction between aerobic P-uptake, which is a function of PHB level, and the aerobic residence time.


1994 ◽  
Vol 30 (11) ◽  
pp. 1-12 ◽  
Author(s):  
R. F. Gonçalves ◽  
F. N. Nogueira ◽  
L. Le Grand ◽  
F. Rogalla

An operational procedure is presented which enables biological phosphorus removal to be performed using a set of five submerged high rate biofilters. The new process was developed using an upflow biofilter with floating filter media, originally conceived to perform nitrification and denitrification of wastewaters (Biostyr-ND). Anaerobic contact periods were introduced in the functioning periods of the biofilters under continuous feed, ensuring alternating anaerobic/aerobic conditions (A/O) on the fixed biomass. The selection of phosphate-removing bacteria in the biofilm was verified by the efficiency of P removal (60 - 70%) and by the high concentrations of total P in the sludge removed from the system during backwash (≈ 3.4 % Pt/TSS). The activity of the autotrophic nitrifying bacteria was not affected by the alternating A/O conditions reached values close to 1 kg N-NH4/m3d. An improvement in the denitrification process was observed due to carbon storage during anaerobic contact.


1999 ◽  
Vol 39 (7) ◽  
pp. 33-40 ◽  
Author(s):  
Eberhard Morgenroth ◽  
Peter A. Wilderer

In contrast to enhanced biological phosphorus removal (EBPR) in activated sludge systems mass transfer processes have a major influence on overall phosphorus removal in biofilm reactors. Based on results from a laboratory scale sequencing batch biofilm reactor (SBBR) and from a mathematical model the influence of the following processes on EBPR in biofilms was evaluated: (1) mass transfer limitation for oxygen, (2) mass transfer limitation for organic substrate, (3) lack of controlled removal of biomass from the system. It was shown that mass transfer of soluble components (oxygen and organic substrate) had only a minor effect on overall phosphorus removal. Soluble components fully penetrate the biofilm at certain times during the SBBR cycle as a consequence of SBBR operation with large concentration variations over the cycle time. The limiting processes for EBPR is the efficient removal of phosphorus rich biomass from the reactor. Biomass at the base of the biofilm that is not removed during backwashing will release accumulated phosphorus due to lysis or endogenous respiration and will not contribute to net phosphorus removal. For efficient operation of EBPR in biofilm systems regular and intensive backwashing resulting in thin biofilms is suggested.


2002 ◽  
Vol 46 (4-5) ◽  
pp. 171-178 ◽  
Author(s):  
A.J. Schuler ◽  
D. Jenkins

Laboratory-scale sequencing batch reactors exhibiting enhanced biological phosphorus removal were analyzed for pH effects on anaerobic phosphorus (P) release, glycogen degradation, and acetate uptake. Samples with non-soluble P/total suspended solids values of either 0.13-0.14 mg/mg (HP) or 0.065-0.075 mg/mg (LP) were analyzed in anaerobic batch tests with excess acetate addition at pH values ranging from 5.2 to 9.5. A polyphosphate-accumulating metabolism (PAM) had a competitive advantage over a glycogen-accumulating metabolism (GAM) at pH > 7.0. Maximum acetate uptake rates by the HP and LP samples occurred at pH values 8.0 and 6.9, respectively. Anaerobic P release/acetate uptake increased with increasing pH at rates similar to previously reported values. Glycogen degradation/acetate uptake decreased with increasing pH above pH 7, which disagreed with previous reports that glycogen degradation/acetate increased or was unaffected by increasing pH. The results suggested that the acetate uptake mechanisms of GAM and PAM may be different.


2006 ◽  
Vol 53 (12) ◽  
pp. 29-37 ◽  
Author(s):  
R. Barat ◽  
T. Montoya ◽  
L. Borras ◽  
A. Seco ◽  
J. Ferrer

The role of calcium (Ca) in enhanced biological phosphorus removal and its possible implications on the metabolic pathway have been studied. The experience has been carried out in an SBR under anaerobic–aerobic conditions for biological phosphorus removal during 8 months. The variations of influent Ca concentration showed a clear influence on the EBPR process, detecting significant changes in YPO4. These YPO4 variations were not due to influent P/COD ratio, pH, denitrification and calcium phosphate formation. The YPO4 has been found to be highly dependent on the Ca concentration, increasing as Ca concentration decreases. The results suggest that high Ca concentrations produce “inert” granules of polyphosphate with Ca as a counterion that are not involved in P release and uptake. Furthermore, microbiological observations confirmed that appreciable changes in PAO and GAO populations were not observed. This behaviour could suggest a change in the bacterial metabolic pathway, with prevailing polyphosphate-accumulating metabolism (PAM) at low influent Ca concentration and glycogen-accumulating metabolism (GAM) at high concentration.


2006 ◽  
Vol 41 (1) ◽  
pp. 72-83 ◽  
Author(s):  
Zhe Zhang ◽  
Eric R. Hall

Abstract Parameter estimation and wastewater characterization are crucial for modelling of the membrane enhanced biological phosphorus removal (MEBPR) process. Prior to determining the values of a subset of kinetic and stoichiometric parameters used in ASM No. 2 (ASM2), the carbon, nitrogen and phosphorus fractions of influent wastewater at the University of British Columbia (UBC) pilot plant were characterized. It was found that the UBC wastewater contained fractions of volatile acids (SA), readily fermentable biodegradable COD (SF) and slowly biodegradable COD (XS) that fell within the ASM2 default value ranges. The contents of soluble inert COD (SI) and particulate inert COD (XI) were somewhat higher than ASM2 default values. Mixed liquor samples from pilot-scale MEBPR and conventional enhanced biological phosphorus removal (CEBPR) processes operated under parallel conditions, were then analyzed experimentally to assess the impact of operation in a membrane-assisted mode on the growth yield (YH), decay coefficient (bH) and maximum specific growth rate of heterotrophic biomass (µH). The resulting values for YH, bH and µH were slightly lower for the MEBPR train than for the CEBPR train, but the differences were not statistically significant. It is suggested that MEBPR simulation using ASM2 could be accomplished satisfactorily using parameter values determined for a conventional biological phosphorus removal process, if MEBPR parameter values are not available.


1985 ◽  
Vol 17 (11-12) ◽  
pp. 297-298 ◽  
Author(s):  
Takao Murakami ◽  
Atsushi Miyairi ◽  
Kazuhiro Tanaka

In Japan various biological phosphorus removal processes have recently been researched by laboratory or pilot plant scale studies and most of them have shown good results. Based on these results, the Japan Sewage Works Agency has conducted a full scale study of the biological phosphorus removal process from June 1982 until February 1983, which was the first full scale operation of this process in Japan. The main purpose of the study was to evaluate phosphorus removal efficiency and also nitrogen removal efficiency of the process and in addition, to ascertain the important operating factors of the process. For the study a treatment train of a large scale sewage treatment plant was remodelled. The aeration tank of 3.825 m3 volume was divided into four equal cells. The whole train including return sludge line was operated entirely independently of the other trains. During the experiment the train was operated under two different modes, Mode 1 and Mode 2. In Mode 1, the train was operated as an A/O process, the first cell of the aeration tank being anaerobic and the other cells oxic. In Mode 2, the train was operated as a Modified Phoredox process. In this case, the first cell was anaerobic, but the second cell was anoxic and nitrified liquor was returned to it from the end of the oxic cells. Mode 1 and Mode 2 were further divided into many ‘runs' and the flow rate varied between 12,550 m3 d−1 and 25,270 m3 d−1 , corresponding to retention times of 7.3 hours and 3.6 hours, respectively. Throughout the experimental period the mean value of influent (primary effluent) total-P concentration was 3.38 mg 1−1 , and that of the final effluent was 0.47 mg 1−1 . A cumulated frequency curve of the data showed that about 93% of measured effluent total-P was below 1.0 mg l−1 . Therefore, it can be concluded that with these influent total-P levels, biological phosphorus removal processes can sufficiently satisfy the effluent standard of 1 mg 1−1 total-P. Even when the process was operated as a Modified Phoredox Process, no obstruction to phosphorus removal because of nitrification was observed and phosphorus removal remained good. However, since the sewage treatment plant treated influent from a combined sewerage system, phosphorus removal was sometimes affected by heavy rainfalls. In such cases phosphorus release in the anaerobic cell was insufficient because of increased influent NOx concentration and accordingly increased denitrification level in the anaerobic cell. Therefore, as a result, enhanced phosphorus uptake in the following cells could not be observed. Higher process stability can be expected if an effective countermeasure to high influent NOx concentration can be made. Influence of flow rate fluctuation on the process was also studied. The treatment train was operated for a week under a daily flow rate fluctuation pattern which ranged between 460 m3 hr−1 and 820 m3 hr−1 . Nevertheless, the effluent total-P concentration showed no increase and stayed constantly lower than 0.5 mg 1−1. The oxidation reduction potential (ORP) was an effective control index to evaluate the degree of phosphorus release in the anaerobic cell. Water temperature did not affect phosphorus release and uptake rates.


Sign in / Sign up

Export Citation Format

Share Document