Selector Volume in Pulp and Paper Activated Sludge Wastewater Treatment Plants – Bench Scale and Pilot Plant Studies

1994 ◽  
Vol 29 (5-6) ◽  
pp. 303-311
Author(s):  
J. Wessberg ◽  
T. Welander ◽  
M. Jönsson

Laboratory activated sludge reactors were operated on effluent wastewater from a kraft mill. Two of the three reactors were initially preceded with a “normal” size aerated selector, 2% of the total aerated volume, with unsatisfactory sludge volume index development. When the selectors were replaced by larger ones, 13% of the aerated volume, the sludge volume index could be kept below 50 ml/g for the selector processes while continuing to be higher and more unstable in the reference process. A pilot plant, operated in situ on the same wastewater, showed a comparable improvement in sludge volume index when its selector, 7% of the total volume, was replaced by one that constituted 13% of the total volume, corresponding to a selector load of 3 g BOD / g VSS * d. According to studies of the COD balance around one bench scale selector, the COD removal mechanism in the selector was respiration/assimilation rather than uptake/storage.

1994 ◽  
Vol 29 (7) ◽  
pp. 221-228 ◽  
Author(s):  
R. Pujol ◽  
J. P. Canler

A study of twelve wastewater treatment plants in France confirms the effectiveness of the contact zone technique in controlling sludge bulking (with a reduction in the Sludge Volume Index in 91% of cases) and foaming (improvement of the situation in 75% of the cases). The study focused on low-F/M activated sludge units in which organisms such as Microthrix p. or type 0041 (characteristic of these plants) were identified. Contact zones do not entail any major limitations, a fact which advocates their use in this type of treatment facility. Rational operation of the plant (in terms of aeration and sludge production) and compliance with a few simple rules will ensure effective use of this technology.


2015 ◽  
Vol 73 (6) ◽  
pp. 1333-1340
Author(s):  
Thiemo Dunkel ◽  
Philipe Ambrozio Dias ◽  
Erika Lizette de León Gallegos ◽  
Viola Tacke ◽  
Andreas Schielke ◽  
...  

The present study demonstrates the application of in situ microscopy for monitoring the growth of filamentous bacteria which can induce disturbances in an industrial activated sludge process. An in situ microscope (ISM) is immersed directly into samples of activated sludge with Microthrix parvicella as dominating species. Without needing further preparatory steps, the automatic evaluation of the ISM-images generates two signals: the number of individual filaments per image (ISM–filament counting) and the total extended filament length (TEFL) per image (ISM–online TEFL). In this first version of the image-processing algorithm, closely spaced crossing filament-segments or filaments within bulk material are not detected. The signals show highly linear correlation both with the standard filament index and the TEFL. Correlations were further substantiated by comparison with real-time polymerase chain reaction (real-time PCR) measurements of M. parvicella and of the diluted sludge volume index. In this case study, in situ microscopy proved to be a suitable tool for straightforward online-monitoring of filamentous bacteria in activated sludge systems. With future adaptation of the system to different filament morphologies, including cross-linking filaments, bundles, and attached growth, the system will be applicable to other wastewater treatment plants.


2001 ◽  
Vol 43 (7) ◽  
pp. 91-96 ◽  
Author(s):  
M. da Motta ◽  
M. N. Pons ◽  
N. Roche

An automated procedure for the characterisation by image analysis of the morphology of activated sludge has been used to monitor the biomass in a pilot wastewater treatment plant, in complement to the usual settleability (sludge volume index, settling velocity) and size distribution (by laser granulometry) measurements.


1988 ◽  
Vol 20 (2) ◽  
pp. 143-152 ◽  
Author(s):  
A. Langi ◽  
M. Priha

The mutagenic properties of pulp and paper mill effluents were studied in three mills: bleached kraft mill with aerated lagoon treatment (Mill 1), bleached kraft mill with activated sludge treatment (Mill 2) and mechanical pulp/paper mill (Mill 3). Both treated and untreated effluents, process streams and molecular fractions were tested for mutagenicity (Ames test. Salmonella typhimurium TA100 and SCE sister chromatid exchange test, Chinese hamster ovary cells). To verify the potential environmental effects the mutagenic activity of concentrated recipient lake water (Mill 2) was also studied. The Ames mutagenicity of the bleached kraft mill effluent (BKME) originated from the first chlorination filtrate, SCE mutagenicity also occurred in the alkali extraction stage filtrate (Mill 1). No Ames mutagenicity was detected in the paper mill effluent, but it was SCE mutagenic. Activated sludge treatment of BKME removed both Ames and SCE mutagenicity, but the aerated lagoon treated BKME was still SCE mutagenic. No mutagenic activity was detected in the recipient water concentrates.


1997 ◽  
Vol 36 (4) ◽  
pp. 307-312
Author(s):  
Michael R. Rasmussen ◽  
Torben Larsen

An on-line settling column for measuring the dynamic variations of settling velocity of activated sludge has been developed. The settling column is automatic and self-cleansing insuring continuous and reliable measurements. The settling column was tested on sludge from a batch reactor where sucrose was added as an impulse to activated sludge. The continuous measurement of settling velocity revealed a highly dynamic response after the sucrose was added. The results were verified with simultaneous measurement of the initial settling rate. A 200 hour experiment showed variations in settling velocity, which was not apparent in the DSVI (Diluted Sludge Volume Index).


1999 ◽  
Vol 40 (11-12) ◽  
pp. 223-229 ◽  
Author(s):  
Frédéric Clauss ◽  
Christel Balavoine ◽  
Delphine Hélaine ◽  
Gaëtan Martin

Forest industry wastewaters are difficult to clean: hydraulic and organic load variations, filamentous bulking or pin-point flocs negatively impact depollution processes. The addition of a fine, mineral, talc-based powder, Aquatal, into the aeration tanks of wastewater treatment plants connected to pulp and paper factories has been successfully tested since end of '97. The first case-study presents full results obtained over a period of 18 months in a 20,000 p.e. plant connected to a paper factory. The mineral powder was regularly added to control sludge volume index, thereby ensuring low suspended solids concentration in the outfluent. Plant operators could easily adapt biomass concentration to match organic load variation, thereby maintaining pollution micro-organisms ratio constant. In a second case study, a trouble-shooting strategy was implemented to counteract filamentous bulking. A one-off, large dosage enabled the plant operator to deal effectively with poor settleability sludge and rapidly control sludge blanket expansion. In both cases, the main common characteristics observed were an increase in floc aggregation and the production of heavier and well-structured flocs. The sludge settling velocity increased and an efficient solid/liquid separation was obtained. After a few days, the mineral particles of Aquatal were progressively integrated into the sludge floc structure. When the mineral powder was added to the activated sludge in the aeration basin, chemical interactions frequently encountered with other wastewater treatment additives did not pose a problem. Moreover, with this mineral additive, the biological excess sludge displayed good thickening properties and dewatering was improved. Despite the addition of the insoluble mineral particles, the amount of wet sludge expelled did not increase. Aquatal offers a rapid solution to floc settleability problems which so frequently arise when physical or biological disorders appear in forest industry wastewater treatment plants.


2003 ◽  
Vol 47 (11) ◽  
pp. 85-92 ◽  
Author(s):  
E. Cotteux ◽  
P. Duchene

The bulking that occurs in biological wastewater treatment plants using activated sludge is very often controlled by the injection of sodium hypochlorite into the return activated sludge (RAS) stream. In the present study undertaken at two pilot plants fed with synthetic wastewater, the impact of the pass frequency of the sludge at the chlorine dosing point on the nitrifying flora is analysed. The pass frequency is one for the pilot plant 1 and two for the pilot plant 2. A dose of chlorine of 4.85 ± 0.05 g/kg/MLVSS per day was applied at both pilots. The preservative effect on nitrifying activity of the lowest concentration of chlorine at the dosing point and therefore of the highest pass frequency was evidenced. Among other tools, a simple method of measurement of the oxygen uptake rate enabled us to monitor the effect of chlorination on nitrification before recording an increase in the ammonia concentration in the bulking.


1994 ◽  
Vol 30 (4) ◽  
pp. 181-190 ◽  
Author(s):  
René Dupont ◽  
Ole Sinkjær

The objective of the work presented is to demonstrate how computer based models can be used to improve the effluent quality from wastewater treatment plants by optimisation of the operation. The investigation was carried out in connection with pilot plant investigations at Damhusllen Wastewater Treatment Plant in order to establish the design basis for upgrading the treatment plants in the city of Copenhagen. Calibration of the model was done with thorough characterisation of the wastewater and the activated sludge as the primary calibration tool. Special attention was paid to the nitrification process, which by previous investigations was shown to be occasionally inhibited. Model constants for the nitrification process were detennined from experiments. Default constants were used for nearly all other constants. The pilot plant was optimized with the calibrated model. Different operational strategies for improvement of the denitrification process were tested. The denitrification process was operated relatively poorly at the time for the optimisation. The calibration showed that it was possible to calibrate the model using the characterization of the wastewater and the activated sludge as the primary calibration tool. Further it was shown that the calihrated model could be used as a tool for optimising the operation of the pilot plant. The suggested operation correlated well with the practical realisable operation.


1994 ◽  
Vol 29 (7) ◽  
pp. 157-165 ◽  
Author(s):  
Gert Holm Kristensen ◽  
Per Elberg Jørgensen ◽  
Per Halkjær Nielsen

In 1989-91, a study was performed to investigate the settling characteristics of activated sludge in Danish treatment plants with biological nutrient removal. The study included three screening series on 38 treatment plants. Furthermore, the study included investigations during one year on seasonal variations in sludge settling characteristics at three treatment plants. The screening investigations were performed in November 1989 and May and September, 1990. Results showed that in the May-screening, 35-45% of the plants had a filament index of 2-2.5 or above, corresponding to a sludge volume index above 150 ml/g. When comparing data for diluted and non-diluted sludge volume indices, a SVI value of 150 ml/g seemed parallel to a DSVI of 110 ml/g. In the November- and September-screenings, some 30% of the plants had activated sludge showing a filament index in or above the critical area. Dominating filamentous microorganisms were found to be (in decreasing order): Microthrix parvicella, Type 0041, Type 021N, Type 0092, Type 0914, and Type 1851. A distinct variation over the year in sludge settling characteristics was found for the three plants. Sludge settling characteristics improved during summer, and deteriorated during winter. For activated sludge with a high content of filamentous microorganisms, the best parameter to follow the variations in sludge settling properties was the filament number. If the activated sludge concentration, the MLSS, varied significantly, the specific filament number was to be applied.


2018 ◽  
Vol 78 (10) ◽  
pp. 2104-2112
Author(s):  
Mateusz Sobczyk ◽  
Agnieszka Pajdak-Stós ◽  
Edyta Fiałkowska ◽  
Wioleta Kocerba-Soroka ◽  
Joanna Starzycka-Giża ◽  
...  

Abstract Biological microscopic analysis is a popular method employed in wastewater treatment plants worldwide for evaluating activated sludge condition. However, many operators still have reservations regarding its reliability. In this study, we evaluated and compared two methods of microscopic sludge investigation: the sludge index (SI) and the Eikelboom–van Buijsen method (EB). We investigated 79 activated sludge samples from nine treatment plants located in southern Poland over a 1-year period. For each sample, sludge volume index values were calculated and compared with the results of evaluation made on the basis of microscopic analysis. Additionally, the effluent quality was analysed in 45 of 79 cases, including investigation of suspended solids, biochemical oxygen demand, chemical oxygen demand, total nitrogen and total phosphorous. The sign test and Wilcoxon matched pairs test showed that a significant difference existed between the two investigated methods. General conclusions from both methods do not provide reliable information concerning nitrogen and phosphorus removal. The EB method had a tendency to be more conservative in its general conclusions than the SI method. Both are highly reliable for estimating activated sludge quality and solid separation properties.


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