Anaerobic Digestion of Floral Waste and Methane Enrichment: A Sustainable Approach for Waste to Energy Conversion

2020 ◽  
Vol 46 (3) ◽  
pp. 299-303
Author(s):  
Kulkarni Milind B. ◽  
P.M. Ghanegaonkar

Disposal of floral waste into water or landfill because of religious beliefs causes water and soil pollution. The purpose of present experimental work is to find an energy proficient solution for the disposal of floral waste. The method used in the present work includes anaerobic digestion of floral waste for biogas generation. The proposed method aims to follow waste-to-energy approach, for meeting the local energy demands. The techniques for getting enhanced biogas production from floral waste include novel alkaline chemical pretreatment of floral waste, and co-digestion of floral waste along with food waste. Alkaline chemical pretreatment of floral waste using sodium carbonate showed improved biogas production up to 106%, as compared to the traditional sodium hydroxide chemical pretreatment. Also, a reduction in the cost of chemical pretreatment up to 90% was possible. Co-digestion of floral waste along with food waste was also found effective for getting enhanced biogas output. A feedstock mixture of 70% of floral waste and 30% food waste could produce 32.6% more biogas than the singular feedstock in the form of floral waste. Alkaline pretreatment of floral waste using sodium carbonate and co-digestion with food waste seem to be the novelty of the work. Application of chemical absorption technique for biogas quality improvement could enrich the methane content of biogas up to 96%. Large-scale application of the proposed techniques of solid waste management can meet the energy demands at potential locations. The biogas with enriched methane content can suitable for widespread applications, such as vehicular applications and electricity generation for the benefit of the end users.

2003 ◽  
Vol 48 (4) ◽  
pp. 169-174 ◽  
Author(s):  
J.-Y. Wang ◽  
H.-L. Xu ◽  
H. Zhang ◽  
J.-H. Tay

A hybrid anaerobic solid-liquid (HASL) bioreactor was developed to enhance food waste conversion. The HASL bioreactor is a modified two-phase anaerobic digestion system with a solid waste reactor and a high-rate anaerobic wastewater reactor, which was a UASB reactor. In this study, the methanogenesis in the UASB reactor was investigated under a semi-continuous operation of the food waste digestion system. The HASL process, including 7 days of start-up and 23 days of semi-continuous operation followed by 6 days of batch operation, was commenced by loading 2.8 kg of shredded food waste. During the semi-continuous operation, 0.2 kg of the same waste was loaded daily. The leachate from acidification phase, i.e., solid waste reactor, remained acidic (pH 4.9-5.5) and high in total VFA (TVFA), 9,500-11,500 mg/L, and COD (8,000-11,800 mg/L) levels. In the methanogenesis phase, i.e., UASB reactor, effective TVFA and COD removals (88 ± 5% and 85 ± 7%, respectively) were obtained, while the methane content was 71%. At the end of operation, about 78% of VS added in the HASL bioreactor was removed, while TOC and total COD reductions were 78% and 79%, respectively. The results showed that the use of UASB reactor in the semi-continuous HASL system can enhance the methanogenesis process and increase the methane content in biogas production.


2016 ◽  
Vol 832 ◽  
pp. 55-62
Author(s):  
Ján Gaduš ◽  
Tomáš Giertl ◽  
Viera Kažimírová

In the paper experiments and theory of biogas production using industrial waste from paper production as a co-substrate are described. The main aim of the experiments was to evaluate the sensitivity and applicability of the biochemical conversion using the anaerobic digestion of the mixed biomass in the pilot fermentor (5 m3), where the mesophillic temperature was maintained. It was in parallel operation with a large scale fermentor (100 m3). The research was carried out at the biogas plant in Kolíňany, which is a demonstration facility of the Slovak University of Agriculture in Nitra. The experiments proved that the waste arising from the paper production can be used in case of its appropriate dosing as an input substrate for biogas production, and thus it can improve the economic balance of the biogas plant.


2021 ◽  
Vol 14 (1) ◽  
Author(s):  
Karol Postawa ◽  
Jerzy Szczygieł ◽  
Marek Kułażyński

Abstract Background Increasing the efficiency of the biogas production process is possible by modifying the technological installations of the biogas plant. In this study, specific solutions based on a mathematical model that lead to favorable results were proposed. Three configurations were considered: classical anaerobic digestion (AD) and its two modifications, two-phase AD (TPAD) and autogenerative high-pressure digestion (AHPD). The model has been validated based on measurements from a biogas plant located in Poland. Afterward, the TPAD and AHPD concepts were numerically tested for the same volume and feeding conditions. Results The TPAD system increased the overall biogas production from 9.06 to 9.59%, depending on the feedstock composition, while the content of methane was slightly lower in the whole production chain. On the other hand, the AHPD provided the best purity of the produced fuel, in which a methane content value of 82.13% was reached. At the same time, the overpressure leads to a decrease of around 7.5% in the volumetric production efficiency. The study indicated that the dilution of maize silage with pig manure, instead of water, can have significant benefits in the selected configurations. The content of pig slurry strengthens the impact of the selected process modifications—in the first case, by increasing the production efficiency, and in the second, by improving the methane content in the biogas. Conclusions The proposed mathematical model of the AD process proved to be a valuable tool for the description and design of biogas plant. The analysis shows that the overall impact of the presented process modifications is mutually opposite. The feedstock composition has a moderate and unsteady impact on the production profile, in the tested modifications. The dilution with pig manure, instead of water, leads to a slightly better efficiency in the classical configuration. For the TPAD process, the trend is very similar, but the AHPD biogas plant indicates a reverse tendency. Overall, the recommendation from this article is to use the AHPD concept if the composition of the biogas is the most important. In the case in which the performance is the most important factor, it is favorable to use the TPAD configuration.


Author(s):  
Kai Schumüller ◽  
Dirk Weichgrebe ◽  
Stephan Köster

AbstractTo tap the organic waste generated onboard cruise ships is a very promising approach to reduce their adverse impact on the maritime environment. Biogas produced by means of onboard anaerobic digestion offers a complementary energy source for ships’ operation. This report comprises a detailed presentation of the results gained from comprehensive investigations on the gas yield from onboard substrates such as food waste, sewage sludge and screening solids. Each person onboard generates a total average of about 9 kg of organic waste per day. The performed analyses of substrates and anaerobic digestion tests revealed an accumulated methane yield of around 159 L per person per day. The anaerobic co-digestion of sewage sludge and food waste (50:50 VS) emerged as particularly effective and led to an increased biogas yield by 24%, compared to the mono-fermentation. In the best case, onboard biogas production can provide an energetic output of 82 W/P, on average covering 3.3 to 4.1% of the total energy demand of a cruise ship.


Energies ◽  
2020 ◽  
Vol 13 (9) ◽  
pp. 2392 ◽  
Author(s):  
Marcin Dębowski ◽  
Marcin Zieliński ◽  
Marta Kisielewska ◽  
Joanna Kazimierowicz

The aim of this study was the performance evaluation of anaerobic digestion of dairy wastewater in a multi-section horizontal flow reactor (HFAR) equipped with microwave and ultrasonic generators to stimulate biochemical processes. The effects of increasing organic loading rate (OLR) ranging from 1.0 g chemical oxygen demand (COD)/L·d to 4.0 g COD/L·d on treatment performance, biogas production, and percentage of methane yield were determined. The highest organic compounds removals (about 85% as COD and total organic carbon—TOC) were obtained at OLR of 1.0–2.0 g COD/L·d. The highest biogas yield of 0.33 ± 0.03 L/g COD removed and methane content in biogas of 68.1 ± 5.8% were recorded at OLR of 1.0 g COD/L·d, while at OLR of 2.0 g COD/L·d it was 0.31 ± 0.02 L/COD removed and 66.3 ± 5.7%, respectively. Increasing of the OLR led to a reduction in biogas productivity as well as a decrease in methane content in biogas. The best technological effects were recorded in series with an operating mode of ultrasonic generators of 2 min work/28 min break. More intensive sonication reduced the efficiency of anaerobic digestion of dairy wastewater as well as biogas production. A low nutrient removal efficiency was observed in all tested series of the experiment, which ranged from 2.04 ± 0.38 to 4.59 ± 0.68% for phosphorus and from 9.67 ± 3.36 to 20.36 ± 0.32% for nitrogen. The effects obtained in the study (referring to the efficiency of wastewater treatment, biogas production, as well as to the results of economic analysis) proved that the HFAR can be competitive to existing industrial technologies for food wastewater treatment.


Processes ◽  
2020 ◽  
Vol 8 (11) ◽  
pp. 1487
Author(s):  
Vicky De Groof ◽  
Marta Coma ◽  
Tom C. Arnot ◽  
David J. Leak ◽  
Ana B. Lanham

Production of medium chain carboxylic acids (MCCA) as renewable feedstock bio-chemicals, from food waste (FW), requires complicated reactor configurations and supplementation of chemicals to achieve product selectivity. This study evaluated the manipulation of organic loading rate in an un-supplemented, single stage stirred tank reactor to steer an anaerobic digestion (AD) microbiome towards acidogenic fermentation (AF), and thence to chain elongation. Increasing substrate availability by switching to a FW feedstock with a higher COD stimulated chain elongation. The MCCA species n-caproic (10.1 ± 1.7 g L−1) and n-caprylic (2.9 ± 0.8 g L−1) acid were produced at concentrations comparable to more complex reactor set-ups. As a result, of the adjusted operating strategy, a more specialised microbiome developed containing several MCCA-producing bacteria, lactic acid-producing Olsenella spp. and hydrogenotrophic methanogens. By contrast, in an AD reactor that was operated in parallel to produce biogas, the retention times had to be doubled when fed with the high-COD FW to maintain biogas production. The AD microbiome comprised a diverse mixture of hydrolytic and acidogenic bacteria, and acetoclastic methanogens. The results suggest that manipulation of organic loading rate and food-to-microorganism ratio may be used as an operating strategy to direct an AD microbiome towards AF, and to stimulate chain elongation in FW fermentation, using a simple, un-supplemented stirred tank set-up. This outcome provides the opportunity to repurpose existing AD assets operating on food waste for biogas production, to produce potentially higher value MCCA products, via simple manipulation of the feeding strategy.


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