Multi-Purpose Fuel: Problems That We Face
A Pratt and Whitney FT4A Marine Gas Turbine Engine rated at 25,000 HP for a 100°F inlet day, was tested at the Naval Ship Engineering Center Philadelphia Division for a total of 201 hours, 15 minutes. The engine was subjected to an initial 30 hour “coking” run, conducted at 10,000 HP, 2380 rpm, to determine adverse effects on the engine under simulated destroyer type operation. Following the 30 hour coking run, the engine was subjected to a 150 hour cycle endurance operation. Salt was admitted to the inlet air. A combustion section inspection was performed at the end of the 30 hour coking run. No detrimental effects were noted at that time. An overall combustion section inspection was performed at the end of the test. A fuel manifold and nozzle spray check was performed with both acceptable for further use. First stage turbine blades showed some degree of sulfidation, while the nozzle guide vanes showed evidence of coating loss and partial penetration into the base metal (on only the uncoated vanes). The major problem area during the test was the failure of the coalescer fuel filter to function properly with Multi-Purpose fuel. Due to the higher pour point (with attendant “wax” precipitation) of the fuel in comparison with normal Marine Diesel (MIL-F-16884), plugging of the coalescer filter elements occurred in a very short period of time. Engine performance over the entire test was satisfactory approximating that of previous FT4A testing.