Multiscale Formation Damage Mechanisms and Control Technology for Deep Tight Clastic Gas Reservoirs

SPE Journal ◽  
2021 ◽  
pp. 1-16
Author(s):  
Yijun Wang ◽  
Yili Kang ◽  
Lijun You ◽  
Chengyuan Xu ◽  
Xiaopeng Yan ◽  
...  

Summary Severe formation damage often occurs during the drilling process, which significantly impedes the timely discovery, accurate evaluation, and efficient development of deep tight clastic gas reservoirs. The addition of formation protection additives into drilling fluid after diagnosing the damage mechanism is the most popular technique for formation damage control (FDC). However, the implementation of traditional FDC measures does not consider the multiscale damage characteristics of the reservoir. The present study aims at filling this gap by providing a complete and systematic damage control methodology based on multiscale FDC theory. First, the characteristics of multiscale seepage channels were described through petrology, petrophysics, and well-history data. Subsequently, based on laboratory formation damage evaluation experiments, the formation damage mechanism of each seepage scale was determined. Finally, based on the multiscale formation damage mechanism, a systematic multiscale FDC technology was proposed. Through the use of optimized drilling fluid based on multiscale FDC theory, high-permeability recovery ratio (PRR), high-pressure bearing capacity of plugging zone, and low cumulative filtration loss were observed by laboratory validation experiments. Shorter drilling cycle, less drill-in-fluid loss, lower skin factor, and higher production rates were obtained by using the optimized FDC drilling fluid in field application. This multiscale FDC theory shows excellent results in minimizing formation damage, maintaining original production capacity, and effectively developing gas reservoirs with multiscale pore structure characteristics.

Geofluids ◽  
2019 ◽  
Vol 2019 ◽  
pp. 1-15 ◽  
Author(s):  
Peng Xu ◽  
Mingbiao Xu

Oil-based drilling fluids (OBDFs) have a strong wellbore stabilization effect, but little attention has been paid to the formation damage caused by oil-based drilling fluids based on traditional knowledge, which is a problem that must be solved prior to the application of oil-based drilling fluid. For ultradeep fractured tight sandstone gas reservoirs, the reservoir damage caused by oil-based drilling fluids is worthy of additional research. In this paper, the potential damage factors of oil-based drilling fluids and fractured tight sandstone formations are analyzed theoretically and experimentally. The damage mechanism of oil-based drilling fluids for fractured tight sandstone gas reservoirs is analyzed based on the characteristics of multiphase fluids in seepage channels, the physical and chemical changes of rocks, and the rheological stability of oil-based drilling fluids. Based on the damage mechanism of oil-based drilling fluids, the key problems that must be solved during the damage control of oil-based drilling fluids are analyzed, a detailed description of formation damage characteristics is made, and how to accurately and rapidly form plugging zones is addressed. This research on damage control can provide a reference for solving the damage problems caused by oil-based drilling fluids in fractured tight sandstone gas reservoirs.


2018 ◽  
Vol 5 (7) ◽  
pp. 180358 ◽  
Author(s):  
Peng Xu ◽  
Mingbiao Xu ◽  
Zhengwu Tao ◽  
Zhihong Wang ◽  
Ting Huang

The great amount of solid particles contained in a weighting agent is a major cause of the problems in both rheology properties and damage control mechanism of an oil-based drilling fluid (OBM). Therefore, a proper type of weighting agent can be a solution for the application of OBM. In this study, three weighting agents that have been commonly used with OBM, namely, standard barite, submicron barite and superfine manganese ore, are studied. Rheological properties of OBM and the degree of formation damage are assessed with regard to the three weighting agents. The agents are also studied in aspects of particle size, micromorphology, filtration loss and wall-building property, acid dissolution efficiency of mud cake, lubricity and sedimentation stability to analyse the effects of the agents on rheological properties and the degree of damage as well as to figure out the mechanism of rheology control and damage control. For the OBM, there is a mutual effect between rheological stability and the degree of damage. In consideration of the agents' properties, we can enhance the rheological stability of the OBM and control the degree of formation damage by properly selecting particle size, using acid-soluble materials and forming the mud cake with ultra-low permeability that can easily be cleared away.


2021 ◽  
Author(s):  
Karl Ronny Klungtvedt ◽  
Mahmoud Khalifeh ◽  
Arild Saasen ◽  
Bjørn Berglind ◽  
Jan Kristian Vasshus

Abstract During drilling of permeable reservoirs, drilling fluid may penetrate the formation and induce damage to the reservoir rock. Specifically, solids present in the drilling fluid may enter the formation and cause subsequent reduction in reservoir permeability in the area near the wellbore. When drilling with a water-based drilling fluid in a reservoir, various polymer-based additives are normally applied to reduce the filtration loss. These additives, such as Xanthan Gum, Poly Anionic Cellulose (PAC) and Starch may help in reducing losses to the formation in presence of small pore-throats and low differential pressures. If the pore throats exceed e.g. 20μm and differential pressures reach 500psi, these additives have little effect on reducing loss of drilling fluid to the formation and thereby little effect in preventing solids from entering the formation. Lost circulation is particularly challenging when losses occur in the reservoir section. This is because LCM treatment may create formation damages. Green et al. (SPE-185889) showed the nature of drilling fluid invasion, clean-up, and retention during reservoir formation drilling. They also showed the lack of direct relation between fluid loss and formation damage. In light of such ideas, a development of new Non-Invasive Fluid (NIF) additives was conducted. These additives were able to handle downhole pressure differences and create a preventative sealing of a permeable formation when applied into a solids-free drilling fluid. Ceramic discs of various permeability and mean pore-throat size were installed into a HTHP pressure cell. Drilling fluid was pumped through the cell and a filter cake was formed across the ceramic disc. A pressure of 500psi was applied and filtration loss was measured over a 30-minute period. Examples are herein presented showing how filter cake materials were applied into the drilling fluid and effectively sealing the permeable surface of the ceramic disc. Also, it will be shown how the filter cake was effectively removed from the discs using a breaker solution. Furthermore, a selection of experiments is presented, showing the possibility to heal lost circulation in permeable reservoirs without the presence of weighing materials, clays or drill-solids in the drilling fluid. A test was also conducted in such a way that the disc was fractured inside the test cell to investigate the impact on fluid loss.


Author(s):  
Erfan Veisi ◽  
Mastaneh Hajipour ◽  
Ebrahim Biniaz Delijani

Cooling the drill bit is one of the major functions of drilling fluids, especially in high temperature deep drilling operations. Designing stable drilling fluids with proper thermal properties is a great challenge. Identifying appropriate additives for the drilling fluid can mitigate drill-bit erosion or deformation caused by induced thermal stress. The unique advantages of nanoparticles may enhance thermal characteristics of drilling fluids. The impacts of nanoparticles on the specific heat capacity, thermal conductivity, rheological, and filtration control characteristics of water‐based drilling fluids were experimentally investigated and compared in this study. Al2O3, CuO, and Cu nanoparticles were used to prepare the water-based drilling nanofluid samples with various concentrations, using the two-step method. Transmission Electron Microscopy (TEM) and X-Ray Diffraction (XRD) were utilized to study the nanoparticle samples. The nanofluids stability and particle size distribution were, furthermore, examined using Dynamic Light Scattering (DLS). The experimental results indicated that thermal and rheological characteristics are enhanced in the presence of nanoparticles. The best enhancement in drilling fluid heat capacity and thermal conductivity was obtained as 15.6% and 12%, respectively by adding 0.9 wt% Cu nanoparticles. Furthermore, significant improvement was observed in the rheological characteristics such as the apparent and plastic viscosities, yield point, and gel strength of the drilling nanofluids compared to the base drilling fluid. Addition of nanoparticles resulted in reduced fluid loss and formation damage. The permeability of filter cakes decreased with increasing the nanoparticles concentration, but no significant effect in filter cake thickness was observed. The results reveal that the application of nanoparticles may reduce drill-bit replacement costs by improving the thermal and drilling fluid rheological characteristics and decrease the formation damage due to mud filtrate invasion.


2021 ◽  
Vol 11 (4) ◽  
pp. 1715-1726
Author(s):  
Ved Prakash ◽  
Neetu Sharma ◽  
Munmun Bhattacharya ◽  
Ashok Raina ◽  
Man Mohan Gusain ◽  
...  

AbstractThis work investigates the efficacy of a biodegradable natural product, litchi leaves powder (LLP) as a filtration loss control agent in the water-based drilling fluid formulations. In order to evaluate the potential of litchi leaves powder (LLP), a strict protocol of experimentations according to API (American Petroleum Institute) standard has been followed. The experimental outcome showed that before hot rolling and after hot rolling of mud samples at 100 °C it was observed that 3–5% Concentration of LLP significantly increased the rheological parameters such as PV, YP and gelation of drilling fluid as compared to reference mud. Also, LLP reformed the filtration loss control characterization, suggesting a better biodegradable fluid loss reducing agent. After hot rolling at 100 °C for 18 h, the water-based drilling fluid with LLP as an additive showed a marked reduction in filtration control property as compared to reference Mud (RM). Experimental results concluded that 5% concentration of LLP significantly reduced the filtration loss of drilling fluid by 70.6% as compared to reference mud under the influence of 100 psi pressure. However, the conventional fluid loss additive CMC (LVG) reduced the filtration loss by maximum 67.5% as compared to reference mud. Therefore, LLP can be used as an alternative to CMC (LVG) in water-based drilling fluid with a maximum subsurface temperature of 100 °C.


2019 ◽  
Vol 10 (4) ◽  
pp. 1643-1655 ◽  
Author(s):  
Abdulrauf R. Adebayo ◽  
Badr S. Bageri

Abstract An efficient drilling fluid will form a filter cake that will minimize the drilling fluid invasion into any drilled formation. Drilling fluid must therefore be adequately evaluated in the laboratory prior to field trial. Filter cake properties such as thickness, porosity, permeability, and pore structure are frequently evaluated using several techniques such as CT scan, SEM, and XRF. However, each of these techniques can evaluate only one or two filter cake properties. This paper presents a simple but novel NMR technique to evaluate filter cake properties such as thickness, pore volume, porosity, and possibly permeability. Furthermore, the amount and particle size distribution of solids that invaded a given rock sample can be obtained using the same technique. The full procedure was tested and verified using four identical rock samples. Drilling fluid invasion and filter cake deposition experiments were conducted on each of the samples, using the same drilling fluid but four different concentrations of fluid loss additive. NMR T2 relaxation measurements were taken at three different stages of each rock sample: before filter cake deposition; after fluid invasion and filter cake deposition; and after filter cake removal. A material balance analysis of the probability density function and cumulative distribution function of the measured T2 profile at the different stages of each sample yielded multiple filtration loss properties of the filter cake. The results obtained showed high accuracy of the NMR versus the current techniques. Moreover, this current method evaluated the majority of the filter cake properties at the same time and in situ hence eliminated the need of using multi-procedures that disturb the sample state. Finally, the presented method can also be used to evaluate secondary damage associated with filter cake removal process.


2017 ◽  
Vol 139 (2) ◽  
Author(s):  
C. P. Ezeakacha ◽  
S. Salehi ◽  
A. Hayatdavoudi

In real time drilling, the complexity of drilling fluid filtration is majorly attributed to changing mud rheology, formation permeability, mud particle size distribution (PSD), filter cake plastering effects, and geochemical reaction of particles at geothermal conditions. This paper focuses on quantifying the major effects as well as revealing their contribution toward effective wellbore stabilization in sandstone formations. We conducted an extensive experimental and analytical study on this subject at different levels. First, we used field application and the results as guides for our experiments. We have considered both oil-based mud and water-based mud. Next, we optimized the mud particle size distribution (PSD) by carefully varying the type, size, and concentration of wellbore strengthening material (WSM). Laboratory high pressure high temperature fluid loss tests were carried out on Michigan and Bandera Brown sandstones. The results from these tests identify the formation heterogeneity and permeability in successful wellbore stabilization. Filter cake permeability calculations, using the analytical model for linear systems, were consistent with filtration rates, and the expected trend of permeability declines with time. Finally, we investigated the evolution of internal filter cake and plastering mechanism, using scanning electron microscopic (SEM) analysis. The test results revealed a significant difference in the formation permeability impairment for the optimal mud PSD and WSM blend.


2011 ◽  
Vol 361-363 ◽  
pp. 461-464
Author(s):  
Ming Zhang ◽  
Tian Tai Li ◽  
Xi Feng Zhang

High density brine drilling fluid has been widely applied in the high pressure and complex oil and gas fields. Effectively controlling high density brine drilling fluid loss is an important factor for reducing the reservoir damage and keeping well stability. Base on general drilling fluid formulations,the affecting factors of filtrate loss of high density brine drilling fluid were analysed through mass laboratory experiments. The results show that the main fctor was the content of caustic soda and bentonite, secondly the density and the shape of adding product. The combination of adding product is one of effective method to control the filtration property of high density brine drilling fluid. The results will provide reliable foundation for successful field application.


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