scholarly journals The Well Control Equipment of Tarim Oil Field Surpressure Gas Well

Author(s):  
Kaihong Zhou ◽  
Hongji Fang ◽  
Bo Fan
2021 ◽  
Author(s):  
Rishabh Bharadwaj ◽  
Bhavya Kumari ◽  
Astha Patel

Abstract E&P activities are the early stage of energy production and pivotal for generating and sustaining economic growth. However, negligence and evaluating the circumstances incorrectly during these operations can lead to calamities like blowouts. This paper discusses two such tragedies, the Pasarlapudi (Krishna-Godavari) Gas Well Blowout of 1995 & Baghjan (Assam-Arakan) Oil Field Blowout of 2020, and provides possible well control measures and lessons learned. Pasarlapudi blowout incident occurred during the drilling operations. The pipe stuck-up situation at 2727m MD (Measured Depth) was detected by conducting a stretch test. Further analysis could include circulating brine, checking lost circulation and identifying casing leaks by measuring Sustained Casing Pressure (SCP), Operator-imposed Pressure (OIP), and Thermal-induced Pressure (TIP). Baghjan's gas well at the depth 3870m was producing at 2.8-3.5 MMSCFD. The aim was to plug the lower producing zone and recomplete the well in the upper Lakadong+Therria sand zone. Well was killed using brine, cement plug was placed and BOP installed. BOP was removed after the plug was set to begin the process of moving the workover rig. Well blew gas profusely during this process. Simulating a blowout and facing one, are two completely different situations. In Pasarlapudi's case, the well blew with an enormous gas pressure of 281.2 ± 0.5 kg/cm2. While drilling the production hole (8.5 inch), either differential pressure sticking, presence of water-swelling clay formation or the partial collapse of wellbore formation caused the pipe stuck-up situation. By conducting stretch test along with circulating brine, root cause of this problem could be identified. If differential sticking occurred, lost circulation could be checked & cured, while keeping the hole full. Circulating brine should solve the problem of swelling clay formation while formation collapse could have occurred due to the presence of plastic formation like salt domes. In the case of Baghjan gas well blowout during workover operations, probable safety measures could include placement of 2 or 3 backup cement plugs along with kill fluid or going for squeeze cementing before placing the cement plug & kill fluid while abandoning the lower producing zone. Attempts were made to bring the well under control by adequate water spraying, installing BOP. Water was pumped through the casing valve and a water reservoir was dug near the well plinth for the placement of pumps of 2500 gallon capacity. Proper safety measures should be used even when they're not the cheapest to avoid repetition of treatments and detrimental situations. SCP, OIP and TIP should be measured periodically whenever possible and the root cause of situations like lost circulation, pipe stuck-ups, kicks, casing leaks should be identified before proceeding towards drastic remedial operations. Innovations in countering well-control situations should be promoted invariably.


SPE Journal ◽  
2016 ◽  
Vol 21 (04) ◽  
pp. 1470-1476 ◽  
Author(s):  
Ebrahim Hajidavalloo ◽  
Saeed Alidadi Dehkohneh

Summary When a blowout oil/gas well catches fire, usually a flow tube is used to detach the fire from the wellhead and provide appropriate conditions for operating team members to approach the well and install the blowout-preventer (BOP) cap. Using the flow tube above the wellhead creates powerful suction around the tube that may jeopardize the safety of crew members. To reduce the power of suction around the well, a new perforated flow tube instead of simple flow tube was introduced. To understand the effect of this new type of flow tube, modeling and simulation of the flow field around the blowout well were performed for both simple and perforated types of flow tube with Fluent 6.3.26 (2003) and Gambit 2.3.16 (2003) softwares. Different parameters around the well mouth were compared in both designs. The results showed that using the perforated flow tube decreases the vacuum around the well by 33% compared with the simple flow tubes. Thus, application of the perforated flow tube can be recommended in well-control operations for safety measures.


2014 ◽  
Vol 997 ◽  
pp. 713-716
Author(s):  
Pu Liu ◽  
Hu Yin ◽  
Tian Xiang Wang ◽  
Meng Han Si

With narrow Density Windows wells and high pressure oil and gas well drilling growing in number, the kick risks becoming increasingly prominent and higher requirements for well control technology being needed, the manage pressure drilling (MPD) technology is used more and more widely. The problems like how to effectively find gas overflowand how to effectively control the overflow in the MPD must be solved.Well must be shuted timely in conventional drilling when overflow happens.The special characteristics of overflow control equipment determines the diversity and effectiveness of its overflow monitoring means in MPD, and the overflow is found more effectively and timely than conventional drilling. Well control risk will increase sharply if kick cannot be timely and effectively identified and controled when overflow occurs. MPD can quickly adjust the wellhead back pressure and inhibit the formation fluid further invasion. Therefore, combining with MPD process and the fluid pressure parameters, the article establishs process of kick recognition and kick control, analyses of the process and analyzes and evaluates the pressure response in process of kick control.MPD can better control the bottom hole pressure in well control situation, ensuring drilling safety. The process of kick recognition and control is of great significance to promote the development and application of kick control technology in MPD.


2019 ◽  
Author(s):  
Leandro Diniz Brandão Rocha ◽  
José Eugênio de Almeida Campos ◽  
Cristiano Venâncio Xavier ◽  
Thijs Visser ◽  
Felipe Freitas ◽  
...  

1985 ◽  
Vol 1985 (1) ◽  
pp. 311-313 ◽  
Author(s):  
S. D. Gill ◽  
C. A. Bonke ◽  
J. Carter

ABSTRACT During the evening of February 22, 1984, the Uniacke G-72 gas well being drilled 150 nautical miles off Halifax, Nova Scotia, by the semisubmersible drilling rig, Vinland, under contract to Shell Canada Resources, blew out of control, emitting gas and condensate at an estimated rate of 300 bbl per day. During the following 10 days while Shell was assembling personnel, vessels, and equipment for reboarding the rig and initiating well control procedures, a comprehensive environmental monitoring program was put in place. An air, slick, and water column sampling program was initiated to provide information on the physical and chemical properties of the condensate. This paper describes the primary findings of the program that involved the coordination of government, area petroleum operators, and consultants.


2022 ◽  
pp. 369-484
Author(s):  
Gerald Raabe ◽  
Scott Jortner

1975 ◽  
Vol 11 (4) ◽  
pp. 352-353
Author(s):  
A. T. Rasi-Zade ◽  
R. A. Ramazanov ◽  
B. O. Frenkel' ◽  
F. G. Rzaev

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