New operational strategy for SBR technology for total nitrogen removal from industrial wastewaters highly loaded with nitrogen

2000 ◽  
Vol 41 (12) ◽  
pp. 85-93 ◽  
Author(s):  
S. Villaverde ◽  
P. A. García Encina ◽  
M. L. Lacalle ◽  
F. Fdz-Polanco

The present work deals with the upgrading of conventional Sequential Batch Reactor (SBR) technology for treating industrial wastewater. The aim is to obtain total nitrogen removal in a single SBR by implementing short aeration cycles. The operational strategy of conventional SBR consisting of a sequence of five phases (filling, aeration, stirring, settling and withdrawing) is simplified into a four phases sequence (filling, short cycled aeration, settling and withdrawing). This operational sequence has been proven to be adequate for total nitrogen removal from high strength wastewater containing nitrogen (up to 700 mg TKN/L) and organic matter (up to 2,000 mg COD/L). Short-cycled aeration allowed for a more efficient use of the oxygen supply for nitrification and the organic carbon content present in the wastewater for denitrification. The results here reported show that initially the tested technology is feasible and can report significant cuts in operation and maintenance when compared with conventional SBR processes. Total nitrogen removal up to 79% was attained treating the effluent of an UASB process designed for treating the wastewater of a potato starch factory. Total nitrogen removal capacities ranging between 0.2 and 0.65 kg of nitrogen per cubic metre per day are reported.

2001 ◽  
Vol 44 (4) ◽  
pp. 279-286 ◽  
Author(s):  
S. Villaverde ◽  
M. L. Lacalle ◽  
P. A. García-Encina ◽  
F. Fdz-Polanco

A conventional activated sludge reactor operated with short cycled aeration was used for total nitrogen removal of UASB anaerobic reactor effluent containing nitrogen (up to 1,200 mg NKT/L) and organic matter (up to 2,000 mg COD/L). Initially the reactor was fed with synthetic water to progressively introduce the UASB effluent. This favored the acclimation of the microorganisms to the real environment. The results obtained throughout this study showed that initially the tested technology is feasible and can report significant cuts on operation and maintenance when compared to conventional activated sludge processes. Total nitrogen removal up to 66% was attained treating the effluent of an UASB process designed for treating the wastewater of a potato starch factory. Total nitrogen removal capacities ranging between 0.1 and 0.58 kg of nitrogen per cubic metre per day are reported. Short-cycled aeration allowed for a more efficient use of the oxygen supply for nitrification and the organic carbon content present in the wastewater for denitrification. This operating protocol has demonstrated serious advantages in terms of operation costs and simplicity when total nitrogen removal is wanted. Most of the existing activated sludge processes, i.e. single continuous flow reactors, can be updated for total nitrogen removal essentially at no cost, the inversion (aeration control system) is rapidly returned as reduction in energy expenditure.


2007 ◽  
Vol 55 (8-9) ◽  
pp. 59-65 ◽  
Author(s):  
A. Onnis-Hayden ◽  
P.B. Pedros ◽  
J. Reade

An experimental study investigating the nitrogen removal efficiency from the recycle stream generated in the dewatering facility of the anaerobically digested sludge at the Deer Island wastewater treatment plant (WWTP) in Boston was conducted using a single submerged attached growth bioreactor (SAGB), designed for simultaneous nitrification and denitrification. The applied nitrogen loading to the reactor ranged from 0.7 to 2.27 kg-N/m3·d, and the corresponding total nitrogen (TN) removal rate ranged from 0.38 to 1.8 kg-N/m3·d. The observed nitrification rates varied from 0.42 kg-N/m3·d to 1.45 kg-N/m3·d with an ammonia load of 0.5 kg-N/m3·d and 1.8 kg-N/m3·d, respectively. An average nitrification efficiency of 91% was achieved throughout the experiment. Denitrification efficiency varied from 55%, obtained without any addition of carbon source, to 95% when methanol was added in order to obtain a methanol/nitrate ratio of about 3 kg methanol/kg NO3−-N.


RSC Advances ◽  
2015 ◽  
Vol 5 (73) ◽  
pp. 59326-59334 ◽  
Author(s):  
A. Chen ◽  
Y. Chen ◽  
C. Ding ◽  
H. Liang ◽  
B. Yang

The presence of 2 and 5 mg L−1of tetracycline decreased total nitrogen removal. Tetracycline induced EPS release and decreased its protective role on cells. Denitrifiers instead of nitrifiers were negatively affected by tetracycline.


2010 ◽  
Vol 61 (9) ◽  
pp. 2259-2266 ◽  
Author(s):  
Styliani Kantartzi ◽  
Paraschos Melidis ◽  
Alexander Aivasidis

In the present study, a laboratory scale system, consisting of a primary settling tank, a continuous stirred tank reactor and a clarifier were constructed and operated, using wastewater from the municipal wastewater treatment plant in Xanthi, Greece. The system operated under intermittent aeration in aerobic/anoxic conditions and feeding of the wastewater once in every cycle. The unit was inoculated with sludge, which originated from the recirculation stream of the local wastewater treatment plant. The wastewater was processed with hydraulic retention time (HRT) of 12 h, in which various experimental states were studied regarding the combination of aerobic and anoxic intervals. The wastewater was fed in limited time once in every cycle of aerobic/anoxic conditions at the beginning of the anoxic period. The two states that exhibited highest performance in nitrification and total nitrogen removal were, then, repeated with HRT of 10 h. The results show that, regarding the nitrification stage and the organic load removal, the intermittent system achieved optimum efficiency, with an overall removal of biological oxygen demand (BOD5) and ammonium nitrogen in the range of 93–96% and 91–95% respectively. As far as the total nitrogen removal is concerned, and if the stage of the denitrification is taken into account, the performance of the intermittent system surpassed other methods, as it is shown by the total Kjeldahl nitrogen (TKN) removal efficiency of 85–87%. These operating conditions suppressed the growth of filamentous organisms, a fact reflected at the SVI values, which were lower than 150 ml/g.


2021 ◽  
Vol 401 ◽  
pp. 123232
Author(s):  
Changhui Zhou ◽  
Jing Bai ◽  
Yan Zhang ◽  
Jinhua Li ◽  
Zhijing Li ◽  
...  

2012 ◽  
Vol 610-613 ◽  
pp. 1454-1458
Author(s):  
Ming Fen Niu ◽  
Hong Jing Jiao ◽  
Li Xu ◽  
Yan Yu ◽  
Jian Wei

A2N is two-sludge system, by using the method that first bringing up the cultivation of denitrifying phosphorus removing bacteria (DPB) and nitrification biofilm separately then connecting them, which can start up A2N system successfully. Nitrification biofilm was cultivated in a sequencing batch reactor (SBR). After 30 days, NH4+-N effluent concentration steadily stayed below 0.5mg·L-1.In another SBR, the activated sludge for the enrichment of DPB is from the anaerobic tank, which was firstly operated under anaerobic/aerobic (A/O) condition. After 20 days, PAOs was successfully enriched. Then, the activated sludge was conducted under anaerobic/anoxic/aerobic (A/A/O) condition, maintaining the anaerobic time, gradually increased anoxic time and induced aerobic time. After 30 days DPB was successfully enriched, two phases totally take 50 days. The removal efficiency of total nitrogen and phosphorus are above 85 % and 95 %, so that A2N system was started up successfully.


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