tubing material
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2021 ◽  
Vol 3 (3) ◽  
pp. 11-23
Author(s):  
M. T. Tleshev ◽  
V. A. Baimbetov

The relevance of this work is caused by the need to reduce operating costs in the group of companies of NC KazMunayGas JSC in general and in Ozenmunaigas JSC in particular by increasing the service life of the tubing used. In this regard, the purpose of research and testing was to select the optimal tubing material for each group of wells. Correct grouping of wells (PSL zoning) is also important for the selection of the optimal tubing material. The article indicates the methodology and characteristics for the distribution of wells into groups (PSL zoning). analysis of the causes (wiping, corrosion) contributing to the rapid wear of tubing in the fields of JSC Ozenmunaigas, and recommendations for their solution.


2021 ◽  
Author(s):  
Hazirah Abdul Uloom ◽  
Asba Madzidah Abu Bakar ◽  
M. Mifdhal Hussain ◽  
Fuziana Tusimin ◽  
Zaidi Rahimy M. Ghazali ◽  
...  

Abstract Based on the production data from first development campaign in 2017, contamination reading of CO2 and H2S from gas production wells were observed increasing from 3% to 10% and from 3ppm to 16ppm respectively within one year production. These findings have triggered the revisit in 2019 development campaign optimization strategy in terms of material selection, number of wells, reservoir targets, and completion design. Thus, tubing material was upgraded to HP1-13CR for the upper part of tubing up to 10,000 ft-MDDF (feet measure depth drilling rig floor) to avoid SSC risk due to the geostatic undisturbed temperature is less than 80 deg C, however the material of deeper tubing remains as 13CR-L80 as per 2017 campaign. Moreover, the mercury content from first campaign was observed to be above threshold limit from intermediate reservoir based on mercury mapping exercise done in August 2018.As the mercury removal system is not incorporated in the surface facilities, the mercury reading from the well in the 2019 campaign need a close monitoring during well testing so that appropriate action can be taken in case the recorded contaminant reading is high. Dedicated zonal sampling plan to be performed if the commingle zone (total) mercury reading was recorded to be above the threshold limit, and that zones will be shut off to preserve the surface facilities. Opportunity was grabbed to optimize number of wells by completing both shallow and intermediate sections in a single selective completion to maximize the project value. However, this combination will lead to major challenges during operation due to the huge difference in reservoir pressure and permeability contrast in each perforated reservoir as the required overbalanced pressure of completion brine for shallow reservoir is much lesser than the requirement for the mildly overpressure intermediate reservoir. Thus, a potential risk of severe losses and well control is present at shallow reservoir. To mitigate this risk, loss circulation material was pre-spotted in the TCP (Tubing conveyed perforation) BHA prior to fire the gun to allow for self-curing process should losses take place. During the first development campaign, the completion tubing was running in hole in two stages. The lower completion was deployed via drill pipe and the perforated zones was secured with fluid loss device located between lower completion tubing and gravel pack packer. The upper completion tubing was then deployed and tied back to the lower completion packer. This approach was applied as mitigation to prevent fluid losses and to ensure the tubing can be safely deployed to the intended final depth. However, based on the actual performance and losses rate data during the first campaign, the completion design in second campaign was optimized and deployed in single stage. Since shallow and intermediate reservoir were combined in multiple production zones where five SSD (Sliding Side Door) were installed, the slickline option to set packer was waived due to the risk of setting tubing plug in deep wells. Pump out plug was considered as an option but then dropped due to high hydrostatic pressure. The packer setting pressure was too close to plug shear pressure. Therefore, a self-disappearing plug was utilized as it did not require any slickline intervention and can be ruptured by pressure cycle. With this option, risk of pre-mature rupture of plug was eliminated. The paper will discuss in detail each challenge mentioned above together with details calculation that was performed throughout evaluation and selection processes prior best solution being selected as these optimizations resulted in nearly three days saving of rig time, contributing to 2.6% of well cost reduction and the required number of wells were optimized to be three instead of four wells. Moreover, a safer production life of wells by selecting a suitable tubing material and eliminating the risk of mercury production above the above threshold limit.


Materials ◽  
2021 ◽  
Vol 14 (15) ◽  
pp. 4105
Author(s):  
Soon-Hyeok Jeon ◽  
Dong-Seok Lim ◽  
Jinsoo Choi ◽  
Kyu-Min Song ◽  
Jong-Hyeon Lee ◽  
...  

The purpose of this work is to quantify the effects of dissolved zinc cations on corrosion and release rates from a pre-filmed Alloy 690 steam generator tubing material that was subsequently exposed to water containing zinc. The corrosion tests were performed in circulating 2 ppm Li and 1000 ppm B water without and with 60 ppb zinc at 330 °C. Gravimetric analyses and oxide characterization revealed that the corrosion rates, release rates, and oxide thicknesses decreased by subsequent exposure of the pre-filmed Alloy 690 to zinc. These benefits are attributed to the formation of a chromium-rich inner oxide layer incorporating zinc.


2021 ◽  
Author(s):  
M. Farriz Noordin ◽  
Sylvia Mavis James Berok ◽  
Haydn Brent Sinanan ◽  
M. Farhan Suratman ◽  
Oka Fabian ◽  
...  

Abstract PETRONAS has undertaken a large EOR project offshore Malaysia involving the use of Immiscible Water-Alternating-Gas (iWAG) wells for fluid injection. These iWAG injection wells will allow the alternate injection of both treated seawater and hydrocarbon gas. A significant concern for these wells is tubing corrosion resistance and integrity for over a 25-year injection life. The initial conceptual design for the iWAG injection tubing utilized Glass Reinforced Epoxy (GRE) & 25Cr tubing material due to the presence of dissolved oxygen in the injected water. The use of these materials present challenges due to limitations in downhole flow device installation with the GRE tubing and high cost of 25Cr tubing. The project team searched for alternative, fit for purpose materials to meet the project's requirements. Based on the recent PETRONAS success case of 17Cr utilization, the team examined the possibility of using 17Cr or lower grade CRA material for injection purposes. By pioneering the first application of 15Cr OCTG as an iWAG injection tubing material in the world, several risks had to be considered. Additionally, all risks had to be mitigated via various approaches ranging from detailed engineering planning to field execution and operation. The process of selecting this metallurgy involved criteria such as cost, performance, manufacturability and operational execution. The selection methodology included a comprehensive evaluation and recommendation process that consisted of: Evaluation of currently used metallurgical properties and limitations Identification of alternatives based on operating conditions, cost and manufacturing constraints Metallurgy qualification through comprehensive laboratory testing. Conducting tubing installation risk analysis Reviewing tubing operational, intervention and abandonment scenarios throughout the well life cycle The successful selection and installation of 15Cr was attributed to: The metallurgy selection, tubing procurement and installation process involving multidisciplinary and multifunctional groups both internal and external to PETRONAS. Rigorous testing at two separate laboratory facilities yielding test results which met and exceeded the required performance criteria. A 15Cr tubing make up efficiency of 100%. Impressive performance during operations resulting in a gross running speed of 371 ft/hr versus an average pipe running speed of 810 ft/hr. Use of low penetration dies to prevent slippage during tubing connection make up. This was critical since CRA material is very sensitive to scratching during contact with metal equipment. This potential metal scratching can lead to corrosion. On time delivery of 15Cr tubing from the OCTG provider ensuring sufficient time for preparation of completion accessories prior to offshore load out. Utilization of 15Cr as an alternative to Duplex and Glass Reinforced Epoxy (GRE) materials has also contributed a direct cost saving of 27% to the project.


2021 ◽  
Author(s):  
Bruce Reichert ◽  
Sebastian Cravero ◽  
Martin Valdez ◽  
Jorge Bunge

Abstract A new coiled tubing (CT) failure mechanism has appeared in the past two to three years. The failures occur in CT strings used for frac plug milling in extend reach horizontal wells. The objective of this paper is to investigate a possible cause for these failures. The primary emphasis is analyzing the dynamic response of the CT to axial vibrations induced by a downhole extended reach tool [1], and the resulting tubing material response leading to failure.


2019 ◽  
Vol 70 (4) ◽  
pp. 1162-1166
Author(s):  
Ibrahim Naim Ramadan ◽  
Eugen Victor Laudacescu ◽  
Maria Popa ◽  
Loredana Irena Negoita

The purpose of the heat transfer analysis at the level of the technological furnace in radiation section was to determine the medium temperature on the outside wall of the pipeline through which the effluent is processed. It is important to keep an outside temperature of the wall of the duct below the maximum allowable temperature at which this carburizing process takes place. Thus, the temperature calculated on the outside pipe wall is 523.5 oC and the maximum allowable temperature of the outside pipe wall is 595.5oC. The carburizing process leads to the modification of the thermal conductivity of the tubing material. Therefore, if steel is enriched with carbon, thermal conductivity decreases.


Author(s):  
Kraig D. Warren

The purpose of the study was to find an alternative supply of material for high pressure tubing used in the manufacture of plastic in Low Density Polyethylene (LDPE) plants. The material selected by A&A Machine & Fabrication, LLC was HS220-27Ca4, which is manufactured by TimkenSteel. The HS220-27Ca4 material is a fine-grain, forged rolled alloy with optimal chemistry of medium carbon and a balance of chromium, nickel and molybdenum to achieve ultra-high strength and toughness. The material was laboratory tested to fatigue standards defined by ASME Section VIII Division 3 Article KD-3. In addition, the material was processed by A&A Machine & Fabrication, LLC to autofrettage requirements set forth in ASME Section VIII Division 3 Article KD-5. To satisfy industry standards and customer specifications, dimensional and non-destructive test data was gathered throughout the fabrication process. This information and comparative chemistry data is presented and reviewed as a means to demonstrate acceptance of HS220-27Ca4 for use in LDPE process.


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