drill pipe
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2022 ◽  
Vol 15 (2) ◽  
Author(s):  
Yonglong Wang ◽  
Zaijiang Yu ◽  
Zhenfeng Wang ◽  
Yuning Sun ◽  
Bo Lu ◽  
...  

2021 ◽  
Author(s):  
Thad Nosar ◽  
Pooya Khodaparast ◽  
Wei Zhang ◽  
Amin Mehrabian

Abstract Equivalent circulation density of the fluid circulation system in drilling rigs is determined by the frictional pressure losses in the wellbore annulus. Flow loop experiments are commonly used to simulate the annular wellbore hydraulics in the laboratory. However, proper scaling of the experiment design parameters including the drill pipe rotation and eccentricity has been a weak link in the literature. Our study uses the similarity laws and dimensional analysis to obtain a complete set of scaling formulae that would relate the pressure loss gradients of annular flows at the laboratory and wellbore scales while considering the effects of inner pipe rotation and eccentricity. Dimensional analysis is conducted for commonly encountered types of drilling fluid rheology, namely, Newtonian, power-law, and yield power-law. Appropriate dimensionless groups of the involved variables are developed to characterize fluid flow in an eccentric annulus with a rotating inner pipe. Characteristic shear strain rate at the pipe walls is obtained from the characteristic velocity and length scale of the considered annular flow. The relation between lab-scale and wellbore scale variables are obtained by imposing the geometric, kinematic, and dynamic similarities between the laboratory flow loop and wellbore annular flows. The outcomes of the considered scaling scheme is expressed in terms of closed-form formulae that would determine the flow rate and inner pipe rotation speed of the laboratory experiments in terms of the wellbore flow rate and drill pipe rotation speed, as well as other parameters of the problem, in such a way that the resulting Fanning friction factors of the laboratory and wellbore-scale annular flows become identical. Findings suggest that the appropriate value for lab flow rate and pipe rotation speed are linearly related to those of the field condition for all fluid types. The length ratio, density ratio, consistency index ratio, and power index determine the proportionality constant. Attaining complete similarity between the similitude and wellbore-scale annular flow may require the fluid rheology of the lab experiments to be different from the drilling fluid. The expressions of lab flow rate and rotational speed for the yield power-law fluid are identical to those of the power-law fluid case, provided that the yield stress of the lab fluid is constrained to a proper value.


Author(s):  
Quoc Anh Tran ◽  
Van Tu Duong ◽  
Hoang Long Phan ◽  
Van Sy Le ◽  
Tan Tien Nguyen

2021 ◽  
Author(s):  
Haochen Han ◽  
Yong Zhang ◽  
Jia Chen ◽  
Qi Sun ◽  
Zhimeng Fang ◽  
...  

Abstract High-speed wired drill pipe and its corresponding communication technology not only can achieve high-speed transmission rate and high-capacity, but also can realize real-time monitoring and dual-way communication in whole section, which can prevent downhole problems effectively. As a series system, the homogeneity and robustness of these wired drill pipes are crucial. This paper focuses on how to overcome the difficulty in manufacturing process of information drill pipe and complete the validation test. In order to guarantee the quality of information drill pipe and satisfy the technological requirements of mass production, we optimize the manufacturing process and put forward reasonable test techniques. The optimizations of manufacturing process include the analysis on constant tension of pressure pipe, quantitative cutting pipe and perforation in pipe nozzle. The testing techniques includes magnetic coupling coil impedance test, high pressure test, communication performance test of both single pipe and series system. The test result can be judged and evaluated by the attenuation value of the signal attenuation test and the signal reflection waveform as well as sealing reliability. With the help of the optimization of the manufacturing process and the application of new tooling, the quality and robustness of information drill pipe is improved obviously. Pass rate in primary assembly is increased from 70% to 92%. After the second assembly, pass rate can be increased to 99.5%. Besides, the work efficiency is greatly improved and the process requirements of mass production are satisfied. The validation test can screen out the drill pipe with poor quality and performance effectively thus to improve the reliability of the whole system. By means of the improvement of manufacturing and the validation test, the comprehensive pass rate of information drill pipes is increased from 84% to 95%. During three field tests in Jilin and Daqing Oilfield, the information drill pipes functioned well and accomplished all the test tasks successfully. High-speed wired drill pipe can improve the downhole data transmission on a large margin. The theorical transmission rate can be up to 100 kbps, 10,000 times as much as the traditional mud impulse telemetry. The manufacturing optimization and test technology can guarantee the performance and realize downhole data highway.


2021 ◽  
Author(s):  
Kimikazu Tsusaka ◽  
Tatsuya Fuji ◽  
Motohiro Toma ◽  
Kengo Fukuda ◽  
Michael Alexander Shaver ◽  
...  

Abstract The 3,000 ft long lateral holes drilled through water-injected area in the carbonate reservoir in the offshore Abu Dhabi have been forced to implement hard backreaming. The abnormal extra operational time has been taken due to poor performance in the operation to pull out a bottomhole assembly after drilling to the total depth. The study aims to analyze root-causes of the hard backreaming through the carbonate reservoir in the studied field. The speed of tripping-out was analyzed every stand of drill pipe by using time domain data of movement of traveling block. The correlations between the speed of tripping-out and rock characteristics such as porosity and constituent minerals in rocks were investigated. Hole shape was analyzed in the representative intervals of low trip-out speed using 16-sector caliper derived from azimuthal density logging. Stress concentration around the borehole wall was also analyzed using geomechanical model. The investigation revealed that hole shrinkage due to plastic deformation of the borehole wall was the most possible root-cause of the hard backreaming in the carbonate reservoir. Namely, BHA had to ream up deformed borehole wall in tripping-out. From the viewpoint of rock characteristics, the speed of tripping-out was found to be lower in the specific geologic layers with higher content of dolomite. This is because dolomite rocks cause larger resistance in reaming it in tripping-out since the strength of dolomite rocks is larger than that of limestone. Based on our findings, use of reamers on bit is found to be the better solution to improve the tripping-out performance in the problematic geologic layers instead of conventional operational attempts such as spotting of acid and use of high viscous fluids in hole cleaning. In addition, optimization of the design and position of reamers and stabilizers is essential to succeed in the future 10,000 ft long extended-reach wells in the studied oil field.


2021 ◽  
Author(s):  
Ola Mohamed Balbaa ◽  
Hesham Mohamed ◽  
Sherif Mohamed Elkholy ◽  
Mohamed ElRashidy ◽  
Robert Munger ◽  
...  

Abstract While drilling highly depleted gas reservoirs with a very narrow drilling window, Common drilling methods like utilizing loss of circulation pills, wellbore strengthening materials and managed pressure drilling (MPD) are being used in several reservoirs, yet it cannot be successful or cost effective if applied in a traditional manner. Innovative approaches to enable drilling wells in highly depleted reservoir in the Mediterranean deep water were adopted. The approaches incorporated design changes to the well and Bottom hole assembly (BHA), optimized drilling practices, and unconventional use of MPD while drilling and cementing production liner. Well design change in comparison to offset wells to allow drilling the reservoir in one hole section. Several design changes were considered in the BHA and drilling fluids to prevent as well as mitigate losses and differential sticking risks. From the BHA viewpoint, one of the key successful prevention measures was maximizing the standoff to reduce the contact area with the formation, this was achieved through utilizing spiral heavy wall drill pipe (HWDP) instead of drill collars in addition to a modeled placement of stabilizers and roller reamers. While on the drilling fluid side, Calcium carbonate material was added to strengthen wellbore, prevent losses and avoid formation damage. Particle size up to 1000 micron and concentration up to 40ppb was used to strengthen the depleted sands dynamically while drilling. Furthermore, as mitigation to stuck pipe, Jar and accelerator placement was simulated to achieve optimum impulse and impact force while maintaining the Jar above potential sticking zone. Whereas to address the consequence of a stuck pipe event, disconnect subs were placed in BHA to allow for recovering the drill string efficiently. MPD was first introduced in the Mediterranean in 2007 and continued to develop this well-known technique to mitigate various drilling challenges. For this well, MPD was one of the key enabling factors to safely drill, run and cement the production liner. Surface back pressure MPD allowed using the lowest possible mud weight in the hole and maintaining downhole pressure constant in order to manage the narrow drilling window between the formation pressure and fracture pressure (less than 0.4 ppg). MPD was also applied for the first time for running and cementing the production liner to prevent losses and achieve good cement quality which is a key to successful well production.


Author(s):  
Hicham Ferroudji ◽  
Ahmed Hadjadj ◽  
Titus Ntow Ofei ◽  
Rahul Narayanrao Gajbhiye ◽  
Mohammad Azizur Rahman ◽  
...  

AbstractTo ensure an effective drilling operation of an explored well, the associated hydraulics program should be established carefully based on the correct prediction of a drilling fluid’s pressure drop and velocity field. For that, the impact of the drill string orbital motion should be considered by drilling engineers since it has an important influence on the flow of drilling fluid and cuttings transport process. In the present investigation, the finite volume method coupled with the sliding mesh approach is used to analyze the influence of the inner cylinder orbital motion on the flow of a power-law fluid (Ostwald-de Waele) in an annular geometry. The findings indicate that the orbital motion positively affects the homogeneity of the power-law axial velocity through the entire eccentric annulus; however, this impact diminishes as the diameter ratio increases. In addition, higher torque is induced when the orbital motion occurs, especially for high values of eccentricity and diameter ratio; nonetheless, a slight decrease in torque is recorded when the fluid velocity increases.


Materials ◽  
2021 ◽  
Vol 14 (23) ◽  
pp. 7379
Author(s):  
Hao Yin ◽  
Jian Liang ◽  
Xiaoyong Ren ◽  
Jie Zhao ◽  
Xin He ◽  
...  

Coating on the surface is one of the main ways to improve the corrosion resistance and wear resistance of materials. In this work, the corrosion, erosion, and wear resistance of WC–10Co4Cr coating and 27CrMoV substrate were compared by simulating the actual working conditions of the drill pipe. The simulation results show that the most serious corrosion occurred at the pipe body and the dominating erosion arose at the pipe joint closing to the inlet of the flow field. WC–10Co4Cr coating has excellent protection to 27CrMoV substrate, resulting in a 400 mV increase in corrosion potential, a two-orders-of-magnitude decrease in the corrosion current, and four times the improvement of the impedance value. The erosion resistance of the WC–10Co4Cr coating increased to more than 30% higher than that of the 27CrMoV substrate. The friction coefficient of the WC–10Co4Cr coating was much lower than that of the 27CrMoV substrate, and the wear resistance of the coating was higher than that of the substrate.


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