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2021 ◽  
Vol 2074 (1) ◽  
pp. 012090
Author(s):  
GuangLiang Fan ◽  
WeiFu Qi ◽  
Yong Yu ◽  
ShuSen Liu ◽  
Ting Yuan

Abstract The outdoor control cabinet of intelligent substation includes the central control cabinet and the intelligent control cabinet. The internal integrated circuits and electronic components are easily affected by the environmental humidity. Through the operation and maintenance data statistics, it is found that the existing heating and dehumidification system in the control cabinet can not fully meet the humidity requirements in the cabinet. In view of this problem, this paper analyzes the factors leading to the increase of humidity in the cabinet, puts forward the research on the improvement of moisture-proof technology of JIS control cabinet in 220kV substation based on big data. In an environment where the air temperature changes rapidly, the test data verify that the moisture-proof technology of JIS control cabinet in 220kV substation based on big data can effectively reduce the humidity in the intelligent control cabinet, and effectively ensure the safe operation of electronic equipment in the intelligent control cabinet.


2021 ◽  
Vol 2005 (1) ◽  
pp. 012092
Author(s):  
Kang Yin ◽  
Xinying Huang ◽  
Tingting Zhong ◽  
Qingwei Chen ◽  
Xingxing Tong

Energies ◽  
2021 ◽  
Vol 14 (12) ◽  
pp. 3659
Author(s):  
Andrzej Szajna ◽  
Mariusz Kostrzewski ◽  
Krzysztof Ciebiera ◽  
Roman Stryjski ◽  
Waldemar Woźniak

Industry 4.0, a term invented by Wolfgang Wahlster in Germany, is celebrating its 10th anniversary in 2021. Still, the digitalization of the production environment is one of the hottest topics in the computer science departments at universities and companies. Optimization of production processes or redefinition of the production concepts is meaningful in light of the current industrial and research agendas. Both the mentioned optimization and redefinition are considered in numerous subtopics and technologies. One of the most significant topics in these areas is the newest findings and applications of artificial intelligence (AI)—machine learning (ML) and deep convolutional neural networks (DCNNs). The authors invented a method and device that supports the wiring assembly in the control cabinet production process, namely, the Wire Label Reader (WLR) industrial system. The implementation of this device was a big technical challenge. It required very advanced IT technologies, ML, image recognition, and DCNN as well. This paper focuses on an in-depth description of the underlying methodology of this device, its construction, and foremostly, the assembly industrial processes, through which this device is implemented. It was significant for the authors to validate the usability of the device within mentioned production processes and to express both advantages and challenges connected to such assembly process development. The authors noted that in-depth studies connected to the effects of AI applications in the presented area are sparse. Further, the idea of the WLR device is presented while also including results of DCNN training (with recognition results of 99.7% although challenging conditions), the device implementation in the wire assembly production process, and its users’ opinions. The authors have analyzed how the WLR affects assembly process time and energy consumption, and accordingly, the advantages and challenges of the device. Among the most impressive results of the WLR implementation in the assembly process one can be mentioned—the device ensures significant process time reduction regardless of the number of characters printed on a wire.


Author(s):  
Claudia BORZEA ◽  
Adrian SAVESCU ◽  
Iulian VLADUCA ◽  
Adrian STOICESCU

The paper presents the functioning regimes of a 132 kW asynchronous three-phase machine, used for the expander-generator system in a compressed air energy storage facility. The installation consists of a 110 kW twin-screw electro-compressor, which supplies pressurized air up to ~16 bar into a 50 cubic meters storage vessel. The compressed air is afterwards released from the reservoir into expander’s inlet, spinning its shaft. When the expander’s shaft spins the electric machine over its synchronous speed, this one enters in generator mode, supplying electric power into the grid. Two power analysers installed on the automation control cabinet monitor the generated/absorbed power and the power supplied/consumed by the system from the grid. Using the data acquired by means of PLC during commissioning tests, we plotted the power curves, differential pressure and significant temperatures, as well as the electric machine’s speed.


Author(s):  
A. I. Repnikov ◽  
M. P. Kukhtik

Automated control system for children's carousel has been developed and manufactured. Control cabinet for children's carousel has been designed and control program for programmable logic controller has been written. Control system increases operation reliability of children's carousel and secures ability to control rotation speed of racks.


2020 ◽  
Vol 2 (1) ◽  
Author(s):  
Hangzhe DONG ◽  
Yazhen ZHANG ◽  
Wantong HU ◽  
Zhenhua BA ◽  
Yanyan ZHANG

With the benefit fierce competition in the steel industry market in recent years, double cold reduction products have been developed towards strength improvement and thickness reduction. The traditional cold-rolling lubrication process with a fixed flow rate and concentration cannot solve the problems which cover uncontrollable shape of strip product and the excessive consumption of lubricating oil. Moreover,based on the analysis of the traditional direct application lubrication system of double cold reduction, a set of design scheme suitable for the emulsion pipeline direct mixing lubrication system of double cold reduction unit is proposed.The design complete the selection of key components which include the static mixer and atomization nozzle selection, pump and oil pump design selection, pipeline design selection, flow type selection, pressure gauge selection, electronic control cabinet design selection and other aspects. Equipment of the emulsion pipeline direct mixing lubrication system of double cold reduction has been developed. Comparing with characteristics of the traditional direct aplication lubrication system, the emulsion pipeline direct mixing lubrication system was better applied to the production practice of a 1220 double cold reduction mill. The consumption of ton of steel was reduced by 9.6%. The rolling energy consumption and oil consumption comprehensive costs decreased by 10.7%, and the strip steel section thickness difference was reduced by 19.3%. In addition, the plate shape quality defect rate decreased by 25.6 %, otherwise creating a large economic benefit for the unit and promoting the application value.


Energies ◽  
2020 ◽  
Vol 13 (3) ◽  
pp. 601 ◽  
Author(s):  
Marit Sigfrid Bakka ◽  
Erling Kristian Handal ◽  
Torgrim Log

During an air separation unit shut-down in a methanol production plant, a stop signal was sent to the control cabinet of a synchronous motor for a booster compressor. The control cabinet stopped magnetizing the rotor, while the system logic ensured that the power circuit breakers for the start reactor coils were opened, in order to be ready for the next start-up. Unintentionally, the circuit breaker was still connected (i.e., power was let through the reactors for a prolonged time period), which led to extensive overheating. Subsequently, the central control room received an unaddressed sub-station smoke alarm, and plant operators were sent out to locate the possible source of smoke. The accessible rooms were searched, and traces of smoke were confirmed. The Emergency Response Organization (ERO) was mustered and, through inspection, the Emergency Response Team (ERT) realized that the smoke originated from a ground floor high-voltage room. Fire hoses were arranged for fire extinguishing, and the ERT withdrew to wait for the room to be electrically isolated. About one minute after briefly opening the only set of doors to the high-voltage room, flames were observed, and a quasi-smoke gas explosion violently forced both door blades open and released a substantial fire ball. Personnel had been in the risk zone shortly before the explosion, but luckily no personnel were hit by the slamming door blades or the emerging flames. The incident revealed several learning points related to improper maintenance, ambiguous smoke alarm, lack of flame detectors in the high-voltage room, insufficient risk understanding and training regarding electrically related fire incidents, and the absence of an automatic fire suppression system. In plants processing hydrocarbons, the safety focus regarding hydrocarbon fire and explosion risk is paramount. However, risks related to electrical accidents and compartment fire dynamics (e.g., backdraft and smoke gas explosion) should also be given proper attention.


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